SUMMARY REPORT • FLUE GAS DESULFURIZATION SYSTEMS • MARCH - APRIL 1976
Table
  1  Summary List of F6D Systems
  2  Status of FGD Systems
  3  Performance Description for Operational FGD Systems
  4  Number and Total MW of FGD Systems
  5  Summary of FGD Systems by Company
  6  Summary of FGD Systems by Vendor
  7  Summary of New and Retrofit FGD Systems by Process
  8  Summary of Operating FGD Systems by Process and Generating Units
  9  Summary of Sludge Disposal Practices for Operational FGD Systems
                                           •
 10  Summary of FGD Systems by Process and Regulatory Class
 11  Summary of Operational FGD Systems
 12  Summary of FGD Systems Under Construction
 13  Summary of Planned FGD Systems
 14  Summary List of FGD Systems in the Early Planning Stages
 15  Status of FGD Systems in the Early Planning Stages
 16  FGD System Operations That Have Been Terminated or Shut Down Indefinitely

     Definitions
                                        Page
                                          3
                                          9
                                         33
                                        131
                                        135
                                        139
                                        143
                                        147
                                        151
                                        155
                                        161
                                        165
                                        169
                                        177
                                        181
                                        187

                                        207
            Prepared by
PEDCo-Environmental Specialists, Inc.
      Suite 13, Atkinson Square
       Cincinnati, Ohio  45246
               Prepared for
 Division of Stationary Source Enforcement
                   and
Industrial Environmental Research Laboratory
   U.S.  ENVIRONMENTAL PROTECTION AGENCY
          Research Triangle Park,
           North Carolina  27711
                                       Contract No.  68-02-1321
                                             Task No.  28

-------
          Table 1
SUMMARY LIST OF FGD SYSTEMS

-------
                                           TABLE 1
                                SUMMARY LIST OF FGO SYSTEMS
   FGD STATUS REPORT 05/76

   1.0. NUMBER AND COMPANY NAME
                                         UNIT NAME
                                                                            LOCATION
                                                                                                  START UP DATE   STATUS
                                                                                                                           REG
                                                                                                                           CLASS
     1 ALABAMA ELECTRIC COOP
     2 ALABAMA ELECTRIC COOP
     3 ALLEGHENY POWER SYSTEM
     4 ALLEGHENY POWER SYSTEM
     5 ARIZONA ELECTRIC POWER COOP
     6 ARIZONA ELECTRIC POWER COOP
     7 ARIZONA PUBLIC  SERVICE
     6 ARIZONA PUBLIC  SERVICE
     9 ARIZONA PUBLIC  SERVICE
    10 ARIZONA PUBLIC  SERVICE
    11 ARIZONA PUBLIC  SERVICE
    12 BASIN  ELECTRIC  POWER  COOP
    13 BASIN  ELECTRIC  POWER  COOP
    14 BASIN  ELECTRIC  POWER  COOP
    15 BASIN  ELECTRIC  POWER  COOP
    16 BASIN  ELECTRIC  POWER  COOP    '
    17 BRAZOS ELECTKIC  POwER  COOP
    IB CENTRAL  ILLINOIS LIGHT CO.
    19 CENTRAL  ILLINOIS LIGHT CO.
    20 CENTRAL  ILLINOIS LIGHT CO.
    21 CENTRAL  ILLINOIS PUBLIC SERV
    22 CINCINNATI GAS  & ELECTRIC CO.
    23 CINCINNATI TAS  8 ELECTRIC CO.
    24 COLUMBUS  A SOUTHERN OHIO ELEC
    25 COLUMBUS  & SOUTHERN OHIO ELEC
    26 COLl'MHUS  * SOUTHERN OHIO ELEC
    27 COLUMOUS  g, SOUTHERN OHIO ELEC
    26 COMMONWEALTH EOISON
    29 COMMONWEALTH EDISON
    30  DETROIT EDISON
    31  DUOUESNE  LIGHT
    32  DUOUESNE  LIGHT
    33  GENERAL MOTORS
    34  GULF POWER CO.
    35 GULF POWER CO.
                                      TOMBIGBEE NO. 2
                                      TOMUIGBEE NO. 3
                                      PLEASANTS NO. 1
                                      PLEASANTS NO. 2
                                      APACHE NO 2
                                      APACHE NO 3
                                      CHOLLA NO 1
                                      CHOLLA NO 2
                                      FOUR CORNERS NO.  4
                                      FOUR CORNERS NO.  5A
                                      FOUR CORNERS NO.  SB'
                                      BLULAH NO.  1
                                      BEULAH NO.  2
                                      MISSOURI  BASIN NO 1
                                      MISSOURI  BASIN NO 2
                                   ^.MISSOURI  BASIN NO 3
                                     .GAT  COOPERATIVE PROJECT  NO.
                                      DUCK CRCEK  NO.l
                                      DUCK CREEK  NO.2
                                      E.D.EDWAROS NO.3
                                      NLWTON NO.l
                                      EAST BEND NO 2
                                      MIAMI  FORT  NO  6
                                   .  CONESVILLE  NO  5
                                   .  CONLSVILLE  NO  6
                                   .  POSTON NO.  5
                                   .  POSTON MO.  6
                                      POWE.RTON NO. 51
                                      WILL COUNTY  NO 1
                                      ST.CLAIR NO  6
                                      ELHAMA
                                      PHILLIPS
                                      CHEVROLET PARMA 1 2 3 & 4
                                      SCHOLZ NO.  1A
                                      SCHOLZ NO. 2A
 JACKSON ALABAMA
 JACKSON ALABAMA
 BELLMONT W VIRGINIA
 BELLMONT W VIRGINIA
 COCHISE ARIZONA
 COCHISE ARIZONA
 JOSEPH CITY ARIZONA
 JOSEPH CITY ARIZONA
 FARMINGTON NEW  MEXICO
 FARMINGTON NEW  MEXICO
 FARMINGTON NEW  MEXICO
 BEULAH  NORTH DAKOTA
 BEULAH  NORTH DAKOTA
 WHEATLAND  WYOMING
 WHEATLAND  WYOMING
 WHEATLAND  WYOMING
 SAN  MIGUEL  TEXAS
 CANTON ILLINOIS
 CANTON ILLINOIS
 BAKTONVILLE  ILLINOIS
 NEWTON ILLINOIS
 RABBIT  HASH  KENTUCKY
 NORTH  BEND  OHIO
 CONESVILLE OHIO
 CONESVILLE OHIO
 ATHENS  OHIO
 ATHENS  OHIO
 PEKlN   ILLINOIS
 ROMEOVILLC ILLINOIS .
 BELLE RIVER MICHIGAN
 ELRAMA PENNSYLVANIA
 SOUTH HEIGHT PENNSYLVANIA
PARMA OHIO
CHATTAHOOCHEE  FLORIDA
CHATTAHOOCHEE  FLORIDA
1.  OPERATIONAL UNITS           H.
2.  UNITS UNDER CONSTRUCTION    5.
3.  PLANNED - CONTRACT AWARDED  6.
                                    PLANNED - LETTER OF INTENT SIGNED
                                    PLANNED - REQUESTING/EVALUATING BIOS
                                    CONSIDERING ONLY FGD SYSTEMS
A.

!'
C.
D*
E.
    BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
    S2IJ-52 !U-JrCT 1° SIAIE STANDARD ™AT I* MORE STRINGENT THAN THE FEDERAL NSPS
    BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
    OTHER
    REGULATORY CLASS UNKNOWN
  3-78
  3-79
  3-79
  3-60
  6-76
  6-79
 10-73
  6-77
  0-  0
  2-76
  0-  0
  0-81
  0-81
  1-80
  6-60
  6-63
 12-79
  6-76
  1-82
  7-79
 12-77
  1-80
  1-78
  6-76
  1-78
  0-81
  0-63
12-79
  2-72
 S-76
10-75
 7-73
 3-74
 2-75
 2-76
 3
 3
 3
 3
 4
 4
 1
 2
 6
 1
 6
 6
 6
 6
 6
 6
 3
 2
 6
 6
 5
 6
 5
 2
 3
 6
 6
 3
 1
2
1
1
1
1
1
 A
 A
 A
 A
 B
 B
 B
 B
 B
 B
 B
 B
 B
 B
 B
 B
 E
 A
 A
 C
 A
 A
 D
 B
 B
 B
 B
 C
 C
 E
 B
 B
B
C
C
                                                                                                        PEOCo-ENVIRONMENTAL

-------
                                          TABLE 1
                               SUMMARY LIST OF FGO SYSTEMS
  FGD STATUS REPORT  05/76

  1.0. NUMBER AND COMPANY NAME
                                    UNIT NAME
                                                                       LOCATION
                                                             START UP DATE   STATUS
                                                                                                                          REG
                                                                                                                          CLASS
36 GULF POWER CO.
37 INDIANAPOLIS POWER ft LIGHT
36 KANSAS CITY POWER A LIGHT
39 KANSAS CITY POWER ft LIGHT
40 KANSAS CITY POWER ft LIGHT
41 KANSAS POWER ft LIGHT
42 KANSAS POWER ft LIGHT
43 KANSAS POWER ft LIGHT
44 KANSAS POWER ft LIGHT
45 KENTUCKY UTILITIES
46 KEY WEST UTILITY BOARD
47 LOUISVILLE GAS   ELECTRIC
48 LOUISVILLE GAS   ELECTRIC
49 LOUISVILLE GAS   ELECTRIC
50 LOUISVILLE GAS   ELECTKIC
51 LOUISVILLE GAS   ELECTRIC
52 LOUISVILLE GAS   ELECTRIC
53 LOUISVILLE GAS   ELECTRIC
54 LOUISVILLE GAS   ELECTRIC
55 MINNKOTA POWER COOPERATIVE
56 MONTANA POWER CO.
57 MONTANA POkER CO.
56 MONTANA POwER CO.
59 MONTANA POuER CO.
60 NEVADA POWER
61 NEVADA POWER
62 NEVADn POWER
63 NEVADA POWER
64 NEVADA POWER
65 NEVADA POWER
66 NEVADA POWER
67 NEVADA POWER
66 NEVADA POWER
69 NEVADA POWER
70 NEW ENGLAND ELEC SYSTEM
1.
2.
3.

A.
B.
C.
0.
E.
                                                   UNITS 1 AND 2
                                 SCHOLZ NOS. IB ft 2B
                             CO. PETERSBURG NO 3
                                 HAWTHORN NO 3
                                 HAWTHORN NO 4
                                 LA CYGNE NO 1
                                 JEFFERY NO. 1
                                 JLFFERY NO. 2
                                 LAWRENCE MO 4
                                 LAMKENCE NO 5
                                 GREEN RIVER
                                 STOCK ISLAND PLANT
                                 CANE RUN NO 4
                                 CANE RUN NO 5
                                 CANE RUN NO 6
                                 MILL CREEK NO 1
                               :. HILL CREEK NO 2
                               ""MILL CREEK NO 3
                                'MILL CREEK NO 4
                                 PAOOYS hUN NO 6
                                 MILTON R. YOUNG NO.
                                 COLSTRIP NO 1
                                 CULSTRIP NO 2
                                 COLSTRIP NO.3
                                 COLSTRIP NO.4
                                 HAKKY ALLEN STATION NO.
                                 HARRY ALLEN STATION NO.
                                 HAKKY ALLEN STATION NO. 3
                                 HARHY ALLEN STATION NO. 4
                                 REIO GARDNER NO 1
                                 REID GARDNER NO 2
                                 REID GARDNER NO 3
                                 REID GARDNER NO 4
                                 WARNER VALLEY STATION NO. 1
                                 WARNER VALLEY STATION NO. 2
                                 BRAYTON POINT NO.3
                                                             1
                                                             2
                                CHATTAHOOCHEE FLORIDA
                                PETERSBURG INDIANA
                                KANSAS CITY MISSOURI
                                KANSAS CITY MISSOURI
                                LA CYGNE KANSAS
                                ST MARY KANSAS
                                ST MARY KANSAS
                                LAWRENCE KANSAS
                                LAWRENCE KANSAS
                                CENTRAL CITY KENTUCKY
                                KEY WEST FLORIDA
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                LOUISVILLE KENTUCKY
                                CENTER NORTH DAKOTA
                                COLSTRIP MONTANA
                                COLSTRIP MONTANA
                                COLSTRIP MONTANA
                                COLSTRIP MONTANA
                                N. E.  LAS VEGAS
                                N. E.  LAS VEGAS
                                N. E.  LAS VEGAS
                                N. E.  LAS VEGAS
                                MOAPA  NEVADA
                                MOAPA  NEVADA
                                MOAPA  NEVADA
                                MOAPA  NEVADA
                                ST. GEORGE  UTAH
                                ST. GEORGE  UTAH
                                SOMERSET MASSACHUSETTS
OPERATIONAL UNITS           4.
UNITS UNDER CONSTRUCTION    &.
PLANNED - CONTRACT AWARDED  6.
PLANNED - LETTER OF INTENT SIGNED
PLANNED • REQUESTING/EVALUATING BIDS
CONSIDERING ONLY FGD SYSTEMS
 3-75
 9-77
11-72
 6-72
 2-73
 6-78
 6-79
12-66
11-71
 9-75
10-72
 6-76
12-77
 9-78
 1-82
 1-61
 7-77
 7-79
 4-73
 6-77
10-75
 7-76
 7-80
 7-61
 6-83
 6-64
 6-85
 6-66
 4-74
 4-74
 6-76
 0- 0
 6-82
 6-63
 0- 0
1
2
1
1
1
9
3
1
1
1
1
2
2
5
6
6
2
3
1
2
1
2
 C
 A
 B
 B
 C
 B
 B
 D
 D
 C
 C
 C
 C
 C
 C
 C
 A
 A
 C
 B
 C
 A
 A
 A
 B
 B
 B
 B
 B
 B
 B
B
B
B
C
BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
BOILER SUBJECT To STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL-TO OR LESS STRINGENT THAN NSPS
OTHER
REGULATORY CLASS UNKNOWN
                                                                                                         PEDCo-ENVIRONMENTAL

-------
                                           TABLE 1
                                SUMMARY LIST OF FGD SYSTEMS
   FGO STATUS REPORT 05/76

   1,0. NUMBER AND COMPANY NAME
    71 NORTHERN INDIANA PUB SERVICE
    72 NORTHERN INDIANA PUB SERVICE
    73 NORTHERN INDIANA PUB SERVICE
    71 NORTHERN STATES POWER CO.
    75 NORTHERN STATES POWER CO.
    76 PENNSYLVANIA POWLR CO.
    77 PENNSYLVANIA POWER CO.
    78 PENNSYLVANIA POWER CO.
    79 PHILADELPHIA ELECTRIC CO.
    60 PHILADELPHIA ELECTRIC CO.
    81 PHILADELPHIA ELECTRIC CO.
    «2 PHILADELPHIA ELECTRIC CO.
    63 PUBLIC  SERVICE CO OF  COLORADO
    64 PUBLIC  SERVICE CO OF  NEW HEX.
    85 PUBLIC  SERVICE CO OF  NEW HEX.
    86 PUBLIC  SERVICE CO OF  NEW HEX.
    87 PUBLIC  SERVICE CO OF  NEW HEX.
    86 PUBLIC  SERVICE INDIANA
    89 PUBLIC  SERVICE INDIANA
    90 RICKENBACKCR AFO
    91 S. CAROLINA  PUB SERV  AUTHORITY
    92 S. MISSISSIPPI ELEC PWH  ASSOC
    93 S. MISSISSIPPI ELEC PUR  ASSOC
    9«t SOUTHERN CALIFORNIA EDISON
    95 SOUTHERN CALIFORNIA EDISON
    96 SOUTHERN ILLINOIS POwEK  COOP
    97 SPRIMGFIELO  CITY  UTILITIES
    96 TENNESSEE VALLEY  AUTHORITY
    99 TENNESSEE VALLEY  AUTHORITY
  100  TENNESSEE VALLEY  AUTHORITY
  101  TEXAS UTILITIES  CO.
  10?  TEXAS UTILITIES  CO.
  103  TEXAS UTILITIES CO.
  10*  TEXAS UTILITIES CO.
  105  UNITED POWER ASSOCIATION
                                     UNIT NAME
                                  BAILLY NO. 7
                                  BAILLY NO. 6
                                  MITCHELL NO 11
                                  SHEKDURNE NO 1
                                  SHERBURNE NO 2
                                  BRUCE MANSFIELD NO. 1
                                  BRUCE MANSFIELD NO. 2
                                  BRUCE MANSFIELD NO. 3
                                  CROMBY
                                  EDUYSTONE NO 1A
                                  EUDYSTONE NO IB
                                  EDDYSTONE NO 2
                                  VALMONT NO.  5
                                  SAN JUAN NO.  1
                                  SAN JUAN NO.  2
                                  SAN JUAN NO.  3
                                  SAN JUAN NO.  
-------
                                           TABLE 1
                                SUMMARY LIST OF FGD SYSTEMS
   F60 STATUS REPORT 05/76

   1.0. NUMBER AND COMPANY NAME
                                     UNIT NAME
                                                                            LOCATION
                                                                                              START UP DATE   STATUS
                                                                                                                           RE6
                                                                                                                           CLASS
   106 UNITED POWER ASSOCIATION
   107 UTAH POWER & LIGHT CO.
   108 UTAH POWER & LIGHT CO.
                                  COAL CREEK NO.  2
                                  EMERY NO.l
                                  HUNTIN6TON N0.1--
UNDERWOOD NORTH DAKOTA
EMERY COUNTY  UTAH
PRICE UTAH
11-79
 6-76
 *-7T
5
3
2
A
A
A
1.  OPERATIONAL UNITS           <*.
2.  UNITS UNDER CONSTRUCTION    5.
3.  PLANNED - CONTRACT AWARDED  6.
A.
B.
C.
0.
E.
                                PLANNED - LETTER OF INTENT SIGNED
                                PLANNED • REQUESTING/EVALUATING BIOS
                                CONSIDERING ONLY FGD SYSTEMS
BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
OTHER
REGULATORY CLASS UNKNOWN
                                                                                                        PEDCo-ENVIRONMENTAL
                                                                8

-------
       Table 2



STATUS OF FGD SYSTEMS

-------
 COMPANY

 POWER STATION
                                             TABLE 2
                                  STATUS OF FGD SYSTEMS DURING
                          05/76
                   CURRENT MONTH
1.0. NUMBER    1
ALABAMA ELECTRIC COOP
TOMBIGREE NO. 2
  225  MM - NEW
COAL   0.8- 1.5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/76
PEABODY ENGINEERING WAS AWARDED CONTRACT TO INSTALL FGD SYSTEM ON
TOMBIGBEE NO. 2. AT THE PRESENT TIME. WORK IS PROCEEDING ON THE FOUNDA-
TION OF THIS LIMESTONE SCRUBBING SYSTEM.
I.D. NUMBER    2
ALABAMA ELECTRIC COOP
TOMBIGBEE. NO. 3
  225  MM - NEW
COAL   0.8- 1.5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/79
PEABODY ENGINEERING WAS AWARDED CONTRACT TO INSTALL FGD SYSTEM ON
TOMBIGBEE NO. 3. AT THE PRESENT TIME, WORK IS PROCEEDING ON THE FOUNDA-
TION OF THIS LIMESTONE SCRUBBING SYSTEM.
I.D. NUMBER    3
ALLEGHENY POWER SYSTEM
PLEASANTS NO. 1
  625  MW - NEW
COAL   2.0- 5.0 PERCENT SULFUR
BABCOCK AND WILCOX
LIME SCRUBBING
STARTUP   3/79
THE THREE PRINCIPAL OPERATING UTILITY COMPANIES OF THE ALLEGHENY POWER
SYSTEM HAVE CONCLUDED A LONG-TERM AGREEMENT WITH THE DRAVO LIME CO. TO
SUPPLY THIOSORBIC LIME FOR THE PLANNED S02 SCRUBBERS AT PLEASANTS NOS. 1
ANij 2. THE CONTRACT FOR THIS LIME SCRUBBING PROCESS HAS BEEN AWARDED TO
BABCOCK AND WILCOX. GUARANTEED S02 AND PARTICULATE REMOVAL EFFICIENCIES
FOR THIS EMISSION CONTROL SYSTEM ARE 90 AND 99.55 PERCENT RESPECTIVELY.
I.D. NUMBER    <»
ALLEGHENY POWER SYSTEM
PLEASANTS NO. 2
  625  MW - NEW
COAL   2.0- 5.0 PERCENT SULFuR
BABCOCK AND WILCOX
LIME SCRUBBING
STARTUP   3/80
THE THREE PRINCIPAL OPERATING UTILITY COMPANIES OF THE ALLEGHENY POWER
SYSTEM HAVE CONCLUDED A LONG-TERM AGREEMENT WITH THE DRAVO LIME CO. TO
SUPPLY THIOSORBIC LIME FOR THE PLANNED S02 SCRUBBERS AT PLEASANTS NOS. 1
AND 2. THE CONTRACT FOR THIS LIME SCRUBBING PROCESS HAS BEEN - AWARDED TO
BABCOCK AND WILCOX. GUARANTEED S02 AND PARTICIPATE REMOVAL EFFICIENCIES
FOR THIS EMISSION CONTROL SYSTEM ARE 90 AND 99.55 PERCENT RESPECTIVELY.
I.D. NUMBER    5
ARIZONA ELECTRIC POWER COOP
APACHE NO 2
  200  MW - NEW
COAL  0.5- 0.8 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   6/78
LETTER OF INTENT TO INSTALL AN FGD SYSTEM WAS ISSUED TO RESEARCH COTTRELL.
ENGINEERING DESIGN WORK IS PROCEEDING. THE INITIAL SITE PREPARATION
FOUNDATION WORK IS ALREADY UNDERWAY.  THE CONCRETE FOR THE SCRUBBER TOWER
HAS ALREADY BEEN POURED.  GUARANTEED S02 AND PARTICULATE REMOVAL EFFI-
CIENCIES ARE 50 AND 99.<» PERCENT RESPECTIVELY.
                                                                                                                PEDCo- ENVIRONMENTAL
                                                                 11

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
                                                                05/76
                       CURRENT MONTH
1.0. NUMBER    6
ARIZONA ELECTRIC POWER COOP
APACHE. MO 3
  205  MW - NEW
COAL   0.5- 0.6 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   6/79
    LETTER OF INTENT TO INSTALL AN FGD SYSTEM WAS ISSUED TO RESEARCH COTTRELLt
    THE ENGINEERING DESIGN WORK IS PROCEEDING. THE INITIAL SITE PREPARATION
    WORK IS ALREADY UNDERWAY. THE CONCRETE FOR THE SCRUBBER TOWER FOUNDATION
    HAS ALREADY BEEN POURED. GUARANTEED S02 AND PARTICULATE REMOVAL EFFI-
    CIENCIES ARE SO AND 99.4 PERCENT RESPECTIVELY.
I.D. NUMBER    7
ARIZONA PUBLIC SERVICE
CHOLLA NO 1
  115  MW - RETROFIT
COAL   0.44-1 PERCENT SULFUR
RESEARCH COTTRCLL
LIMESTONE SCRUBBING
STARTUP  10/73
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
    FGD SYSTEM HAS BEEN OPERATIONAL SINCE NOVEMBER 1973.  RELIABILITY FOR
    MODULES A AND B DURING THE MONTH OF APRIL WAS 99 AND  97.4 PERCENT RE-
    SPECTIVELY. RELIABILITY FOR BOTH MODULES HAS AVERAGED IN EXCESS OF 90 AND
    63 PERCENT RESPECTIVELY DURING THE PERIOD OF APRIL 1979 TO JANUARY 1976.
I.D. NUMBER    B
ARIZONA PUBLIC SERVICE
CHOLLA NO 2
  250  MW - NEW
COAL   0.44-1 PERCENT SULFUR
RESEARCH COTTRELL
LIKE.STONE SCRUBBING
STARTUP   6/77
    RESEARCH COTTRELL WAS AWARDED A CONTRACT TO INSTALL FGO SYSTEM ON
    CHOLLA NO. 2.  AND IS PRESENTLY WORKING ON THE DESIGN PHASE OF THIS
    PROJECT. ENGINEERING IS SUBSTANTIALLY COMPLETE.   CONSTRUCTION IS
    UNDERWAY.
I.D. NUMBER    9
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 4
  755  MW - RETROFIT
COALi 0.7 - 0.75S SULFUR (AVG)
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    THIS 755 HW UNIT WILL BE CONTROLLED PENDING THE OUTCOME OF TESTS TO BE
    MADE ON THE PROTOTYPE 160 MW FGO MODULE NOW BEING INSTALLED ON UNIT s.
I.D. NUMBER   10
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 5A
  160  MW - RETROFIT
COAL. 0.7 PERCENT SULFUR
SCE
LIME SCRUBBING
STARTUP   2/76
    THIS 160 MW SYSTEM HAS BEEN MOVED FROM THE MOHAVE STATION OF SOUTHERN
    CALIFORNIA EDISON WHERE THE SYSTEM WAS PREVIOUSLY TESTED. THE SYSTEM
    WILL TREAT APPROXIMATELY 20 PERCENT OF THE FLUE GAS FROM UNIT NO.  5,
    RATED AT 755 MW(NET). THE ENGINEERING AND CONSTRUCTION WORK HAS BEEN
    COMPLETED. THE SYSTEM BECAME OPERATIONAL ON FEBRUARY 17. 1976. THE EXPER-
    IMENTAL SCRUBBER WAS TAKEN OUT OF SERVICE IN MID-APRIL FOR A SCHEDULED
    BOILER OVERHAUL.
                                                                                                              PEDCo- ENVIRONMENTAL
                                                                12

-------
 COMPANY
                                             TABLE 2
                                  STATUS OF FGO SYSTEMS DURING
                          OS/76
 POWER STATION                                           CURRENT MONTH '
1.0. NUMBER   11
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. SB
  595  MW - RETROFIT
COALt 0.7 - 0.75i SULFUR (AVG)
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
THE BALANCE OF THIS 755 HW UNIT WILL BE CONTROLLED PENDING THE OUTCOME
OF TESTS TO BE MADE ON THE PROTOTYPE 160 HW FGO MODULE NOW BEING INSTALLED
NO START-UP DATE HAS BEEN SCHEDULED.
I.D. NUMBER   12
BASIN ELECTRIC POWER COOP
BEULAH NO. 1
  i»50  MW • NEW
COAL 1.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/81
THE UTILITY IS NOW INVESTIGATING VARIOUS FGD PROCESSES. THIS NEW STATIONt
CURRENTLY KNOWN AS THE BEULAH PROJECTt WILL INCLUDE TWO NEW COAL-FIRED
BOILERS WHICH WILL BE REQUIRED TO COMPLY WITH WITH AIR EMISSION STANDARDS
VIA THE BEST AVAILABLE TECHNOLOGY.
I.D. NUMBER   19
BASIN ELECTRIC POWER COOP
BEULAH NO. 2
  450  MW - NEW
COAL 1.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/61
THE UTILITY IS NOW INVESTIGATING VARIOUS FGD PROCESSES. THIS NEW STATION,
CURRENTLY KNOWN AS THE BEULAH PROJECT, WILL INCLUDE TWO NEW COAL-FIRED
B04LERS WHICH WILL BE REQUIRED TO COMPLY WITH WITH AIR EMISSION STANDARDS
VIA THE BEST AVAILABLE TECHNOLOGY.
I.D. NUMBER   l«t
BASIN ELECTRIC POWER COOP
MISSOURI BASIN NO 1
  550  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   1/80
BECAUSE OF THE STRICT WYOMING EMISSION STANDARDS OF 0.2LBS PER MILLION
BTU.LOW SULFUR COAL ALONE WILL NOT MEET STANDARDS.  BASIN ELECTRIC IS NOW
INVESTIGATING VARIOUS FGO PROCESSES.
I.D. NUMBER   15
BASIN FLECTRIC POWER COOP
MISSOURI BASIN NO 2
  550  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/60
BECAUSE OF THE STRICT WYOMING EMISSION STANDARDS OF 0.2LBS PER MILLION
BTU.LOW SULFUR COAL ALONE WILL NOT MEET STANDARDS.  BASIN ELECTRIC IS NOW
INVESTIGATING VARIOUS FGD PROCESSES.
                                                                                                             PEDCo-ENVIRONMENTAL
                                                                  13

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76

                       CURRENT MONTH
I.D. NUMHLR   16
BASIN ELECTRIC POWER COOP
MISSOURI BASIN NO 3
  550  MU - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/83
    BECAUSE OF THE STRICT WYOMING EMISSION STANDARDS OF 0.2LBS PER MILLION
    BTUtLOW SULFUR COAL ALONE WILL NOT MEET STANDARDS.  BASIN ELECTRIC IS NOW
    INVESTIGATING VARIOUS FGO PROCESSES.
I.D. NUMBER   17
BRAZOS ELECTRIC POWER COOP
G X T COOPEHATIVE PROJECT NO.l
  i»00  MW - NEW
COAL  1.67 PERCENT SULFUR
BABCOCK & WILCOX
LIMESTONE SCRUBBING
STARTUP  12/79
    BABCOCK AND WILCOX HAS BEEN AWARDED THE CONTRACT FOR THE INSTALLATION OF
    THIS ENTIRE NEW SYSTEM. THE EMISSION CONTROL EQUIPMENT FOR THE COAL-FIRED
    RAUIANT BOILER WILL CONSIST OF ELECTROSTATIC PKECIPITATORS UPSTREAM OF
    THE LIMESTONE SCRUBBING MODULES. THE SCRUBBER FLUE GAS CAPACITY IS
    NOMINALLY DESIGNED TO EXCEED 1.5 MILLION ACFM. THE DESIGN SOg REMOVAL
    EFFICIENCY IS 66 PERCENT FOR m»00 PPM S02 INLET. LIGNITE COAL WILL BE
    FIRED IN THE BOILER. THE CONSULTING ENGINEERING FIRM IS TIPPETT AND GEE.
1.0. NUMBER   18
CENTRAL ILLINOIS LIGHT CO.
DUCK CREEK NO.l
  100  MU - NEW
COAL 2.5-3.0 PERCENT SULFUR
RILEY STOKER/ENVIRONEERING
LIMESTONE SCRUBBING
STARTUP   6/76
    THE UNIT IS NOW UNDER CONSTRUCTION AND IS SCHEDULED FOR COMPLETION IN
    JUNE 1976. STATION CAPACITY IS HOOMW,  BUT FLUE GAS FROM ONLY 100 MW
    WU.L BE TREATED INITIALLY.
I.D. NUMBER   19
CENTRAL ILLINOIS LIGHT CO.
DUCK CREEK NO.2
  100  MW - NEW
COAL 2.5-3.0 PERCENT SULFUR
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP   1/82
    THIS PROPOSED LIMESTONE UNIT IS SCHEDULED TO COMMENCE OPERATION IN
    JANUARY 1962. A SYSTEM SUPPLIER HAS NOT YET  BEEN SELECTED.
I.D. NUMBER   20
CENTRAL ILLINOIS LIGHT CO.
E.D.EDWARDS NO.3
  357  MW - RETROFIT
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   7/79
    THE UTILITY PLANS TO USE LOW SULFUR COAL FROM 6/76 UNTIL SYSTEM STARTUP.
    TH£ PROCESS AND SYSTEM SUPPLIER HAVE NOT YET  BEEN SELECTED.
                                                                                                            PEDCo-ENVIRONMENTAL
                                                                14

-------
  COMPANY

  POWER  STATION
           TABLE 2
STATUS OF F&D SYSTEMS DURING
OS/76
                       CURRENT MONTH
 I.D.  NUMBER    21
 CENTRAL  ILLINOIS  PUBLIC  SERV
 NEWTON NO.l
   600 MK  -  NEW
 COAL  2.8-3.2 PERCENT  SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP  12/77
    THE UTILITY IS NOW IN THE PROCESS OF EVALUATING BIOS FOR LIME/LIMESTONE
    AND DOUBLE ALKALI SCRUUBING. A DECISION CONCERNING THE PARTICULAR PROCESS
    AND SYSTEM SUPPLIER WILL BE ANNOUNCED SHORTLY.  THE DESIGN BASIS OF THE
    SCRUBBING SYSTEM CALLS FOR S02 REMOVAL EFFICIENCY TO MEET AIR QUALITY
    STANDARDS FOR 4 PERCENT SULFUR COAL.
 I.D. NUMBER    22
 CINCINNATI GAS ft ELECTRIC CO.
 EAST BEND NO 2
   600   MW - NEW
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   1/80
    UTILITY WILL GO OUT FOR BIOS IN LATE  1976.  THE  COMPANY  IS  PRESENTLY  OB-
    TAINING CONSTRUCTION AND OPERATING PERMITS.  STARTUP DATE  HAS  BEEN MOVED
    BACK TO JANUARY 1980.  THE COAL  SOURCE FOR THIS  UNIT  HAS NOT  VET  BEEN SE-
    LECTED.
 I.D. NUMBER   23
 CINCINNATI GAS A ELECTRIC CO.
 MIAMI FORT NO 8
  500  MW - NEW
 COAL 1.3 PERCENT SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   1/76
    THE  UTILITY  HAS  SIGNED  A  CONTRACT  FOR  THE  PURCHASE  OF  LOW  SULFUR COAL
    (1.3 PERCENT SULFURI. THE COAL  BED FOR UNIT  NO.8  IS NOW  IN THE PROCESS OP
    BEING REDESIGNED TO  ACCEPT THE  LOW SULFUR  COAL.   IN ADDITION  TO LIME/
    LIMESTONE  SCRUBBING! THE  UTILITY IS ALSO INVESTIGATING THE POSSIBILITY
    OF'BURNING LOW SULFUR COAL 10.7 PERCENT SULFUR) IN  ORDER TO MEET NSPS.
    NO COMMITMENTS HAVE  BEEN  MADE.
1.0. NUMBER   24
COLUMBUS & SOUTHERN OHIO ELEC.
CONESVILLE NO 5
  <«00  MM - NEW
COAL  4.5 - 4.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
STARTUP   6/76
    THE  UTILITY SIGNED LONG-TERM CONTRACTS WITH DRAVO FOR THE PURCHASE OF
    THIOSORRIC LIME  AND WITH  IUCS FOR THE PURCHASE OF SLUDGE FIXATIVES. THE
    BOILER  AND FGD SYSTEM ARE STILL UNDER CONSTRUCTION. THIS MINE MOUTH PLANT
    PLANS TO BURN COAL WITH 17 PERCENT ASH CONTENT AND 4.5 TO 4.9 PERCENT
    SULFUR  CONTENT.  AN ELECTROSTATIC PRECIPITATOR WILL BE INSTALLED UPSTREAM
    OF THE  FGO SYSTEM.  PRESENT PLANS CALL FUR ONE MODULE OF THIS DUAL.MODULAR
    SYSTEM  TO GO ON-LINE JUNE 23t 1976.
I.D. NUMBER   25
COLUMBUS & SOUTHERN OHIO ELEC.
CONESVILLE NO 6
  400  MW • NEW
COAL  4.5 - 4.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
STARTUP   1/78
   THE UTILITY SIGNED LONG-TERM CONTRACTS WITH ORAVO FOR THE PURCHASE OF
   THIOSORBIC LIME AND WITH IUCS FOR THE PURCHASE OF SLUDGE FIXATIVES. CON-
   STRUCTION ON THIS UNIT IS CURRENTLY SCHEDULED FOR 1977 WITH COMPLETION
   EXPECTED BY JANUARY 1978. SIMILAR TO CONCSVILLE NO.5. THIS MINE MOUTH
   PLANT WILL BURN COAL WITH 17 PERCENT ASH CONTENT AND 4.5 TO 4.9 PERCENT
   SULFUR CONTENT. AN ELECTROSTATIC PRECIPITATOR WILL BE INSTALLED UPSTREAM
   OF THE FGD SYSTEM.
                                                                                                             PEDCo-ENVIRONMENTAL
                                                                15

-------
 COMPANY

 POWER STATION

I.D. NUMBER   26
COLUMBUS g SOUTHERN OHIO ELEC,
POSTON NO. 5
  375  MW - NEW
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76

                       CURRENT MONTH.
    UNIT WILL BURN 2.5 PERCENT SULFUR OHIO COAL,
I.D. NUMBER   27
COLUMBUS S SOUTHERN OHIO ELEC*
POSTON NO. 6
  375  MW - NEW
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/83

I.D. NUMBER   20
COMMONWEALTH EDISON
POWERTON NO. 51
  •425  MW - RETROFIT
COAL 3.6 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP  12/79

I.D. NUMBER   29
COMMONWEALTH EUISON
WILL COUNTY NO  1
  167  MW - RETROFIT
COAL - 9463 BTU,   2.IS  SULFUR
BABCOCK  & WILCOX
LIMESTONE SCRUBBING
STARTUP   2/72

 I.D. NUMBER    30
DETROIT  EDISON
ST.CLAIR NO f,
   180   MW  - RETROFIT
COAL   3.7  PERCENT SULFUR
PEABODY  ENGINEERING
LIMESTONE  SCRUBBING
    UNIT WILL BURN 2.5 PERCENT SULFUR OHIO COAL.


                "FOR"THIS"FGD"SYSTEM"HAS BEEN AWARDED TO UNIVERSAL OIL
    PoDUE ?RO«SI IS°A CLOSED-LOOP WET LIMESTONE SCRUBBING SYSTEM
    imirn WILL BE BACKFITTED TO BOILER 5li ONE OF TWO IDENTICAL BOILERS
    §uJpLY?NG STEAM TO AN 850 MW TURBINE-GENERATOR. THE FGD SYSTEM IS DE-
    !l6NED  TO TREAT FLUE GAS RESULTING FROM THE COMBUSTION OF HIGH SULFUR
    III" ?s.6 PE"ENT SULFUR* 8.3 PERCENT ASH* 17.3 PERCENT MOISTURE* 10,500
    BTU/LB.) AND MEET S02 EMISSION STANDARDS OF 1.6 LB. S02/MM BTU.


               CKGROUNriNFORMATION'sECTION'lN'TABLE 3 OF THIS REPORT. THIS
               HAS BEEN OPERATIONAL SINCE FEBRUARY 1972. THE UNIT HAS RE-
              sS!!l?E W SSJlFOttoSlllG A MAJOR BOILER. TURBINE, AND SCRUB-
         nuiRhAUL  SYSTEM OPERABILITY FOR BOTH MODULES DURING THE REPORT
        iS!  KS ts AND 2! PERCENT IN MARCH AND 20 AND «9 PERCENT IN APRIL FOR
    NOUULES A AND B KESPECT IVELY. MODULES A AND B WERE IN SERVICE A TOTAL OF
    Sw So a£! HOURS HOURS RESPECTIVELY, IN  "«, WHICH TRJNWTES INTO
    ANNUAL  OPEKABILITY FACTORS OF 52 AND H2 PERCENT RESPECTIVELY. ............
             »      sf       u   OF  »»«KE "«. TK
     i ri«
-------
  COMPANY

  POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS OUR ING
05/76
                                                          CURRENT MONTH
 I.D.  NUMBER   31
 DUQUESNE LIGHT
 ELRAMA
   510  MW - RETROFIT
 COAL   1.0 • 2. B PERCENT SULFUR
 CHEMICO.
 LIME  SCRUBBING
 STARTUP  10/75
    THC FGD SYSTEM MAS PLACED IN SERVICE ON OCTOBER 26,  1975.  INITIAL
    OPERATION PROCEEDED WITH FLUE GAS FROM ONE BOILER BEING TREATED BY THE
    SCKUBOING SYSTEM,  P SECOND BOILER WAS TIED INTO THE  SYSTEM ON FEBRUARY *t
    1976.  DURING THE REPORT PERIOD MODIFICATIONS TO THE  FIFTH  SCRUBBING VES-
    SEL WERE COMPLETED AND THE VESSEL IS NOW OPERATING WITH TWO RUBBER-LINED
 1.0.  NUMBER    32
 DUQUESNE  LIGHT
 PHILLIPS
   110  MW -  RETROFIT
 COAL    1*0-  2.8  PERCENT  SULFUR
 CHEMICO
 LIME  SCRUBBING
 STARTUP   7/73
    REFER  TO  BACKGROUND  INFORMATION  SECTION  IN  TABLE  3  OF  THIS  REPORT.   THIS
    FGO SYSTEM  HAS  BELN  OPERATIONAL  SINCE  JULY  1973.  THE UTILITY  REPORTS THAT
    A  TOTAL OF  <»  BOILERS (NOS.  3t4«5,A  6)  WERE  COUPLED  INTO  THE SCRUBBING
    SYSTEM DURING THE  REPORT  PERIOD.  THE SYSTEM IS  NOW  OPERATING  ON  HIGH
    CALCIUM LIME  FOLLOWING  THE  COMPLETION  OF  THE  THIOSORBIC  LIME  TEST PRO-
    GRAM.  THE SCRUBBING  SYSTEM  AVAILABILITY DURING  THE  FIRST QUARTER Op  1976
    WAS 72 PERCENT.  THE  SLUDGE  STABILIZATION  PRACTICES  ARE STILL  CONTINUING
    AT  THIS FACILITY.
 I.D.  NUMBER    33
 GENERAL MOTORS
 CHEVROLET  PARMA 1  2  3  «  f
   32  MW  . RETROFIT
 COAL   2.5 PERCENT SULFUR
 KOCH
 DOUBLE ALKALI
 STARTUP
    REFER  TO  BACKGROUND  INFORMATION SECTION  IN  TABLE 3 OF THIS REPORT. THIS
    FGD  SYSTEM HAS BEEN  OPERATIONAL SINCE MARCH 197*. SYSTtM OPERABILlTY
   •DURING THE MONTHS OF MARCH AND APRIL WAS 17 AND 76 PERCENT RESPECTIVELY.
    SYSTEM OPERABILITY AVERAGED IN EXCESS OF sa PERCENT DURING THE LAST EIGHT
    MONTHS. CURRENTLY, A SCRUBBING SYSTEM CHARACTERIZATION STUDY, SPONSORED
    BY THE EPA, IS BEING CONDUCTED BY A.D. LITTLE.
I.D. NUMBER   3t
GULF POWER CO.
SCHOLZ NO. 1A
   20  MW - RETROFIT
COAL   3.0 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
DOUBLE ALKALI
STARTUP   2/75
   REFER TO BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT. THIS
   FGD SYSTEM HAS BELN OPERATIONAL SINCE FEB. 1975. THE PROTOTYPE SYSTEM
   OPERATED A TOTAL OF H7HH HRS. DURING 1975i TRANSLATING INTO AN ANNUAL
   AVERAGE OPERABILITY OF 89 PERCENT. THE SYSTEM WAS PUT BACK IN SERVICE
   MARCH 12, 1976, FOLLOWING A SCHEDULED BOILER OVERHAUL. SYSTEM OPERABILITY
   WAS 9«t PERCENT FOR THE DURATION OF THE MONTH.
I.D. NUMBER   35
GULF POWER CO.
SCHOLZ NO. 2A
   20  MW - RETROFIT
COAL   3.0 PERCENT SULFUR
FOSTER WHEELER
ACTIVATED CARBON
STARTUP   2/76
   KEFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THE
   SYSTEM SUPPLIER AND TEST DIRECTOR {SOUTHERN SERVICES) REPORTED THREE
   OPERATIONAL RUNS DURING THE REPORT PERIOD. PERFORMANCE OF THE FRONT-END
   OF THE SYSTEM (ADSORPTION AND REGENERATION) WAS CONSIDERED ADEQUATE. THE
   RESOX SECTION OPERATED INTERMITTENTLY DURING THE REPORT PERIOD BECAUSE OF
   PLUGGING PROBLEMS IN THE SULFUR CONDENSER. TO DATE. THE SYSTEM S02
   REMOVAL EFFICIENCY HAS EXCEEDED THE NOMINAL DESIGN VALUE (96 PERCENT).
                                                                                                            PEDCo-ENVIRONMENTAL
                                                              17

-------
  COMPANY

  POWER  STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING  05/76

                       CURRENT MONTH'
 1.0.  NUMBER    36
 GULF  POWLR CO.
 SCHOLZ  NOS.  in  X  2B
    23  MW -  RETROFIT
 COAL  5.0 PERCENT  SULFUR  (MAX)
 CHIYODA INTERNATIONAL
 THOROUGHBRED 101
 STARTUP  3/75
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF REPORT. THIS FGD
    SYSTEM HAS BEEN OPERATIONAL SINCE MARCH 1975,  THE TOTAL SYSTEM OPERABILI-
    TY.  INCLUDING SYSTEM COMMISSIONING,  EXTENDING  FROM FEB. 11,1975,  TO
    DECEMBER 31,1975,  WAS 60 PERC'ENT. SYSTEM OPERABILITY FOR THE MONTHS OF
    MARCH AND APRIL WAS 100 AND m  PERCENT RESPECTIVELY. THE SYSTEM WAS TAKEN
    OUT  OF SERVICE ON  APRIL 5 FOR A SCHEDULED SYSTEM'S DESIGN MODIFICATION.
 I.D. NUMBER    37
 INDIANAPOLIS POWER  X  LIGHT CO.
 PETERSBURG NO  3
   530  MW - NEW
 COAL  3.0-3.5  PERCENT SULFUR
 UNIVERSAL OIL  PRODUCTS
 LIMESTONE SCRUBBING
 STARTUP   9/77
    UNIVERSAL OIL PRODUCTS HAS BEEN SELECTED  TO  BUILD THE  LIMESTONE  SCRUBBING
    SYSrLM.  THE FLUE  GAS FROM THE  530  MW  UNIT WILL  BE TREATED  BY  FOUR
    SCRUBBING MODULES.  CONSTRUCTION ON THI-S SYSTEM  IS NOW  IN PROGRESS.
    WORK IS  PROCEEDING  ACCORDING TO SCHEDULE. CURRENTLY, WORK  ON  THE
    FOUNDATION AND INSTALLATION OF THE RECYCLE TANKS  IS BEING  COMPLETED.
    THE SCRUBBING MODULES ARE NOW  BEING FABRICATED. THE STARTUP DATE HAS
    BEEN MOVED BACK TO  SEPTEMBER 1977.
 1.0. NUMBER   38
 KANSAS CITY POWER X LIGHT
 HAWTHORN NO 3
  140  MW . RETROFIT
 COAL   0.6- 3.0 PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIMESTONE INJECTION XWET SCRUB
 STARTUP  11/72
    REFER  TO  BACKGROUND  INFORMATION  SECTION  IN  TABLE  3  OF  THIS  REPORT.  THIS
    FGD  SYSTEM  HAS  BEEN  OPERATIONAL  SINCE  NOVEMBER  1972. BOTH MODULES WERE
    DOWN THROUGHOUT THE  REPORT  PERIOD.  THE UTILITY  IS CURRENTLY ELIMINATING
    THi  BY-PASS SEALS  AND  INSTALLING SLIDE-GATE DAMPERS. IN ADDITION, THE
    B-MOUULE  WAS RECONVERTED  TO AN UNDERBED  SPRAY ARRANGEMENT BECAUSE OF
    CONTINUING  PLUGGING  PROBLEMS.
I.D. NUMBER   39
KANSAS CITY POWER X LIGHT
HAWTHORN NO 
-------
  COMPANY

  POWER  STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
05/76
                       CURRENT MONTH
 I.D.  NUMBER    41
 KANSAS POiJER  « LIGHT
 JEFFERY NO. 1
   680  MM - NEW
 COAL  0.32 PERCENT SULFUR
 COMBUSTigi! ENGINEERING
 LIMESTONE SCRUBBING
 STARTUP   6/76
    THE UTILITY HAS PURCHASED AN AIR QUALITY CONTROL SYSTEM FROM COMBUSTION
    ENGINEERING FOR PARTICULATE AND S02 REMOVAL. THE SYSTEM WILL CONSIST OF
    AN ESP DOWNSTREAM OF THE AIR HEATER PLUS ID FANS AND SPRAY TOWERS. AN
    OVERFIRE AIR SYSTEM AT THE TANGENTIAL FIRED PULVERIZED BURNERS WILL CON-
    TROL THE NOX EMISSIONS. THE CLEANED GASES WILL BE VENTED TO A 600 FOOT
    STACK.
 I.D. NUMBER   42
 KANSAS POWER « LIGHT
 JEFFERY NO. 2
  680  MM - NEW
 COAL 0.32 PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIMESTONE SCRUBBING
 STARTUP   6/79
    THE UTILITY HAS PURCHASED AN AIR QUALITY CONTROL SYSTEM FROM COMBUSTION
    ENGINEERING FOR PARTICULATE AND S02 REMOVAL.  THE SYSTEM WILL CONSIST OF
    AN ESP DOWNSTREAM OF THE AIR HEATER PLUS ID FANS AND SPRAY TOWERS.  AN
    OVtRFIRE AIR SYSTEM AT THE TANGENTIAL FIRED PULVERIZED BURNERS WILL CON-
    TRUL THE NOX EMISSIONS. THE CLEANED GASES WILL BE VENTED TO A 600 FOOT
    STACK.
 I.D. NUMBER   43
 KANSAS POWER 8 LIGHT
 LAWRENCE NO 4
  125  MW - RETROFIT
 COAL 0.5 PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIMESTONE INJECTION 4WET SCRUB
 STARTUP  12/68
    REFEK  TO BACKGROUND  INFORMATION SECTION IN TABLE 3 OF  THIS REPORT.  THIS
    FGU  SYSTEM HAS BEEN  OPERATIONAL SINCE  DECEMBER 1966. THIS UNIT  IS CUR.
    RENTLY BURNING LOW SULFUR  WYOMING COAL. THE OPERATION  OF  THE  SCRUBBER HAS
    BEEN MORE EFFICIENT  AND  ECONOMICAL FOR THIS COAL TYPE  BECAUSE A LESSER
    DEGREE OF S02  REMOVAL  IS REQUIRED FOR  COMPLIANCE.  THE  UTILITY PLANS TO
    REPLACE THIS SCRUBBING SYSTEM  WITH A VENTRI-ROD AND SPRAY TOWER SCRUBBING
    SYSTEM.
I.D. NUMBER   44
KANSAS POWER ft LIGHT
LAWRENCE NO 5
  400  MW - NEW
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE INJECTION &WET SCRUB
STARTUP  11/71
    REFER  TO  BACKGROUND  INFORMATION  SECTION  IN  TABLE  3  OF  THIS  REPORT.  THIS
    FGD  SYSTEM HAS  BEEN  OPERATIONAL  SINCE  NOVEMBER  1971. THIS UNIT  IS CUR-
    RENTLY  BURNING  LOW SULFUR  WYOMING  COAL.  THE OPERATION  OF THE  SCRUBBER HAS
    BEEN MORE EFFICIENT  AND  ECONOMICAL FOR THIS COAL  TYPE  BECAUSE A LESSER
    DEGREE  OF S02 REMOVAL  IS REQUIRED  FOR  COMPLIANCE. THE  UTILITY PLANS TO
    REPLACE. THIS SCRUBBING SYSTEM WITH A VENTRI-ROD AND SPRAY TOWER SCRUBBING
    SYSTEM.
I.D. NUMBER   45
KENTUCKY UTILITIES
GREEN RIVER   UNITS 1 AND
   64  MW - RETROFIT
COAL  3.6 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   9/7S
   REFER  TO BACKGROUND  INFORMATION SECTION  IN TABLE 3 OF THIS REPORT. THIS
   SYSTEM BECAME OPERATIONAL SEPTEMBER 13,  1975. THE OPERATIONAL DATA
   SUPPLIED BY THE UTILITY FOR THE REPORT PERIOD SHOWS THAT SYSTEM
   AVAILABILITYi RELIABILITY. OPERABILITY.  ANU UTILIZATION WAS 97« 95t 65*
   AND 52 PERCENT RESPECTIVELY FOR THE MONTH OF MARCH AND 90. 100. 100. AND
   77 PERCENT RESPECTIVELY FOR THE MONTH OF APRIL.
                                                                                                            PEDCo- ENVIRONMENTAL
                                                                19

-------
  COMPANY

  POULR STATION

 I.D. NUMBER   46
 KEY WEST UTILITY BOARD
 STOCK ISLAND PLANT
    37  riW - NEW
 OIL    2.4 PERCENT SULFUR
 ZURN AIR SYSTEMS
 LIMESTONE SCRUBBING
 STARTUP  10/72

 I.D. NUMBER   47
 LOUISVILLE GAS 8 ELECTRIC
 CANE RUN NO if
   176  MW - RETROFIT
 COAL   3.5-i».05 PERCENT SULFUR
 AMERICAN AIR FILTER
 LIME SCRUBBING
 STARTUP   6/76

 I.D.  NUMBER   i»8
 LOUISVILLE  GAS g ELECTRIC
 CANE  RUN NO 5
   183  MW - RETROFIT
 COAL    3.5-i*.05  PERCENT SULFUR
 COMBUSTION  ENGINEERING
 LIME  SCRUBBING
 STARTUP   12/77

 1.0.  NUMBER    49
 LOUISVILLE  GAS g, ELECTRIC
 CANE  RUN  NO  6
  277  MW -  RETROFIT
 COAL   3.5-  4.0 PERCENT SULFUR
 NOT SELECTTED
 NOT SELECTED
 STARTUP   9/7fl

 I.D. NUMBER    50
 LOUISVILLE GAS g ELECTRIC
 MILL CREEK NO 1
  330  MW - RETROFIT
COAL   3.5- 4.0 PERCENT SULFUR
NOT SELECTED
LIME SCRUBBING
STARTUP   1/62
           TABLE 2
STATUS OF FGD SYSTEMS DURING
05/76
                       CURRENT MONTH

    REFEH TO BACKGROUND INFORMATION SECTION IN TABLE 3~OF~THIS~REPORTl"THIS~'
    FGO SYSTEM HAS BEEN OPERATIONAL SINCE OCTOBER 1972.  THF FGD SYSTEM HAS
    ?F™ ^,Tv°F SLRVICE SINCE JANUARY 28,1975. MODIFICATIONS AND REPAIRS ARE
    CURRENTLY IN PROGRESS.  SYSTEM RESTART IS STILL INDEFINITE.  A CHECKOUT
    OF ALL SYSTEM MOTORS AND PUMPS MUST  BE COMPLETED BEFORE STARTUP CAN
    COMMENCE.
    THE  UTILITY  HAS  SIGNED  A  CONSENT  AGREEMENT  WITH  THE  EPA  FOR  THE  INSTAL-
    LATION  AND OPERATION  OF FGD EQUIPMENT  ON  THIS  UNIT BY  JUNE 1,1976.  THE
    CONTRACT  HAS BEEN  AWARDED TO  AMERICAN  AIR FILTER. THE  SYSTEM WILL OPERATE
    ON A CLOSED  WATER  LOOP  AND THE SLUDGE  WILL  BE  STABILIZED. THIS SYSTEH IS
    PRESENTLY UNDER  CONSTRUCTION.                                            .
   THE UTILITY HAS SIGNEJ A CONSENT AGREEMENT WITH THE EPA"FOR~THE~INSTALT
   LATION AND OPERATION OF FGO EQUIPMENT ON THIS UNIT BY DECEMBER 1,1977.
   THL,,CONTRACT FOR THIS LIME SCRUBBING SYSTEM HAS BEEN AWARDED TO
   COMBUSTION ENGINEERING. THE UNIT IS PRESENTLY UNDER CONSTRUCTION.
   THL UTILITY HAS SIGNED A CONSENT AGREEMENT WITH THE EPA FOR THE INSTAL
   LATION AND OPERATION OF FGO EQUIPMENT ON THIS UNIT BY SEPTEMBER 1,1978
   DURING THE REPORT PERIOD THE UTILITY ANNOUNCED THAT THEY HAVE SEEN
   SELECTED BY THE EPA TO NEGOTIATE A CONTRACT FOR THE INSTALLATION OF A
   DOUBLE ALKALI SYSTEM ON THIS UNIT.  THE PROCESS BEING GIVEN PRIME
   CONSIDERATION IS THE CEA/AOL DUAL ALKALI FGD SYSTEM.
   A COMPLIANCE SCHEDULE HAS BEEN SUBMITTED TO THE JEFFERSON~COUNTY"AIR~
                  DISTRICT WITH »/M ESTABLISHED AS THE IlSlS OATC F0«
                                                                                                          PEDCo-ENVIRONMENTAL
                                                                 20

-------
  COMPANY

  POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING
05/76
                       CURRENT MONTH'
 I.D. NUMBER   51
 LOUISVILLE GAS & ELECTRIC
 MILL CREEK NO 2
   330  MM • RETROFIT
 COAL   3.5- 4.0 PERCENT SULFUR
 NOT SELECTED
 LIME SCRUBBING
 STARTUP   1/81
    A COMPLIANCE SCHEDULE HAS BEEN SUBMITTED TO THE JEFFERSON COUNTY AIR POL-
    LUTION CONTROL DISTRICT WITH 1/61 ESTABLISHED AS THE STARTUP DATE FOR AN
    FGU SYSTEM.
 I.D. NUMBER   52
 LOUISVILLE GAS 8 ELECTRIC
 MILL CREEK NO 3
   425  MW - NEW
 COAL   3.5- 4.0 PERCENT SULFUR
 AMERICAN AIR FILTER
 LIME SCRUBBING
 STARTUP   7/77
    THL UTILITY HAS SIGNED A CONSENT AGREEMENT WITH THE EPA FOR THE INSTAL-
    LATION AND OPERATION OF FGU EQUIPMENT ON THIS POWER GENERATING UNIT BY
    JULY 1,1977. THIS NEW FACILITY WILL BE REQUIRED TO MEET FEDERAL NSPS FOR
    THE LIMITATION OF S02 EMISSIONS. CONTRACT HAS BEEN AWARDED TO AMERICAN
    AIR FILTER. THE SYSTEM WILL OPERATE ON A CLOSED WATER LOOP AND THE SLUDGE
    WILL BE STABILIZED.  CONSTRUCTION HAS BEGUN ON THE FGD SYSTEM.
 I.D. NUMBER   53
 LOUISVILLE GAS 8 ELECTRIC
 MILL CREEK NO 4
   425  MW - NEW
 COAL   3.5- 4.0 PERCENT SULFUR
 AMERICAN AIR FILTER
 LIME SCRUBBING
 STARTUP   7/79
    THE UTILITY HAS SIGNED A CONSENT AGREEMENT WITH THE EPA FOR THE INSTAL-
    LATION AND OPERATION OF FGD EQUIPMENT ON THIS POWER GENERATING UNIT BY
    JULY 1.1979. THIS NEW FACILITY WILL BE REQUIRED TO MEET FEDERAL NSPS FOR
    THE LIMITATION OF S02 EMISSIONS. THE CONTRACT HAS BEEN AWARDED TO
    AMERICAN AIR FILTER FOR A LIME SCRUBBING SYSTEM.
 I.D. NUMBER   54
 LOUISVILLE GAS 8 ELECTRIC
 PADDYS RUN NO 6
    65  MW - RETROFIT
 COAL  3.5-4.0 PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIME SCRUBBING
 STARTUP   4/73
    REFEK TO  BACKGROUND  INFORMATION  SECTION IN  TABLE  s OF  THIS  REPORT.  THIS
    FGD SYSTEM  MAS  BEEN  OPERATIONAL  SINCE  APRIL 1973.  OPERABILITY  WAS  100
    PERCENT  IN  JANUARY.  S02  REMOVAL  EFFICIENCY  WAS  99  PERCENT DURING THIS
    OPERATING PERIOD.  THE  SYSTEM  WAS SHUTDOWN IN EARLY FEBRUARY IN PREPARA-
    TION FOR  THE  EPA SCRUBBER  AND SLUDGE STUDY  WHICH  MAY COMMENCE  IN JUNE.  OR
    JULY OF  1976.   THE SCHUBbEH WILL NOT BE OPERATED  UNTIL THIS TIME UNLESS
    THE NEED  ARISES (PEAK  LOAD DEMAND). CURRENTLY,  THE UTILITY  IS  COMPLETING
    MODIFICATIONS ON THIS  UNIT IN ANTICIPATION  OF THE  STUDY PROGRAM.
 I.D.  NUMBER   55
 MINNKOTA POWER COOPERATIVE
 MILTON R. YOUNG NO.  2
   450  MW - NEW
 LIGNITE - 6.500 BTu,  0.7K S
COMBUSTION EQUIP. ASSOCIATES
 LIME/ALKALINE FLYASH SCRUBBING
 STARTUP   6/77
    THL  CONTRACT  FOR  THIS  FGD  SYSTEM  HAS  BEEN  AWARDED  TO  COMBUSTION  EQUIPMENT
    ASSOCIATES. THE A/c.  FIRM IS  SANDERSON AND  PORTER.  THE BOILER  IS  NOw UNDER
    CONSTRUCTION.  THE TANKS FOR  THE FGU SYSTEM HAVE BEEN  FABRICATED  AND ARE
    SCHEDULED FOR  INSTALLATION IN JULY 1976. A PILOT PLANT (5000  ACFM) WAS
    PUT  IN  SERVICE ON OCTOBER  13,1975. THE PILOT PLANT KUNS ARE BEING CON-
    DUCTED  TO DETERMINE  THE MAJOR CRITERIA FOR A FULL-SUE INSTALLATION.
    SPECIFICALLY.THIS INCLUDES RELIABILITY TESTING. EVALUATION OFF VARIOUS PH
    CONTROL SYSTEMS AND  ANALYSES OF VARIOUS TYPES OF FLYASH ABSORBENTS.
                                                                                                            PEOCo-ENVIRONMENTAL
                                                               21

-------
  COMPANY

  POWER STATION

 1.0. NUMBER   56
 MONTANA POWER CO.
 COLSTRIP NO 1
   360  MW - NEW
 COAL   0.0 PERCENT SULFUR
COMBUSTION EQUIP. ASSOCIATES
 LIME/ALKALINE FLYASH SCRUBBING
 STARTUP  10/75
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76

                       CURRENT MONTH

    THE COLSTRIP PLANT IS A MINE  MOUTH INSTALLATION.  CONSTRUCTION ON~THls"""~'
    UNIT WAS COMPLETED BEHIND SCHEDULE.  THE  FGD  SYSTEM STARTED  UP IN LATE
    1975 AND PROCEEDED THROUGH A  SHAKLDOWN AND DEBUGGING  OPERATION PHASE.  THE
    UNIT IS NOW OPERATING AT FULL COMMERCIAL CAPACITY.  OPERATING  DATA AC-
    CUMULATED TO-DATE IS  IN THE PROCESS  OF BEING EVALUATED  BY THE UTILITY  FOR
    PRESENTATION TO  STATE REGULATORY AGENCIES.
 I.D. NUMBER   57
 MONTANA POWER CO.
 COLSTRIP NO 2
   360  MW - RETROFIT
 COAL   0.8 PERCENT SULFUR
COMBUSTION EQUIP. ASSOCIATES
 LIME/ALKALINE FLYASH SCRUBBING
 STARTUP   7/76

 I.D. NUMBER   58
 MONTANA POWER CO.
 COLSTRIP NO.3
   700  MW - NEW
 COAL  0.7 PERCENT SULFUR
 NOT  SELECTED
 NOT  SELECTED
 STARTUP   7/80

 I.D.  NUMBER   59
 MONTANA POWER  CO.
 COLSTRIP N0.it
   700   MW - NEW
 COAL   0.7 PERCENT  SULFUR
 NOT  SELECTED
 NOT  SELECTED
 STARTUP    7/81

 I.D. NUMBER   60
NEVADA  POWER
HARRY ALLEN STATION NO. 1
  500  MW  • NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/63
    THE  COLSTRIP  PLANT  IS  A  MINE MOUTH  INSTALLATION. THIS FGD SYSTEM  IS NOW
    UNDER  CONSTRUCTION.  TURBINE ROLL AND SYSTEM CHECKOUT IS SCHEDULED FOR
    MID-JUNE  1976. NO DELAYS FOR THE JULY STARTUP ARE ANTICIPATED. THE
    CONSULTING  ENGINEERING FIRM IS BECHTEL.
   THE UTILITY IS CURRENTLY WAITING FOR APPROVAL OF A CERTIFICATE TO
   CONSTRUCT BOILERS 3 AND * BEFORE PROCEEDING WITH ORDERS TO INSTALL FGD
   SYSTEMS. THE FGD PROCESS BEING GIVEN PRIME CONSIDERATION FOR UNITS 3 AND
   «f IS THE LIME/ALKALINE FLYASH SCRUBBING SYSTEM CURRENTLY OPERATING AND
   BEING INSTALLED ON COLSTRIP UNITS 1 AND 2 RESPECTIVELY
   THE UTILITY IS CURRENTLY WAITING FOR APPROVAL OF A CERTIFICATE TO
   CONSTRUCT BOILERS 3 AND H BEFORE PROCEEDING WITH ORDERS TO INSTALL FGD
   SYSTEMS. THE FGD PROCESS BEING GIVEN PRIME CONSIDERATION FOR UNITS 3 AND
   «» IS THE LIME/ALKALINE FLYASH SCRUBBING SYSTEM CURRENTLY OPERATING AND
   BEING INSTALLED ON COLSTRIP UNITS 1 AND 2 RESPECTIVELY
   CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD
   TIONS HAVE NOT YET BEEN PREPARED.
                                                                                                        PEDCo-ENVIRONMti^AL
                                                              22

-------
 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76
 POWER STATION
                       CURRENT MONTH
1.0. NUMBER   61
NEVADA POWER
HARRY ALLEN STATION NO. 2
  500  NW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/Bf
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGO SYSTEM.  SPECIFICA-
    TIONS HAVE NOT YET BEEN PREPARED.
I.D. NUMBER   62
NEVADA POWER
HARRY ALLEN STATION NO.
  500  MM - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/65
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGO SYSTEM.  SPECIFICA-
    TIONS HAVE NOT YET BEEN PREPARED.
I.D. NUMBER   63
NEVADA POWER
HARRY ALLEN STATION NO.
  500  MW • NEW
COAL
NOT SELECTED
NOT SELLLTED
STARTUP   6/66
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.
    TIONS HAVE NOT YET BEEN PREPARED.
    •'-4.                    *
SPECIFICA-
I.D. NUMBER   61
NEVADA POWER
REID GARDNER NO 1
  125  MW • RETROFIT
COAL   0.5- 1.0 PERCENT SULFUR
COMBUSTION EQUIP. ASSOCIATES
SODIUM CARBONATE SCRUBBING
STARTUP
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS  REPORT.   THIS
    FGD SYSTEM HAS BEEN OPERATIONAL SINCE  APRIL 1974.  SYSTEM  OPERAblLlTY FOR
    THE MONTHS OF  MAKCH AND APRIL  WAS  72 AND 91 PERCENT RESPECTIVELY. ONE
    FOKCED SCRUBBER OUTAGE  OCCURRED DURING THE REPORT  PERIOD  BECAUSE OF  A
    VENTURI LEAK.  THE  BOILER WAS SHUTDOWN  APRIL 5 FOR  A VALVE AND  COAL CON-
    DUIT INSPECTION.
I.D. NUMBER   65
NEVADA POWER
REIO GARDNER NO 2
  125  MW - RETROFIT
COAL   0.5- 1.0 PERCENT SULFUR
COMBUSTION EQUIP. ASSOCIATES
SODIUM CARBONATE SCRUBBING
STARTUP   t/7H
    REFER  TO  BACKGROUND  INFORMATION  SECTION  IN  TABLE  3  OF  THIS  REPORT.  THIS
    FGD  SYSTEM  HAS  BEEN  OPERATIONAL  SINCE  APR.  197t.  SYSTEM  OPERABILITV FOR
    THE  MONTHS  OF MARCH  AND  APRIL  WAS  60 AND 77 PERCENT RESPECTIVELY. DURING
    THE  REPORT  PERIOD  SEVERAL FORCED SCRUBBER OUTAGES WERE REPORTEDi
    PRIMARILY CAUSED BY  PLUGGED  SENSING LINES.  REHEATER REPAIRS,
    AND  MALFUNCTIONS IN  THE  TRAY SYSTEM.
                                                                                                         PEOCo-ENVIRONMENTAL
                                                               23

-------
  COMPANY
           TABLE 2
STATUS OF FGO SYSTEMS DURING
05/76
  POWER  STATION
                       CURRENT MONTH
 I.D. NUMBER   66
 NEVADA POWER
 REID GARDNER NO 3
   125  MM - NEW
 COAL   0.5- 1.0 PERCENT SULFUR
 COMBUSTION EQUIP. ASSOCIATES
 SODIUM CARBONATE SCRUBBING
 STARTUP   6/76
    FOK SPECIFIC INFORMATION ON THE TYPE OF SCRUBBING SYSTEM CURRENTLY UNDER
    CONSTRUCTION FOR THIS UNIT REFER TO THE BACKGROUND INFORMATION SECTIONS
    FOH REID GARDNER NOS 1 AND 2 IN TABLE 3 OF THIS REPORT. THE PRELIMINARY
    CHECKOUT AND OPERATION OF THE BOILER HAS ALREADY STARTED. THE FGD SYSTEM
    IS NOW SCHEDULED TO COMMENCE OPERATION ON JUNE 7t 1976. CONSTRUCTION IS
    STILL PROCEEDING.
 I.D. NUMBER   67
 NEVADA POWER
 REID GARDNER NO 
-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F6D SYSTEMS DURING  05/76

                       CURRENT NONT*1
ItO. NUMUCR   71
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 7
  190  MW - RETROFIT
COAL 3 PERCENT SULPUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOR PER-
    FORMANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT UNDER CONSTRUCTION AT THEIR
    O.N.MITCHELL NO.11 UNIT.  LOU SULFUR COAL MAY BE EMPLOYED TO COMPLY WITH
    S02 EMISSION REGULATIONS.  •
I.D. NUMBER   72
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 8
  400  MW - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.   ALSO WAITING FOR PERFOR-
    MANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT UNDER CONSTRUCTION AT THEIR
    D. H. MITCHELL NO. 11 UNIT.   LOW SULFUR COAL MAY BE BURNED TO COMPLY WITH
    S02 EMISSION REGULATIONS.
I.D. NUMBER   73
NORTHERN INDIANA PUB SERVICE
MITCHELL NO 11
  115  MW - RETROFIT
COAL   3.2- 3.5 PERCENT SULFUR
DAVY POWEKGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP   5/76
    THIS FGD SYSTEM IS AN INTEGRATION OF THE WELLMAN-LORD S02 RECOVERY PRO-
    CESS OF DAVY POWEKGAS AND ALLIED CHEMICAL'S S02  TO SULFUR REDUCTION
   -PROCESS. DAVY POWEKGAS IS THE ENGINEER AND CONSTRUCTOR OF THE  FGD
   'FACILITY AND ALLIEU CHEMICAL is THE SYSTEM OPERATOR AND PRODUCT  MARKETER.
    THE STARTUP DATE  FOR THE  OPERATION OF THIS SYSTEM HAS BEEN DELAYED ONE
    MONTH BECAUSE OF  A FIRE WHICH OCCURRED IN THE  ABSORBER SECTION OF  THE FGD
    SYSTEM. PRESENTLY. THE SYSTEM OPERATORS ARE CHECKING OUT THE VARIOUS SUB-
    SYSTEMS BY  PASSING WATER  AND GAS THROUGH THE EQUIPMENT.
I.D. NUMBER   7t
NORTHERN STATES POWER CO,
SHERBURNE NO 1
  680  MW - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   5/76
    A  PRELIMINARY  SYSTEM  CHECKOUT  BY  PASSING  WATER  AND  AIR  THROUGH  THE  EQUIP-
    MENT  WAS  SUCCESSFULLY COMPLETED BY  THE  UTILITY.  THE SYSTEM  WAS  PUT  IN
    SERVICE ON MARCH  U,  1976.  TREATING FLUE  GAS  FROM BOILER  NO.l.  WHICH
    FIRES A LOW SULFUR  WESTERN  COAL.  FOLLOWING  THE  3/16 STARTUP THE SYSTEM
    WAS TESTED ON  VARIOUS LOAD  CAPACITIES AND IS  CURRENTLY  OPERATING AT FULL
    COMMERCIAL LOAD.  A  30-DAY VENDOR  RELIABILITY  TEST PROGRAM IS SCHEDULED
    TO COMMENCE IN MID-SUMMER 1976.
1.0. NUMBER   75
NORTHERN STATES POwER CO.
SHERBURNE NO 2
  680  MW - NEW
COAL 0.6 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   5/77
    THE  FGD  SYSTEM  IS  CURRENTLY  UNDER  CONSTRUCTION.  RECENT  SCRUBBER DESIGN
    CHANGES  HAVE  CAUSED  EQUIPMENT DELIVERY DELAYS.  IN  ADDITION.  SOME PROBLEMS
    HAVE ARISEN IN  OBTAINING  SOME ELECTRICAL CONTROLS. HOWEVER.  THE OVERALL
    SCHEDULE HAS  NOT BEEN  UPSET  AND  CONSTRUCTION OF  THE SYSTEM IS CONTINUING
    ON SCHEDULE.
                                                                                                            PEDCo-ENVIRONMENTAL
                                                             25

-------
 COMPANY

 POWER STATION

I.D. NUMBER   76
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. I
  835  Mw - NEW
COAL   1.3 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   1/76

I.D. NUMBER   77
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 2
  835  MW - NEW
COAL   1.3 PERCENT SULFUR
CMEMICO
LIME SCRUBBING
STARTUP   1/77

I.D. NUMBER   78
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 3
  635  MW - NEW
COAL   1.3 PEKCENT SULFUR
PULLMAN KELLOGG
LIMESTONE SCRUBBING
STARTUP   1/79

I.D. NUMBER   79
PHILADELPHIA ELECTRIC CO.
CROMBY
  150  MW - RETROFIT
COAL   2-1 PERCENT SULFUR
UNITED ENGINEERS
MAGNESIUM OXIUF SCRUBBING
STARTUP  10/78
                                             TABLE 2
                                  STATUS OF FGD SYSTEMS DURING
                           05/76
                    CURRENT  MONTH

"REFER'TO'THE BACKGROUND INFORMATION SECTION  IN TABLE  3 OF THIS REPORT.
 THIS EMISSION CONTKOL SYSTEM IS CAPABLE  OF REMOVING FLYASH AND S02 FROM
 3.35 MM ACFM OF  FLUE GAS VIA WET LIME  SCRUBDING.  THE  INITIAL SHAKEDOWN
 AND DEBUGGING PHASL OF OPERATION BEGAN FOR PART OF  THE SYSTEM IN DECEMBER
 1975. FULL COMMERCIAL OPERATION COMMENCED IN APRIL  1976.  TO OATEt ALL 6
 OF THE SCRUBBER/ABSORBER TRAINS HAVE BEEN PUT INTO  OPERATION.
 THE FGD SYSTEM FOR THIS INSTALLATION WILL BE A CHEMICO WET LIME SCRUBBING
 SYSTEM CAPABLE OF REMOVING PARTICULATE MATTER AND S02 FROM THE FLUE GAS.
 THIS SYSTEM IS CURRENTLY UNDER CONSTRUCTION. LONG DELAYS HAVE BEEN EN-
 COUNTERED IN MATERIAL DELIVERIES. THE FGD SYSTEM STARTUP DATE IS NOW
 SCHEDULED FOR APRIL 1977.
 PULLMAN INC., ANNOUNCED DURING THE REPORT PERIOD THAT ITS PULLMAN KELLOGG
 DIVISION HAS BEEN AWARDED A CONTRACT IN EXCESS OF $50 MILLION FOR AN FGD
 SYSTEM TO BE INSTALLED ON THIS COAL-FIRED 835 MW UNIT. THE EMISSION CON-
 TRQL SYSTEM WILL CONSIST OF 5 WEIR HORIZONTAL CROSS-FLOW WET ABSORBER
 MOUULES OPERATED IN CONJUNCTION WITH A PATENTED CATALYTIC CHEMISTRY PRO-
 CESS DEVELOPED BY KELLOGG. ESP'S WILL BE INSTALLED UPSTREAM OF THE
 SCRUBBING SYSTEM.

"THE'UTILITY PLANS TO RETROFIT ONE OF THE TWO BOILERS AT CROMBY WITH  AN
 FGU SYSTEM. HOWEVER, A FINAL DECISION HAS NOT BEEN MADE.  THE PROCESS
 BEING GIVEN PRIME CONSIDERATION IS MAGNESIUM OXIDE SCRUBBING DESIGNED
 JOINTLY BY UNITED ENGINEERS AND PHILADELPHIA ELECTRIC.  ENGINEERING
 DESIGN WORK IS SCHEDULED FOR 1976.  FGD SYSTEM STARTUP IS NOW SCHEDULED
 FOR OCTOBER 1978.
 1.0. NUMBER   BO
 PHILADELPHIA ELECTRIC CO.
 EDDYSTONE NO 1A
  120  MW - RETROFIT
 COAL   2.5 PERCENT SULFUR
 UNITED ENGINEERS
 MAGNESIUM OXIDE SCRUBBING
 STARTUP   9/75
 THE S02 SCRUBBER HAS BEEN TEMPORARILY SHUTDOWN BECAUSE THE ACID PLANT RE-
 GENERATION FACILITY AT THE OLIN CHEMICAL SULFURIC ACID PLANT IN PAULS80RO
 NEW JERSEY HAS PERMANENTLY CEASED OPERATIONS. CONSIDERATIONS ARE NOW
 BEING GIVEN TO THE RELOCATION OF THE REGENERATION FACILITY. ONCE THIS DE-
 CISION IS MADE A MINIMUM PERIOD OF SIX MONTHS WILL BE REQUIRED TO RELO-
 CATE THE REGENERATION FACILITY. THE PARTICULATE SCRUBBERS ARE CONTINUING
 TO OPERATE. THE UTILITY IS STILL EXPERIENCING PROBLEMS WITH THE FANS. RE-
 HEAT BURNERS. OAMPERSt AND EXPANSION JOINTS.
                                                                                                            PEDCo-INYIRONWItrtlAL
                                                                 26

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76

                       CURRENT MONTH
I.D. NUMBER   81
PHILADELPHIA ELECTRIC CO.
EODYSTONE NO IB
  2i*0  MW - RETROFIT
COAL 2.5 PERCENT SULFUR
UNITED ENGINEERS
MAGNESIUM OXIDE SCRUBBING
STARTUP  10/76
    THE RETROFITTING OF SECOND STAGE SCRUBBERS ON THE BALANCE OF THE FLUE GAS
    FROM EODYSTONE 1 IS AWAITING PERFORMANCE OF THE EXISTING 2-STAGE UNIT
    WHICH IS TREATING ONE THIRD OF THE BOILER FLUE GAS.  THIS UNIT CONSISTS
    OF A AND B PARTICULATE SCRUBBING TRAINSi EACH ARE 120 MW.  CHECK VALVE
    FAILURE ON A TRAIN HAS BEEN CORRECTED.  FAN ON B TRAIN IS STILL AT THE
    FACTORY FOR REPAIR.
I.D. NUMBER   62
PHILADELPHIA ELECTRIC CO.
EODYSTONE NO 2
  336  MU - RETROFIT
COAL 2."» PERCENT SULFUR
UNITED ENGINEERS
MAGNESIUM OXIDE SCRUBBING
STARTUP  10/76
    COMPANY IS AWAITING PERFORMANCE OF FGD SYSTEM ON UNIT 1 BEFORE PROCEEDING
    WITH DESIGN OF FGD SYSTEM ON THIS BOILER.  HOWEVER ENGINEERING PHASE IS
     TENTATIVELY PLANNED TO START IN JAN 76. AT WHICH TIME EVALUATION OF
    DATA FROM UNIT 1 SHOULD BE COMPLETE.
1.0. NUMBER   63
PUBLIC SERVICE CO OF COLORADO
VALMONT NO. 5
   50  MW - RETROFIT
COAL  0.72 PERCENT SULFUR
UOP / PUB SERVICE OF COLORADO
LIMESTONE SCRUBBING
STARTUP  10/74
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 9 OF THIS REPORT. THIS
    SYSTEM HAS BEEN OPERATIONAL SINCE NOVEMBER 197
-------
  COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76
  POWER STATION
                                                          CURRENT MONTH
 I.D.  NUMBER   86
 PUBLIC SERVICE CO OF NEW MEX.
 SAN JUAN NO.  3
   500  MW - NEW
 COAL  0.6 PERCENT SULFUR
 DAVY  POWERGAS
 WELLNAN LORD
 STARTUP   5/79
    A LETTER OF INTENT HAS BEEN SIGNED WITH DAVY POWERGAS FOR A WELLMAN
    LORD UNIT. THE PROJECTED STARTUP DATE OF THIS SYSTEM HAS BEEN DELAYED ONE
    YEAR TO HAY 1979.
 I.D.  NUMBER    67
 PUBLIC  SERVICE CO  OF NEW HEX,
 SAN JUAN  NO.  H
   500  MW - NEW
 COAL  0.6  PERCENT SULFUR
 DAVY  POWERGAS
 WELLMAN LORD
 STARTUP   5/61
    A LETTER  OF INTENT  HAS  BEEN  SIGNED  WITH  DAVY  POWERGAS FOR A WELLMAN
    LORD UNIT.  THE  PROJECTED STARTUP  DATE OF THIS SYSTEM HAS BEEN DELAYED ONE
    YEAR TO HAY 1981.
 I.D. NUMBER    88
 PUBLIC SERVICE INDIANA
 GIBSON NO. 3
  650  MW - NEW
 COAL 3.3 PERCENT SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/78
   BID EVALUATION IS UNDERWAY.
 I.D. NUMBER   89
 PUBLIC SERVICE INDIANA
 GIBSON NO. i»
  650  MW • NEW
 COAL 3.3 PERCENT SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/79
   BID SPECIFICATIONS ARE BEING PREPARED.
I.D. NUMBER   90
RICKENBACKER AFB
RICKENBACKER
   20  MW • RETROFIT
COAL 3.6 PERCENT SyLFUR
RESEARCH COTTRELL
LIME SCRUBBING
STARTUP   3/76
   THL SYSTEM SUPPLIER REPORTED THAT THE FGD SYSTEM BECAME OPERATIONAL ON
   MARCH 11, 1976. SYSTEM OPERABILITV WAS REPORTED TO BE 97 PERCENT FOR THE
   DURATION OF THE MONTH. THE SYSTEM WAS BROUGHT DOWN ON APRIL H» BECAUSE
   OF PUMP PROBLEMS. A 1.5 WEEK OUTAGE RESULTED BECAUSE OF A SPARE PART
   SHIPMENT. S02 INLET CONCENTRATIONS HAVE BEEN AT THE 1800 PPM LEVEL, LIHE
   UTILIZATION HAS BEEN GOOD. THE S02 REMOVAL EFFICIENCY WAS REPORTED TO BE
   AS HIGH AS 96 PERCENT.
                                                                                                            PEOCo-ENVIRONMENTAL
                                                                28

-------
  COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING
                                                                 05/76
  POWER STATION
                                                          CURRENT MONTH
 I.D.  NUMBER   91
 S.  CAROLINA PUB SERV AUTHORITY
 WINYAH NO.  2
   mo  MW - NEW
 COAL   1.0 PERCENT  SULFUR
 BABCOCK £ WILCOX
 LIMESTONE SCRUBBING
 STARTUP   5/77
    THE CONTRACT HAS BEEN AWARDED TO B&W FOR CONSTRUCTION OF A LIMESTONE SYS-
    TEM TREATING 50 PERCENT OF THE GAS FLOW FROM A 260 MW BOILER.  THIS UNIT
    WILL FIRE 1 PERCENT SULFUR COAL AND THE GUARANTEED REMOVAL EFFICIENCY IS
    69 PERCENT. DIFFERENT METHODS OF SLUDGE DISPOSAL ARE CURRENTLY BEING EX-
    AMINED BY THE UTILITY.
 I.D.  NUMBER    92
 S.  MISSISSIPPI ELEC  PWR  ASSOC
 R.O.  MORHOW  NO.l
   160  MW  -  NEW
 COAL  1  PERCENT SULFUR
 RILEY STOKER/ENVIRONEERING
 LIMESTONE  SCRUBBING
 STARTUP 11/77
    THE CONTRACT  FOR  THIS  LIMESTONE  SYSTEM HAS  BEEN  AWARDED  TO  RILEY
    STOKER/ENVIRONEERING.   GUARANTEED S02  REMOVAL  EFFICIENCY IS 65  PERCENT.
    FABRICATION OF  EQUIPMENT  IS  NOW  IN PROGRESS. SYSTEM STARTUP IS  SCHEDULED
    FOR NOVEMBER  1977.
 1.0.  NUMBER   93
 S. MISSISSIPPI ELEC PWR  ASSOC
 R.D.  MORROW NO.2
  160  MW . NEW
 COAL  1 PERCENT SULFUR
 RILEY STOKEK/ENVIRONEERING
 LIMESTONE SCRUBBING
 STARTUP   6/76
    THE  CONTRACT FOR  THIS LIMESTONE  SYSTEM HAS BEEN  AWARDED  TO RILEY
    STOKER/ENVIRONEERING.  GUARANTEED S02 REMOVAL EFFICIENCY IS 65 PERCENT.
    FABRICATION OF EQUIPMENT  IS NOW  IN PROGRESS. SYSTEM STARTUP IS SCHEDULED
    FOR  JUNE  1976.
I.D. NUMBER   91
SOUTHERN CALIFORNIA EDISON
MOHAVE NO IB
  620  Mw - RETROFIT
COAL   0.5- 0.6 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   6/77
   THE TOTAL CAPACITY OF BOILER IS 790 MW. EXISTING EXPERIMENTAL FGD NODULE
   WILL TREAT ONLY 170 MW.  FINAL SELECTION OF THE PROCESS HAS BEEN POST-
   PONED. SEE MOHAVE 1A.
I.D. NUMBER   95
SOUTHERN CALIFORNIA EDISON
MOHAVE NO. 2
  790  MW . RETROFIT
COAL   0.5 TO 0.6 X SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   6/77
   A PROTOTYPE 170 MW LIME SCRUBBING SYSTEM (HORIZONTAL MODULE) ON THIS UNIT
   WAS OPERATED FROM NOVEMBER 1973 UNTIL FEBRUARY 1975. AVAILABILITY FOR THE
   PERIOD 1/16/70 TO 2/9/75 AVERAGED 73.58.  THIS SYSTEM IS TO BE REINSTALL-
   ED AT THE FOUR CORNERS PLANT. OPERATED BY AhlZONA PUBLIC SERVICE.
                                                                                                      PEDCo-ENVIRONMENTAL
                                                                29

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
                                                                05/76
                       CURRENT MONTH
I.D. NUMBER   96
SOUTHERN ILLINOIS POWER COOP
SOUTHERN ILLINOIS POWER PT. 4
  184  MW - NEW
COAL
BABCOCK ft WILCOX
LIMESTONE' SCRUBBING
STARTUP   1/7B
    THE CONTRACT FOR THIS LIMESTONE SCRUBBING SYSTEM HAS BEEN AWARDED TO
    BABCOCK AND WILCOX. THE FGD SYSTEM WILL CONSIST OF 2 SCRUBBING MODULESi
    TREATING THE FLUE GAS FROM A COAL-FIRED BOILERt HAVING A NOMINAL DESIGN
    CAPACITY OF 691.500 ACFM AT 290F. THE DESIGN S02 REMOVAL EFFICIENCY IS
    89.4 PERCENT* BASED UPON AN INLET OF 3.326 PPM OF $02. THE CONSULTING
    ENGINEERING FIRM FOR THE PROJECT IS BURNS-MCDONALD.
1.0. NUMBER   97
SPRINGFIELD CITY UTILITIES
SOUTHWEST NO. 1
  200  MW - NEW
COAL 3.5 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP   8/76
    THE CONSTRUCTION OF THE BOILER AND FGD SYSTEM AT THIS INSTALLATION IS
    STILL PROCEEDING BEHIND SCHEDULE. THE SCRUBBER,  ESP, AND I.D.FANS ARE NOW
    BEING INSTALLED. COMPLETION IS SCHEDULED FOR MID-SUMMER 1976. SYSTEM
    STARTUP HAS BEEN DELAYED TO AUGUST 1,1976.
I.D. NUMBER   96
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A
   10  MW - RETROFIT
COAL 2.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
STARTUP   4/72
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
    TURBULENT CONTACT ABSORBER ITCA) LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN
    OPERATIONAL SINCE APRIL 1972.  THIS TEST PROGRAM IS FUNDED BY THE EPA.
    TVA IS THE CONSTRUCTOR AND FACILITY OPERATOR.  THE BECHTEL CORP. OF SAN
    FRANCISCO IS THE MAJOR CONTRACTOR, TEST DIRECTOR. AND REPORT WRITER.
I.D. NUMBER   99
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10B
   10  MW - RETROFIT
COAL 2.9 PERCENT SuLFUR
CHEMICO
LIME/LIMESTONE SCRUBBING
STARTUP   4/72
    REFER TO BACKGROUND INFORMATION SECTION  IN TABLE 3 OF THIS REPORT.  THIS
    VEMTURI/SPRAY TOkCR LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN OPERATIONAL
    SINCE APRIL 1972.  THIS TEST  PROGRAM IS  FUNDED BY  THE EPA.  TVA IS THE
    CONSTRUCTOR AND FACILITY  OPERATOR. THE  BECHTEL CORP. OF SAN FRANCISCO IS
    THE MAJOR CONTRACTOR,TEST DIRECTOR, AND REPORT WRITER.
I.D. NUMBER  100
TENNESSEE VALLEY AUTHORITY
WIUOWS CREEK NO 8
  550  MW - RETROFIT
COAL   3.7 PERCENT SULFUR
TENNESSEE VALLEY AUTHORITY
LIMESTONE SCRUBBING
STARTUP   2/77
    CONTRACTS HAVE  BEEN  LET  ON  ALL  MAJOR  PROCESS  EQUIPMENT  INCLUDING  THE
    SCRUBBER,  MIST  ELIMINATOR,  PIPING,  INSTRUMENTATION,  HOT AIR  INJECTION
    SYSTEM AND AIR  HEATER  FANS.  THE ID  FANS ARE NOW  BEING INSTALLED AS  IS  THE
    LIMESTONE CRUSHER. ALL EQUIPMENT REQUISITIONS HAVE BEEN COMPLETED*  THE
    SCHEDULED STARTUP DATE IS FEBRUARY  1977.   *
                                                                                                            PEDCo-ENVIRONMENTAL
                                                              30

-------
 COMPANY

 POWER STATIO.M
           TABLE 2
STATUS OF FGD SYSTEMS DURING  05/76

                       CURRENT MONTH
I.D. NUMBER  101
TEXAS UTILITIES CO.
MARTIN LAKE NO. 1
  793  Mki - NEW
COAL   1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   1/77
    THE CONTRACT FOR THIS FGO SYSTEM WAS AWARDED TO RESEARCH-COTTRELL. THIS
    NEW FACILITY IS NOW UNDER CONSTRUCTION. THE FGD SYSTEM STARTUP DATE IS
    NOW SCHEDULED FOR JANUARY 1977.
I.D. NUMBER  102
TEXAS UTILITIES CO.
MARTIN LAKE NO. 2
  793  MW - NEW
COAL   1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STAKTUP  10/77
    THE CONTRACT FOR THIS FGD SYSTEM WAS AWARDED TO RESEARCH-COTTRELL. THIS
    NEW FACILITY IS NOW UNDER CONSTRUCTION. THE FGD SYSTEM STARTUP DATE IS
    NOW SCHEDULED FOR OCTOBER 1977.
I.D. NUMBER  103
TEXAS UTILITIES CO.
MARTIN LAKE NO. 3
  793  MW - NEW
COAL 1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  12/78
    UTILITY HAS SIGNED A LETTER OF INTENT WITH RESEARCH COTTRELL. THE BOILER
    IS CURRENTLY BEING ERECTED AT THIS NEW FACILITY.
I.D. NUMBER  104
TEXAS UTILITIES CO.
MARTIN LAKE NO. H
    793 Mb - NEW
COAL i.o PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  12/79
    UTILITY HAS SIGNED A LETTER OF INTENT WITH RESEARCH COTTRELL.  THE BOILER
    IS CURRENTLY BEING ERECTED AT THIS NEW FACILITY.
I.D. NUMBER  105
UNITED POWER ASSOCIATION
COAL CREEK NO. 1
  545  Mb - NEW
LIGNITE - 0.63 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE
STARTUP  11/76
    THE UTILITY  IS CURRENTLY IN THE  PROCESS OF REQUESTING/EVALUATING  BIDS  FOR
    A NON-REGENERABLE LIME  OR LIMESTONE  SCRUBBING SYSTEM FOR S02 REMOVAL.  IN
    ADDITION.  THE  BIDDER  CAN ALSO  SPECIFY  ALKALINE FLYASH SCRUBBING AS  AN
    ALTERNATIVE  S02 REMOVAL PROCESS.  INITIAL STARTUP  OF  THE INSTALLATION IS
    NOW PROJECTED  FOR 6/78  WITH FULL  COMMERCIAL OPERATION BY 11/76.
                                                                                                            PEDCo-ENVIRONMENTAL
                                                                  31

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F6D SYSTEMS DURING
05/76
                       CURRENT MONTH
I.D. NUMBER  106
UNITED POWER ASSOCIATION
COAL CREEK NO. 2
  545  MW - NEW
LIGNITE - 0.63 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE
STARTUP  11/79
    THE UTILITY IS CURRENTLY IN THE PROCESS OF REQUESTING/EVALUATING BIDS FOR
    A NON-REGENERABLE LIME OR LIMESTONE SCRUBBING SYSTEM FOR S02 REMOVAL. IN
    ADDITION, THE BIDDER CAN ALSO SPECIFY ALKALINE FLYASH SCRUBBING AS AN
    ALTERNATIVE S02 REMOVAL PROCESS. INITIAL STARTUP OF THE INSTALLATION IS
    NOW PROJECTED FOR 8/79 WITH FULL COMMERCIAL OPERATION BY 11/79.
I.D. NUMBER  107
UTAH POWER & LIGHT CO.
EMERY NO.l
  i»00  MW . NEW
COAL 0.5 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   6/76
    THE CONTRACT FOR THIS FGD SYSTEM HAS BEEN AWARDED TO CHEMICO.  THE PEBBLE
    LIME WET SCRUBBING SYSTEM IS DESIGNED TO OPERATE IN AN OPEN-LOOP MODE
    WITH AN S02 REMOVAL EFFICIENCY OF 80 PERCENT  FOR LOW SULFUR UTAH COAL.
    PARTICULATE EMISSIONS WILL BE CONTROLLED BY AN UPSTREAM ESP,  THE SLUDGE
    WILL BE STABILIZED WITH FLYASH AND DISPOSED ON THE PLANT SITE.
I.D. NUMBER  108
UTAH POWER * LIGHT CO.
HUNTINGTON NO.l
  <»15  MW • RETROFIT
COAL  0.5 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   6/77
    A LETTER OF INTENT HAS BEEN SIGNED  WITH  CHEMICO FOR  THE  INSTALLATION OF
    A LIME SCRUBBING SYSTEM ON THIS  NEW UNIT.  MATERIALS  ARE  NOW  ARRIVING AT
    THE. PLANT SITE.  SITE PREPARATION AND CONSTRUCTION  IS NOW UNDERWAY.  THE
    STAJE  OF UTAH REGULATIONS REQUIRE THE BEST AVAILABLE AND MOST  COST
    EFFECTIVE TECHNOLOGY FOR S02 REMOVAL.
                                                                                                          PEDCo-ENVIRONMENTAL
                                                                32

-------
                      Table 3




PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS
                           33

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  09/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F60 VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 F6D STATUS

 EFFICIENCY,
  PARTICIPATES


  S02


 WATER MAKE UP


 SLUDGE DISPOSAL


 UNIT COST
 OPERATIONAL
  EXPERIENCE
 ARIZONA PUBLIC SERVICE

 CHOLLA NO 1

 JOSEPH CITY ARIZONA

  115 MW

 COAL   0.
-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                           THE  CHOLLA POWER  PLANT

     THE CHOLLA POWER STATION, LOCATED NEAR JOSEPH CITY,  ARIZONA,  HAS ONE  115-NW COAL-FIRED BOILER IN SERVICE AND TWO 250 MW UNITS UNDER CONSTRUCTION.
                                                   •
UNIT 1 IS A DRY-BOTTOM PULVERIZED-COAL-FIRED UNIT DESIGNED BY COMBUSTION ENGINEERING.  THE COAL NOW BEING-BURNED HAS AN AVERAGE HEATING VALUE (DRY BAS^S)
OF 12,146 BTU/LB AND ASH AND SULFUR CONTENTS OF 12.3  PERCENT AND 0.44 PERCENT, RESPECTIVELY.                   |                   .          ,     , ,i,
     THE FGD SYSTEM AT THE CHOLLA PLANT WAS MANUFACTURED  BY RESEARCH-COTTRELL AND  INSTALLATION WAS COMPLETED ON DECEMBER 3, 1973.  THE COMBINED S02
REMOVAL EFFICIENCY (FOR BOTH MODULES A AND B) IS REPORTED TO BE 58.5 PERCENT.  THE SYSTEM CONSISTS OF TWO SCRUBBING MODULES (A AND B).  EACH MODULE IS
DESIGNED FOR 240,000 ACFM THROUGHPUT AT 276°F, AND HANDLES 50 PERCENT OF THE BOILER'S FLUE GAS LOAD.  MODULF A HAS A VARIABLE-THROAT FLOODED-DISC
SCRUBBER (FDS) FOLLOWED BY A PACKED TOWER: MODULE B IS SIMILAR  BUT THE TOWER IS NOT PACKED AND SLURRY IS NOT CIRCULATED THROUGH IT.  EITHER ONE OR BOTH
OF THE SCRUBBERS CAN BE BYPASSED.  GAS LEAKAGE AROUND EACH TRAIN IS ESTIMATED TO BE ABOUT 4.5 PERCENT OF THE GAS BEING TREATED.  THE TOWER PACKING,
WHICH IS ABOUT 2 FEET THICK, IS MADE OF POLYPROPYLENE CORRUGATED SHEETS JOINED TOGETHER  IN CRISS-CROSS PATTERNS SIMILAR TO HONEYCOMBS.  THE TOWER
DEMISTERS ARE MADE OF POLYPROPYLENE, AND THE REHEATERS ARE SHELL AND TUBE  TYPE CONSISTING OF THREE TUBE BUNDLES.
     LIMESTONE FOR THE FGD SYSTEM IS PURCHASED IN GROUND  FORM SUITABLE FOR SLURRYING.  THE MAIN SOURCE OF SUPPLY IS THE SUPERIOR CO., LOCATED NEAR
PHOENIX, ARIZONA.
     THE PLANT HAS NO SLUDGE TREATMENT OR FIXATION SYSTEMS. THE SLUDGE IS PUMPED TO THE FLY ASH POND ON AN INTERMITTENT BASIS THROUGH A COMMON PIPING
SYSTEM WITH THE FLY ASH.  NO POND WATER IS RECYCLED TO THE FGD  SYSTEM.
PROBLEMS AND SOLUTIONS
     DECEMBER. 1973 TO APRIL 2. 1974 - BECAUSE OF A DIFFERENCE  IN  SIZE OF  THE MAIN DUCT AND THE REHEATER TRANSITION DUCT, THE-GAS FLOW PRODUCED HARMONIC
VIBRATIONS IN THE REHEATER.  THE VIBRATIONS WERE PARTIALLY DAMPED  BY INSTALLATION OF BAFFLES.  ONE OF THE REHEATER TUBE BUNDLES WAS BADLY CORRODED
BY ACID THAT CONDENSED IN THE UNINSULATED DUCT UPSTREAM OF THE  REHEATERS.  THE TUBE BUNDLE WAS REPLACED, AND A BAFFLE WAS INSTALLED TO DIVERT CONDENSED
ACID FROM REHEATER TUBES.  ALSO. THE DUCT UPSTREAM OF THE REHEATER WAS INSULATED.  THE ACID CONDENSATION OCCURRED ONLY IN THE MODULE WITH NO TOWER
PACKING AND HENCE LOW S02 REMOVAL EFFICIENCY.
                                                                                                                               PEDCo-ENVIRONMENTAL
                                                                          36

-------
CHOLLA POWER PLANT (Continued)
     ANOTHER PROBLEM WAS DUE TO SOLIDS BUILDUP IN THE  FDS STUFFING GLAND BOX AND ON TOP OF THE SPRAY DOME.  ALSO, SOME LINES PLUGGED,  PARTICULARLY
WHEN THE SYSTEM OPERATED AT LOW FLOW RATES.   SOLIDS  SETTLED OUT  IN STANDBY PUMPS, AND EXCESSIVE FAN VIBRATIONS OCCURRED BECAUSE OF ACCUMULATION OF SCALE
BUILDUP WHEN THE UNIT WAS IDLE.  TO SOLVE THESE PROBLEMS, PACKING GLAND POSITION WAS REVERSED (INSTALLED UPSIDE DOWN). THE FAN WAS SANDBLASTED, THE
PIPING WAS MODIFIED TO ELIMINATE STAGNANT POCKETS, AND PUMPS WERE FLUSHED IMMEDIATELY AFTER REMOVAL FROM SERVICE.
     MORE RECENT PROBLEMS INCLUDE:   SIGNIFICANT CORROSION ATTACH IN THE VESSEL WALLS OF THE FLOODED-DISC PARTICUALTE SCRUBBER OR MODULE;  ACID CORROSION
IN THE REHEATER HOUSING OF MODULE B; SCALE BUILDUP IN  THE PIPE OUTLET AT THE SLUDGE/FLY ASH EVAPORATION POND; PLUGGING IN THE SCRUBBER TOWER PACKING
AND MIST ELIMINATOR; EROSION IN THE PUMPS; CORROSION IN THE BOILER EXHAUST ELBOW OF THE DUCTWORK LEADING FROM THE SCRUBBERS TO THE STACK.
                                                                                                                              PEDCo-ENVIRONMENTAL
                                                                         37

-------
   FGD SYSTEM RELIABILITY
      CHOLLA UNIT NO.  1

Month
Jan. 74
Feb. 74
Mar. 74
Apr. 74
May 74
Jun. 74
Jul. 74
Aug. 74
Sep. 74
Oct. 74
Nov. 74
Dec. 74
Jan. 75
Feb. 75
Mar. 75
Apr. 75
May 75
Jun. 75
Jul. 75
Aug. 75
RELIABILITY
(*)
Module A Module B
97
100
100
66
98
100
97
97
95
83
100
100
98
96

88
48
100
97
95
90
94
66
57
99
100
92
97
99
68
98
100
99
99

65
40
100
98
100
                   Comments
Annual boiler and FGD System overhaul.
Modules were both off-line for most of month for  scheduled repairs and cleaning.
Substantial plugging of packing and mist eliminators was observed.
No problems reported.
Modules were shut down to clean flow restrictions 1n flooded-dlsc reclrculatlon lines.
Module A  was down for Inspection one time.
                                                                      PEDCo-ENVIRONMENTAL
                   38

-------
                                                          FGD SYSTEM RELIABILITY
                                                       CHOLLA UNIT NO. 1 (continued)
Month
Sep. 75
Oct. 75
Nov. 75
Dec. 75

Jan. 76
 Feb. 76
 Mar. 76
 Apr. 76
99
99
99
98
                         Comments
Minor outage due to flooded-dlsc lines.
Outages resulted from scheduled equipment overhauls and recoatlng of vessels.
No major outages or problems occurred during the report period.  Minor problems
during December Included the rebuilding  of a recycle  pump and malfunctioning of
the B-side reheater coll.
Module A operated 715 hours during the report month,  and Module  B operated 654 hours.
Module A experienced some minor valve and line plugging.  Module B operating hours were
lower because of reduced system requirements.
The unit 1s currently experiencing coating failures 1n the elbow of the  scrubber exhaust duct.
Also, the utility performed some minor repairs to the housing of the B-s1de reheater.
                                                                                                                         PEDCo-ENVlRUNirtt.mL
                                                                          39

-------
                    TABLE  3
 PERFORMANCE  DESCRIPTION FOR  OPERATIONAL  F6D  SYSTEMS  05/76


  IDENTIFICATION NO.     10

  UTILITY NAME          ARIZONA PUBLIC SERVICE

  UNIT NAME             FOUR  CORNERS NO.  5A

  UNIT LOCATION         FARMINGTON NEW MEXICO

  UNIT RATING            160  MW

  FUEL CHARACTERISTICS  COALi 0.7 PERCENT SULFUR

  FGD VENDOR            SCE

  PROCESS               LIME SCRUBBING

  NEW OR RETROFIT       RETROFIT

  START UP DATE          2/76

 FGD STATUS            OPERATIONAL

 EFFICIENCY.
- PARTICULATES


  S02


 WATER  MAKE UP


 SLUDGE  DISPOSAL


 UNIT COST
  rr                  ™IS  16° MW  SYSTE" H«S BEEN MOVED FROM THE MOHAVE STATION OF SOUTHERN
  EXPERIENCE            CALIFORNIA EDISON WHERE THE SYSTEM WAS PREVIOUSLY TESTED. THE SYSTEM
                       WILL  TREAT APPROXIMATELY 20 PERCENT OF THE FLUE GAS FROM UNIT NO. 5,
                       RATED AT 755 MW(NET). THE ENGINEERING AND CONSTRUCTION WORK HAS BEEN
                       COMPLETED. THE SYSTEM BECAME OPERATIONAL ON FEBRUARY 17i 1976. THE EXPER.
                       IMENTAL SCRUBBER HAS TAKEN OUT OF SERVICE IN MID-APRIL FOR A SCHEDULED
                       BOILER OVERHAUL*
                                                         40
                                                                                                       PEDCo-ENVIRONMENTAJ.

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
  29


 COMMONWEALTH EOISON


 WILL COUNTY NO 1


 RONCOVILLE ILLINOIS


  167 MW


 COAL - 9<»63 BTUt   2.IX SULFUR


 BABCOCK ft WILCOX


 LIMESTONE SCRUBBING


 RETROFIT


  2/72


 OPERATIONAL



 98 PERCENT
  S02
 82 PERCENT
 WATER MAKE UP
 106 GAL/LB MOLE S02 REMOVED
 SLUDGE DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  CLAY LINED POND
 UNIT COST
S96/KW CAP. W/NO SLUDGE TREAT.6.9 MILLS/KWH AT 653 BLR. CAP.
 OPERATIONAL
  EXPERIENCE
 REFEK TO BACKGKOUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE FEBRUARY 1972. THE UNIT WAS RE-
 TURNED TO SERVICE IN MAKCH FOLLOWING A MAJOR BOILER, TU.iBINE, AND SCRUB-
 BER OVERHAUL. SYSTEM OPERABILITY FOR BOTH MODULES DURINu THE REPORT
 PERIOD WAS <*5 AND 20 PERCENT IN MARCH AND 20 AND H9 PERCENT IN APRIL FOR
 MODULES A AND U RESPECTIVELY. MODULES A AND B WERE IN SERVICE A TOTAL OF
 3213 AND 2580 HOURS HOURS RESPECTIVELY* IN 1975, WHICH TRANLATES INTO
 ANNUAL OPERABILITY FACTORS OF 52 AND <»2 PERCENT RESPECTIVELY.
                                                           41
                                                                                                      PEDCo-ENVIRONMENTAL

-------
                                                          BACKGROUND INFORMATION
                                                                    ON
                                                        THE WILL COUNTY POWER STATION

     IN 1970. COMMONWEALTH EDISON CONTRACTED WITH BECHTEL  CORPORATION TO  INVESTIGATE THE SULFUR REMOVAL SYSTEMS THEN AVAILABLE HAVING A SUFFICIENT
DEGREE OF DEVELOPMENT TO WARRANT LARGE-SCALE INSTALLATION  ON WILL COUNTY  STATION'S UNIT NO. 1.  AFTER DECIDING ON A WET SCRUBBER SYSTEM USING LIME OR
LIMESTONE, BECHTEL PREPARED A SPECIFICATION AND RELEASED IT FOR BID.  FROM NINE BIDDERS THAT WERE SOLICITED, SEVEN PROPOSALS WERE RECEIVED.  AFTER
DETAILED STUDY AND BID EVALUATION WITH SPECIAL CONSIDERATION OF THE PROJECT SCHEDULE, BABCOCK AND WILCOX WAS AUTHORIZED IN SEPTEMBER 1970 TO BEGIN
DETAILED ENGINEERING FOR A LIMESTONE SLURRY SYSTEM.   COMPLETION DEADLINE  FOR THE PROJECT WAS DECEMBER 31, 1971, A DEADLINE ESTABLISHED BY THE
ILLINOIS COMMERCE COMMISSION AS PART OF A RATE CASE.
     THE BABCOCK AND WILCOX PROCESS WAS GUARANTEED TO REMOVE .98 PERCENT OF THE FLY ASH AND 76 PERCENT OF THE SULFUR DIOXIDE.  THESE EFFICIENCIES
WERE BASED ON A DUST INLET LOADING OF 1.355 GRAINS PER STANDARD CUBIC FOOT AT 70°F AND ON BURNING OF ILLINOIS COAL CONTAINING 4 PERCENT SULFUR.
     THE WILL COUNTY POWER STATION IS LOCATED"NEAR ROMEOVILLE,  ILLINOIS.  THE PLANT HAS FOUR ELECTRIC POWER GENERATING UNITS WITH A TOTAL RATED
CAPACITY OF 1147 MW.  ONLY UNIT NO. 1 IS RETROFITTED WITH  AN FGD SYSTEM.
     UNIT NO. 1 IS A WET-BOTTOM COAL-FIRED BOILER PRODUCING  167 MW OF ELECTRICITY.  THE BOILER WAS MANUFACTURED BY BABCOCK AND WILCOX AND WAS INSTALLED
IN 1955.  THE PLANT NOW BURNS A LOW-SULFUR (K3 PERCENT) WESTERN COAL AND A HIGH-SULFUR ILLINOIS COAL.
     THE WET LIMESTONE FGD SYSTEM AT WILL COUNTY WAS PLACED  IN  SERVICE ON FEBRUARY 23, 1972.  THE SYSTEM CONSISTS OF TWO FGD MODULES (IDENTIFIED AS
A AND B), LIMESTONE HANDLING AND MILLING FACILITIES, AND A SLUDGE TREATEMENT AND STABILIZATION UNIT.  S02 REMOVAL EFFICIENCY IS REPORTED TO BE
82 PERCENT.  SHORTLY AFTER STARTUP AND DURING INITIAL SHAKEDOWN, NUMEROUS PROBLEMS WERE ENCOUNTERED.  COMMONWEALTH EDISON SHUT DOWN MODULE B IN
MAY 1973 TO CONCENTRATE ON SOLVING THE PROBLEMS OF MODULE  A.  MODULE  B WAS NOT RESTARTED UNTIL MAY 1975.
     THE LIMESTONE GRINDING FACILITIES CONSIST OF TWO WET  BALL  MILLS, EACH RATED AT 12 TONS PER HOUR. OF LIMESTONE.  THE LIMESTONE IS 97.5 PERCENT
CALCIUM CARBONATE, AND CONTAINS 0.99 PERCENT MAGNESIUM CARBONATE AND  0.48 PERCENT SILICA.  IT IS RECEIVED IN COARSE-GROUND FORM (ABOUT 1/2 INCH OR
LESS) AND IS FINELY GROUND TO 95 PERCENT THROUGH 320 MESH.
                                                                                                                          PEDCo-ENVIRONMENTAL
                                                                        42

-------
MILL COUNTY (Continued)

     SLUDGE FROM THE SYSTEM IS SENT TO A CLARIFIER.  THE OVERFLOW IS RETURNED TO THE PROCESS;  THE UNDERFLOW IS  STABILIZED BY MIXING IT WITH LIME AND
FLY ASH.  ABOUT 200 POUNDS OF LIME AND 400 POUNDS OF FLY ASH ARE USED PER TON OF DRY SOLIDS OF SLUDGE.   THE FIXED SLUDGE IS TRANSPORTED BY CONCRETE
MIXING TRUCKS TO AN ON-SITE HOLDING BASIN FOR SOLIDIFICATION.  THE STABILIZED MATERIAL IS THEN HAULED AWAY  APPROXIMATELY A WEEK LATER TO AN OFF-SITE
DISPOSAL AREA.
PROBLEMS AND SOLUTIONS
     1972 - DEMISTER PLUGGING WAS A CONSTANT PROBLEM, MAINLY BECAUSE OF HEAVY LIMESTONE ACCUMULATIONS ON THE BOTTOM OF THE DEMISTER AND PARTLY BECAUSE
OF LOW WASHWATER PRESSURE CAUSED BY LEAKS IN THE POND RETURN BYPASS.  BECAUSE OF THESE PROBLEMS MODULES A AND B WERE OUT OF SERVICE FOR SEVERAL DAYS
EACH MONTH DURING MARCK, APRIL, JUNE, AND JULY 1972.  THE MODULES WERE ALSO OUT OF SERVICE FROM SEPTEMBER 26 TO NOVEMBER 21, 1972, BECAUSE THE BOILER
WAS DOWN.
     IN ORDER TO SOLVE THE DEMISTER PROBLEM, THE SLURRY NOZZLES WERE LOWERED AND THE SLURRY CIRCULATION SYSTEM  WAS  LEFT OUT OF SERVICE TO KEEP THE
DEMISTER CLEAN.  SINCE THE SITUATION DID NOT IMPROVE, THE DEMISTER ELEMENTS WERE HAND-WASHED.   THIS SOLVED  THE  PROBLEM PARTIALLY, BUT CAUSED DIFFICULTY
WITH THE VENTURI NOZZLES BECAUSE BROKEN ELEMENTS FROM THE DEMISTER GOT INTO THE SLURRY SYSTEM.
     AT HIGH GAS FLOW RATES, THE REHEATER OF MODULE B VIBRATED EXCESSIVELY.  THEREFORE, MODULE B WAS TAKEN  OUT  OF SERVICE IN APRIL TO ALLOW REHEATER
MODIFICATIONS, WHICH INCLUDED REBRACING OF THE REHEATER TUBES AND INSTALLATION OF A BAFFLE PLATE TO REDUCE  THE  VIBRATIONS.
     OTHER REASONS FOR OUTAGES WERE EROSION AND PLUGGING OF SPRAY NOZZLES, INTERNAL AND EXTERNAL BUILDUP OF DEPOSITS ON VENTURI NOZZLES, CORROSION,
SULFITE BLINDING PROBLEMS, AND FAN VIBRATIONS.
     1973 - DEMISTER PLUGGING CONTINUED.  FURTHERMORE, THE DEMISTER ON MODULE B BROKE LOOSE FROM ITS MOUNTINGS  AND  THE RESULTANT CARRYOVER OF WASH-
WATER PLUGGED THE REHEATER.  THIS REHEATER ALSO LEAKED BECAUSE OF CHLORIDE PITTING CORROSION.   MODULE A WAS DOWN FROM APRIL 24 TO MAY 24, 1973, AND
MODULE B WAS DOWN FROM APRIL TO DATE.  THERE WAS NO SCRUBBER OPERATION FROM AUGUST 27 to SEPTEMBER 26,  1973.
     IN EFFORTS TO SOLVE THE DEMISTER AND REHEATER PROBLEMS, A CONSTANT UNDERSPRAY AND INTERMITTENT OVERSPRAY WERE  USED TO WASH ALL THE DEMISTER
COMPARTMENTS OF MODULE A.  EXTRA NOZZLES WERE ADDED AND A CLEAN WATER SUPPLY WAS MAINTAINED.  THE REHEATER  UNIT WAS ALSO RETUBED.
     1974 - ONLY MODULE A OPERATED DURING 1974.  THE MAIN PROBLEMS WERE FREEZING OF THE VENTURI THROAT  DRIVE MECHANISM, TANK SCREEN BLINDING, DUCT
CORROSION, AND VIBRATIONS.  LOSS OF BUILDING HEAT CAUSED EXTENSIVE DAMAGE AND KEPT THE SYSTEM DOWN FOR  THE  ENTIRE MONTH OF JANURY 1974.
     1975 - ENTERING 1975 MODULE A WAS OPERATIONAL AND MODULE B WAS STILL UNDERGOING MODIFICATION.  IN  THE  FIRST QUARTER OF 1975 THERE WERE EIGHT
A-MODULE OUTAGES; ONLY ONE HAS A FORCED OUTAGE. DUE TO THE SPLITTING OF A SLURRY VENTURI SUPPLY HOSE.  MOBULE B WAS RETURNED TO SERVICE ON MAY 20, 1975.

                                                                                                                             PEDCo-ENVIRONMEMlAL

                                                                       43

-------
WILL COUNTY (continued)
THE UTILITY DECIDED TO OPERATE THE  SCRUBBER ON ILLINOIS HIGH-SULFUR COAL.   WHEN THIS OPERATION BEGAN, A MULTITUDE OF PROBLEMS OCCURRED:   LOWER
PARTICULATE REMOVAL EFFICIENCIES, HIGH SLURRY CARRYOVERS. DEMISTER PLUGGING, REHEATER COIL FOULING AND LEAKS.  MODULE A WAS TAKEN OUT OF SERVICE
IN MID-JUNE FOR THE REMAINDER OF 1975.  BY MID-SEPTEMBER 1975 MODULE B WAS TAKEN OUT OF  SERVICE OWING TO MASSIVE SCALING IN THE ABSORBER SYSTEM.
FINALLY. UNIT NO. 1 WAS  SHUT DOWN FOR OVERHAUL OF THE BOILER. TURBINE. AND SCRUBBER IN MID-OCTOBER; THIS OUTAGE LASTED MORE THAN 4 rtONTHS.
     OPERABILITY FACTORS FOR EACH MODULE AND THE CORRESPONDING COMMENTS FOR THE REPORT PERIOD ARE PRESENTED IN THE FOLLOWING TABLE.
                                                                                                                        PEDCo- ENVIRONMENTAL

                                                                     44

-------
                                                           FGD SYSTEM OPERABILITY
                                                           WILL COUNTY UNIT NO.  1 *
  PERIOD            OPERABILITY (X)
Month/Year        Module A   Module B
Mar. 72               0        35
Apr. 72
May  72
Jun. 72
Jul. 72
Aug. 72
34
70
14
32
          31
79
21
                         Comments
Module A down for repair and modification of demister wash  piping assembly.
Module B was removed from service every 2 or 3 days  to  hand-wash the demister.
Other problems were vibration of reheater tube bundle,  rapid  erosion of scrubber
spray nozzles, plugging of venturl nozzles.
Module A out of service for 6 days because of near-rupture  of a venturl pipe
expansion joint.  Heavy buildup of sol Ids on demister.   Module B out of service most
of the time for similar repair of venturl pipe expansion joint, and for modification
of reheater unit and demister wash system.
A two week outage of Module B to rebrace the reheater  unit, to Install underspray
nozzles on demister, and to Install heavier screens  In the  sump.  Reheater plugging
caused additional outages.
Both Modules were out of service owing to high differential pressure across the
demlsters.  Leakage of pond return bypass valve caused demister  plugging.   Also during  this
period, the rubber lining of scrubber A was repaired.

Plugging of venturl nozzles and demister caused shutdown of Module  A for  2 days for
repairs.  Module B was out of service for 22 days for cleaning of the  demister and
reheater unit,  Installation of overhead spray nozzles, and replacement of sections
of the demister.  The boiler was down for 2 days for repair of the  generator.
                                                                                                                          PEDCo-ENVIRONMENTAl
                                                                      45

-------
                                                    HILL COUNTY UNIT NO. 1 (continued)
  PERIOD
Month/Year
Sep. 72
Oct. 72
Mar. 73

Apr. 73

May 73
Jun. 73

Jul. 73
  OPERABILITY (X)
Module A   Module B
    0        30.
Nov. 72
Dec. 72
Jan. 73
Feb. 73
0
22
0
22
0
30
0
24
   65
    0
    16

    51
11

13

 0
 0
                         Comments
Boiler down Sept.  1-5 because of no demand.   I.D. fan problem caused unstable operation of the
boiler most of the month.   Module  A was  down  for modification of reheater unit and repair of
redrculatlon tank screens.
Boiler and scrubbers were down.  Principal modifications  Included Installation of
reheater baffle plates to dampen vibrations and Installation of an experimental demlster
wash system.
Boiler problems causing unstable operation kept both modules down during this month.
Modules operated Intermittently because  of electrostatic  preclpltator testing and mis-
cellaneous Instrument problems.
Both modules were down for repairs and modifications.
Modules were out of service because of cracks In  the Inlet ductwork of  the booster fan.
Improper Installation of demlster  caused plugging of Module B reheater  unit.
Module A was out of service for 5  days because of demlster plugging.  Boiler was down
for 4 days of Inspection.  Module  B was  down  because of leaks from reheater tubes.
Persisting problems with demlster  and deposits of calcium sulfate scale on reheater
tubes of Module A.
Both modules were out of service during  this  month.
Module B was kept down to allow concentration on  the problems with Module A.  Boiler-
related problems were responsible for most of the outages of Module A.
Module A problems:  reheater tubes leaks and high fan vibrations.
                                                                                                                              PEDCo-ENVIRONMEFITAL
                                                                        46

-------
                                                     WILL COUNTY UNIT NO.  1  (continued)
  PERIOD
Month/Year
Jul. 73
Sep. 73

Oct. 73

Nov. 73
Dec. 73
Jan. 74
Feb. 74
Mar. 74
Apr. 74
May  74
  OPERABILITY (X)
Module A   Module B
   19         0
    0         0

   32         0

   51         0
   21
   72
   93
                       •  Comments
More reheater tube leaks on Module A attributed to chloride corrosion attack.
Modules were down.  During this month.  Chicago Fly Ash Co. finished cleaning and treating
the northeast half of the sludge pond.
Module A tripped several times because  of bad limit switches  In  the bypass and block dampers.
Unit was also taken down to balance the booster I.D. fan.
Routine Inspection of Module A revealed some plugging.  Module was kept down for cleaning
and some modification.  Poor gas distribution In module suspected to contribute to demlster
problems.
Modules were down.  The month was devoted to modification and maintenance, mostly of demlster,
ventuM throats, pumps, and Isolation valves.
Modules were down owing to freezing In  the 10-Inch-diameter,  4400-ft. line between modules"
and pond.  Some damage to sump pumps.  Freezing also damaged  some Instruments.
The frozen pipeline was thawed, reanchored, and returned to service.  The Instruments
damaged by freezing were repaired.  Module A kept down until  arrival of second-stage
demlster.
Module A was ready for service March 20 but was not returned  to  service till March 27    ''
because boiler was down.
Module A continued to operate until April 19 (except for two  short  inspection outages) for
23 consecutive days.  Operation was on  low-sulfur coal.  Sump screen from Module B was
substituted for damaged screen In Module A.
Module. A operated for entire month except for short outages for  Inspection.  Much of this
operation was on high-sulfur coal.
                                                                                                                                PEDCo-ENVIRONMENTAL
                                                                        47

-------
                                                     HILL COUNTY  UNIT NO. 1  (continued)
  PERIOD
Month/Year
Jun. 74

Jul. 74

Aug. 74

Sep. 74

Oct. 74

Nov. 74
Dec. 74

Jan. 75

Feb. 75
  OPERABILITY (X)
Module A   Module B
   55         0

   96         0

   91         0

   85         0

   94         0
   97
   99

   99

   99
0
0
                         Comments
Module A operated for about 300 hours.   The system was  off for  2 weeks  for repair of venturl
throat drive.
Module A operated for the whole month except for one Inspection outage  and two  boiler
shutdowns.  Module B remains down until  satisfactory operation  of Module A Is achieved.
Module A was down six times this month:   three times because of no  boiler demand, twice
for repair of leaks In steam piping,  and once for balancing of  a fan.
Module A was off three times;  once for  cleaning of deposits from the venturl throat, once
for repair of a desuperheater leak, and  once because boiler was down.
Module A was down four times:  once because of boiler outages,  once for Inspection, and
twice for repair of reheater leaks.
Module A was out of service three times:  twice because of no demand and once for Inspection.
Module A was down twice:  once for Inspection and once  for repair of valve In spent-liquor
line to pond.
Module A was down twice:  once for Inspection and once  for no demand.   Modification
of module B Is continuing.
Module A was out of service twice: once for Inspection and once for no demand.  One small
reheater leak 1n a stainless steel bundle was blanked-off on-line.   During the  Inspection,
demlster underwash nozzles were cleaned  and a small section of  demlster was replaced.
Inspection showed that conditions Inside the scrubber were about the same as before.  Coal
burned this month averaged less than  IX  sulfur.  Modification of Module B Is continuing.
Chicago Fly Ash Is treating material  from the scrubber  with portland cement and fly ash and
                                                                                                                              PEDCp-ENYIRONMENTAL

-------
                                                      HILL COUNTY UNIT NO.  1  (continued)
   PERIOD
 Month/Year

 Mar. 75

 Apr. 75
 Nay  75
Jun. 75
Jul. 75
Aug. 75
  OPERABILITY (*)
Module A   Module B

   40         0

   40         0
   84
  61
37
85
            79
   0       .100
                          Comments
 dumping the treated material  Into  the  north half of the holding basin.
 Module A was down four  times:   twice for no demand, once for a venturl hose leak, once for an
 accidental  50-mlnute trip.
 Sludge pond was  overburdened  by near-continuous operation of Module A.  The FGD system was
 shut down to allow evaporation  of water from the pond.  During shut down, the following
 modifications were made.  Pump  gland water flows were reduced from 10 to 5 gpm.  Filter
 backwash was routed out of sys'tem.  Continuous demlster underspray was changed to Intermittent.
 Module A reminded out of service until May 5, when It was determined that there was enough
 freeboard In the  pond to start  operating.  There were two more outages:  one for 45 minutes,
 the  result  of a damper trip; the other for cleaning of underspray nozzles.
 Module B was  placed  In service  10:20.A.M., May 20, for the first time since noon on April
 13,  1973.   After  brief start-up, which was routine, operation was delayed until the 20th
 because of  two broken oil pumps on the reclrculatlon tank mixers.  Since the start-up,  Module B
 has  been  out  of service twice:  once for a venturl pump trip, and once for a reclrculatlon
 tank  level  trip.   The total outage time was only 1 hour. 40 minutes.
 Module  A  sustained five outages during the month.   Module Is presently out of service to allow
 Installation of new demlsters and reheater.  Module B  was out of service 8 times.   Longest
 outage was  for 95 hours for cleaning of booster fan and demlster.   Booster fan vibrations
 caused a  shutdown on June 30.
Module A  cannot be returned to service until  the new reheater,  ordered In April,  Is  received
and Installed.  Module B sustained  four outages.   Reheater  failures at 1000 hours seem  to  be
caused by vibration fatigue.   One minor steam header leak also  occurred.

                                                                       PEDCo-ENVIRONMENTAL
                                                                        49

-------
                                                      WILL COUNTY  UNIT  NO.  1  (continued)
   PERIOD            OPERABILITY (%)
 Month/Year        Module A   Module  B
 Sep.  75               0        63
 Oct.  75


 Nov.  75


 Dec.  75

 Jan.  76
 Feb.  76
Mar.  76


Apr. 76
 0        100
 0          0
45         20
20
49
                          Comnents
 Nodule A remained out of service all month  because of delay on the new reheater order.
 Module B was down three times  because of massive absorber scale, demlster and  I.D. booster
 fan cleaning, balancing I.D. booster fan, and plugging of absorber pump screen.  Total outage
 time was 238 hours,  40 minutes.
 On October  11,  overhaul  began  on the Will County Unit No. 1 boiler, turbine, and scrubber.
 Module B experienced two minor outages during the 11-day period prior to the overhaul.
 Module A was down for delivery of the new reheater.
 The scheduled overhaul  of the  boiler, turbine, and scrubber modules continued.  Major
 maintenance  areas included module reheaters, pond return pump, venturl spray nozzles,
 venturl  and  absorber modules,  pump valves, and sumps.
 Module B reheater was  returned from manufacturer after repairs and revisions.  Scrubber re-
 heaters  could be  Installed and operating by the end of January.
 The unit remained out of  service for completion of the boiler, turbine,  and scrubber over-
 haul  that began on October 11, 1975.  System restart Is now scheduled for mid-March 1976.
 Unit  No.  1 returned  to service 1n March following an extended  major boiler,  turbine and
 scrubber overhaul.  Module A was put into the gas path on March  22 and remained 1n  service
 until March 29 because of delays 1n the Installation of a repaired reheater.
 During the month of April Module A Incurred  pump liner failures when  an  Isolation valve broke
and fell into the venturl recycle pump.   Module B outages during  the  month resulted from reheater
tube bundle leaks; plugged absorber tank  screens;  and venturl  pump liner failure.   High
sulfur coal  (3.5 percent sulfur)  was burned  in  the boiler throughout  the month.  In addition, the
utility initiated a testing  and evaluation program during the  month.   This program  1s designed
to provide data and Information concerning chemistry  and  related operating characteristics.
                                                                         50
                                                                                                                                PEDCo- ENVIRONMENTAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  05/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
  31
 DUOUESNE LIGHT
 ELRAHA
 ELRAMA PENNSYLVANIA
  510  nw
 FUEL CHARACTERISTICS  COAL  1.0  -  2.6 PERCENT  SULFUR
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP  DATE
 FGD STATUS
 EFFICIENCY.
 PARTICIPATES
 S02

 WATER HAKE UP
 CHEniCO
 LINE  SCRUBBING
 RETROFIT
 10/75
 OPERATIONAL
63 PERCENT FOR 2» SULFUR COAL
SLUDGE DISPOSAL
 STABILIZED SLUDGE DISPOSED IN  UNLINED POND
UNIT COST
                     S93/KW CAPITAL
OPERATIONAL
 EXPERIENCE
THE FGD SYSTEM WAS PLACED IN SERVICE ON OCTOBER 26t  1975.  INITIAL
OPERATION PROCEEDED WITH FLUE GAS FROM ONE BOILER BEING TREATED BY THE
SCRUBBING SYSTEM. A SECOND BOILER WAS TIED INTO THE  SYSTEM ON FEBRUARY <*.
1976. DURING THE REPORT PERIOD MODIFICATIONS TO THE  FIFTH  SCRUBBING VES-
SEL WERE COMPLETED AND THE VESSEL IS NOW OPERATING WITH TWO RUBBER-LINED
                                                                                                       PEDCo-ENVIRONMENIAL
                                                         51

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                            ELRAMA POWER STATION

     DUQUESNE LIGHT COMPANY, AN INVESTOR-OWNED ELECTRIC UTILITY. SERVES ABOUT ONE-HALF MILLION CUSTOMERS  IN SOUTHWESTERN PENNSYLVANIA AND HAS A NET
GENERATING CAPABILITY OF APPROXIMATELY 2500 MW.  THIS CAPABILITY IS GENERATED BY COMBUSTION TURBINES  IN SIMPLE AND COMBINED-CYCLE MODES, BY NUCLEAR
PLANTS, AND BY COAL-FIRED POWER STATIONS.  THE COMPANY IS SOLE OWNER AND OPERATOR  OF  THREE COAL-FIRED STATIONS, TWO OF WHICH HAVE BEEN RETROFITTED WITH
WET SCRUBBERS USING LIME AS A REAGENT.
     THE SCRUBBER FACILITY AT THE 494-MW ELRAMA STATION IS ALMOST IDENTICAL TO THE SYSTEM AT THE  PHILLIPS STATION.  GIBBS & HILL IS THE ARCHITECT-
ENGINEER, AND CHEMICO SCRUBBERS HAVE BEEN INSTALLED WITHIN THE SAME DESIGNATED BATTERY AS AT PHILLIPS.  MECHANICAL AND ELECTRICAL DUST-REMOVAL EQUIPMENT
REMOVES MOST PARTICULATES FROM THE BOILER EMISSIONS, AND THE GAS TO AND FROM THE SCRUBBERS IS HEADERED IN THE SAME WAY.  UNLIKE THE PHILLIPS SYSTEM.
HOWEVER. THERE ARE FOUR BOILERS. EACH WITH ITS OWN TURBINE GENERATOR.  FIVE SINGLE-STAGE SCRUBBERS WERE INSTALLED. WITH THE INTENTION THAT KNOWLEDGE
GAINED FROM THE TEST PROGRAM AT PHILLIPS WOULfr BE APPLIED TO ELRAMA TO ENABLE COMPLIANCE WITH EMISSION REGULATIONS.
                                              *
     THE FIRST ELRAMA SCRUBBER WAS PLACED IN SERVICE ON OCTOBER 26, 1975.   IT HAD  BEEN SCHEDULED  FOR  AN EARLIER STARTUP DATE, BUT BECAUSE OF THE
SEVERITY AND NUMBER OF PROBLEMS ENCOUNTERED AT PHILLIPS. STARTUP WAS DELAYED UNTIL MANY OF THE PROBLEMS AT PHILLIPS WERE RESOLVED AND THE MODIFICATIONS
COULD BE INCORPORATED AT BOTH STATIONS.
     BOILER NO. 2 WAS INITIALLY CONNECTED TO THE FGD SYSTEM ON OCTOBER 26.  1975.  THIS BOILER HAS AN  EQUIVALENT CAPACITY OF APPROXIMATELY 100 MW, AND
THE EMISSIONS ARE HANDLED BY ONE SCRUBBER.  TO ENSURE RELIABILITY IN THE CASE OF A SCRUBBER MALFUNCTION,  TWO SCRUBBERS ARE OPERATED AT PARTIAL LOAD
TO PROTECT THE BOILER AND TURBINE GENERATOR AGAINST A TRIP-OFF.
     THE BOILER OPERATED CONTINUOUSLY ON THE SCRUBBER SYSTEM THROUGH JANURY 1976.   TWO MINOR OUTAGES  OCCURRED DURING THIS PERIOD. ONE CAUSED BY
INOPERATIVE THROAT DAMPERS AND THE OTHER INVOLVING FAILURE OF A LIME FEEDER BELT.
     UNTIL ADDITIONAL CONSTRUCTION IS COMPLETED. TWO BOILERS ARE THE MAXIMUM THAT  CAN BE TIED INTO THE SCRUBBING SYSTEM.  TO DATE THE UTILITY
HAS ENCOUNTERED THE USUAL MINOR STARTUP PROBLEMS AND SOME MAJOR PROBLEMS AS WELL.   THE MAJOR PROBLEMS HAVE ENTAILED FROZEN PIPES AND THICKENERS. THE
LATTER INVOLVING HARDWARE AND DESIGN ASSOCIATED WITH RECIRCULATION OF THE SLUDGE WITHIN THE THICKENERS TO ATTAIN 30 TO 40 PERCENT SOLIDS CONCENTRATION.
     THE SLUDGE BEING GENERATED AT THIS STATION IS TREATED BY THE IUCS METHOD, WHICH  EMPLOYS A VACUUM FILTER THAT INCREASES THE SOLIDS IN THE UNDER-
FLOW TO 50 TO 60 PERCENT. SO THAT LESSER AMOUNTS OF DRY FLY ASH ARE REQUIRED FOR MIXING WITH THE  SLUDGE.
                                                                                                                               PEDCo- ENVIRONMENTAL
                                                                        52

-------
                                                           ELRAMA POWER STATION
                   Operating Hours
Period         Boiler            Scrubber Vessels
              12         1234
                                                             Garments
Oct. 75
  To
Jan. 76
Feb. 76

Mar. 76
Apr. 76
1169  1508   976   838
One boiler was connected to the scrubber system on October 26, 1975.  A second boiler
was connected on February 4, 1976.   Four of  the scrubber vessels have been In service
1n various combinations.  The service hours  to January 31, 1974 are posted 1n the
accompanying table.  The fifth vessel has not been In service because 1t Is being re-
vised for trial Installation of rubber-lined recycle pumps.
The system operated during the report period with 2 boilers coupled Into the scrubbing
system.  Revisions to the fifth scrubbing vessel have been completed and operations
are proceeding with two rubber-lined recycle pumps.
                                                                       53
                                                                                                                            PEDCo-ENVIRONMENIAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT HATING
   32


  DUQUESNE LIGHT

  PHILLIPS


  SOUTH  HEIGHT  PENNSYLVANIA

   410 MW
 FUEL CHARACTERISTICS  COAL    1.0-  2.6 PERCENT  SULFUR
 FGD VENDOR

 PROCESS


 NEW OR RETROFIT

 START UP  DATE

 FGO STATUS

 EFFICIENCY,
 PARTICULATES
  CHEMICO


  LIME SCRUBBING

  RETROFIT

  7/73


  OPERATIONAL
 S02
                      83 PERCENT FOR 2» SULFUR COAL
WATER MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND


S103/KW CAPITAL * 5 MILLS/KWHRANNUALIZED COSTS


 REFER TO BACKGROUND INFORMATION SECTION IN TABLE  3  OF  THIS  REPORT.   THIS
 FGO SYSTLM HAS OEEN OPERATIONAL SINCE JULY 1973.  THE UTILITY  REPORTS THAT
 A TOTAL OF H BOILERS (NOS.  3t<*.5,&  6) WERE COUPLED  INTO  THE SCRUBBING
 SYSTEM DURING THE REPORT PERIOD.  THE  SYSTEM IS  NOW  OPERATING  ON  HIGH
 CALCIUM LIME FOLLOWING THE  COMPLETION OF THE THIOSORBIC  LIME  TEST PRO-
 GRAM. THE SCRUBBING SYSTEM  AVAILABILITY DURING  THE  FIRST QUARTER OF  1976
 WAS 72 PERCENT.  THE SLUDGE  STABILIZATION PRACTICES  ARE STILL  CONTINUING
 AT THIS rACICZTY•
                                                                                                     PEOCo- ENVIRONMENTAL
                                                         54

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                           PHILLIPS POWER STATION

     THE PHILLIPS POWER STATION IS LOCATED ON THE OHIO RIVER ABOUT 20 MILES NORTHWEST OF PITTSBURGH.   THE  POWER STATION CONSISTS OF SIX COAL-FIRED
BOILERS HAVING A NET GENERATING CAPABILITY OF 307 MW.   THE RESULATANT FLUE GASES ARE DISCHARGED TO A  COMMON  HEADER, TO WHICH THE FGD MODULES ARE
CONNECTED THROUGH ISOLATION VALVES.  THE BOILERS ARE CURRENTLY BURNING COAL WITH A HEATING  VALUE OF 11,350 BTU PER POUND AND SULFUR AND ASH CONTENTS
OF 2.2 AND 18.2 PERCENT, RESPECTIVELY.
     THE FGD SYSTEM, WHICH SUPPLEMENTS THE EXISTING MECHANICAL AND ELECTROSTATIC DUST COLLECTORS, CONSISTS OF FOUR TRAINS OF WET VENTURI-TYPE SCRUBBERS,
INSTALLED AT A COST OF APPROXIMATELY $103/kW.  GIBBS & HILL, INC., WAS ENGAGED AS THE A-E FIRM FOR THE ENTIRE PROJECT; BATTERY LIMITS OF THE CHEMICO
CORPORATION ARE CONFINED TO THE SCRUBBERS AND ASSOCIATED PUMPS AND CONTROLS BETWEEN THE INLET HOT GAS DUCT MANIFOLD AND THE EXIT WET GAS HEADER (IN-
CLUDING THE REHEATER, EXCLUDING THE NEW ID FANS).
     THE FOUR TRAINS ARE LOCATED DOWNSTREAM Of EXISTING MECHANICAL COLLECTORS AND ESP'S INSTALLED IN  SERIES  ON EACH OF THE SIX PULVERIZED-COAL-FIRED
BOILERS.  THREE OF THE TRAINS ARE SINGLE-STAGE VENTURI SCRUBBERS ORIGINALLY INTENDED FOR PARTICULATE  REMOVAL.  THE FOURTH TRAIN IS A DUAL-STAGE VENTURI
SCRUBBER-ABSORBER AND IS THE PROTOTYPE FOR DETERMINING THE FEASIBILITY OF TWO-STAGE SCRUBBING FOR COMPLIANCE WITH S02 EMISSION LIMITS.
     EACH TRAIN IS EQUIPPED WITH A NEW WET-TYPE ID FAN.  A NEW COMMON DUCT DIRECTS GAS STREAMS FROM AIR BOILERS TO THE SCRUBBER SYSTEM, WHERE THEY CAN
BE SENT TO ANY OR ALL OF THE TRAINS.  THE SCRUBBED GAS IS EXHAUSTED THROUGH A COMMON DUCT AND AN OIL-FIRED REHEATER TO A NEW GROUND-SUPPORTED STACK,
WHICH CONTAINS AN INNER ACID-RESISTANT BRICK STACK.
     SLAKED QUICKLIME IS ADDED TO THE LOWER CONE OF EACH OF THE SCRUBBER VESSELS TO NEUTRALIZE THE RECIRCULATING LIQUOR, WHICH, IN SINGLE-STAGE SCRUB-
BING WITH HIGH-CALCIUM LIME, REACTS WITH APPROXIMATELY 50 PERCENT OF THE SOg IN THE FLUE GAS.   A LIQUOR BLEED FLOW OF APPROXIMATELY 4 PERCENT IS SENT
TO ONE OR BOTH OF THE THICKENERS FOR REMOVAL OF SOLIDS.  THE OVERFLOW IS RETURNED TO THE SYSTEM, AND  THE UNDERFLOW IS PIPED TO THE SLUDGE TREATMENT
SYSTEM.  THE UNDERFLOW IS STABILIZED BY THE ADDITION OF 200 POUNDS OF CALCILOX PER TON OF DRY  SOLIDS  IN THE  SLUDGE.  THE FIXED SLUDGE IS TRANSPORTED
TO EXPERIMENTAL PLASTIC-LINED PONDS LOCATED ABOUT ONE MILE FROM THE STATION, WHERE THE MATERIAL SOLIDIFIES.
     FLUE GASES FROM THE BOILERS ARE ACCELERATED TO A HIGH VELOCITY IN THE SCRUBBER.   AT THE  THROAT.  THE GASES COLLIDE WITH THE SCRUBBING LIQUID,
ATOMIZING IT INTO SMALL DROPLETS.  THE FLY ASH AND THE SULFUR DIOXIDE IN THE GAS ARE PICKED UP BY THE SLURRY DROPLETS AND EXIT AT THE BASE OF THE
TOWER.  THE GAS THEN REVERSES DIRECTION ADN FLOWS UP THROUGH THE MIST ELIMINATOR. WHERE FINE  DROPLETS ARE  REMOVED BEFORE THE GAS LEAVES THE
SCRUBBER.
                                                                                                                              PEDCo-ENVIRONMENTAL
                                                                        55

-------
PHILLIPS POWER STATION (continued)
     STARTUP OF A PORTION OF THE PHILLIPS SCRUBBER SYSTEM BEGAN JULY 1973.  SEVERAL PROBLEMS THEN DEVELOPED IN THE FORM OF EROSION OF  FANS AND THE LIME
FEED SYSTEM. CAUSING OUTAGES OF THE SCRUBBER SYSTEM.  AFTER AN EXTENDED OUTAGE, THE SCRUBBER SYSTEM WAS RETURNED TO SERVICE IN MARCH 1974.  THE SYSTEM
HAS BEEN OPERATING CONTINUOUSLY SINCE THAT TIME  WITH VARIOUS NUMBERS OF BOILERS CONNECTED TO THE SCRUBBER SYSTEM AND SCRUBBER TRAINS IN  SERVICE.
     DETERMINATION OF THE AVAILABILITY OF THE PHILLIPS  SYSTEM HAS BEEN DIFFICULT.  UNTIL ALL BOILERS WERE CONNECTED TO THE SCRUBBERS,  THERE WAS AT
LEAST ONE SPARE TRAIN AND AS MUCH AS 100 PERCENT SPARE  SCRUBBER CAPACITY.  THEREFORE. HAVING A TRAIN OUT OF SERVICE FOR MAINTENANCE DID  NOT REDUCE THE
CAPABILITY OF THE SCRUBBER SYSTEM.   UNTIL ALL SIX BOILERS WERE CONNECTED, MEANINGFUL AVAILABILITY FACTORS COULD NOT BE COMPUTED.   ON MARCH 17. 1975, THE
SIXTH BOILER WAS CONNECTED, AND ALL FOUR SCRUBBER TRAINS WERE REQUIRED TO BE  IN SERVICE.  OPERATION IN THAT MODE CONTINUED UNTIL  AUGUST  4, 1975.  WHEN
THE NO. 6 BOILER WAS REMOVED FROM THE SCRUBBER SYSTEM BECAUSE THE pH LEVEL COULD NOT BE MAINTAINED AND DEPOSITS BECAME UNMANAGEABLE TO THE POINT  THAT
SCRUBBER OUTAGES WERE REDUCING GENERATING CAPABILITY OF THE STATION.
                                                                                                                           PEDCo-ENVIRONMENTAL
                                                                       56

-------
                                                           PHILLIPS POWER STATION

                         Operating Hours
                    Boiler                         Scrubber-Absorber
Month     1234      5      6      101    201    301     401                                Comments
                                                                                Fourth FGD train and  sixth  boiler were  tied  In on March 17. 1975.  Par-
                                                                                tlculate tests  In May showed outlet  loadings of 0.04 Ib/mllllon Btu.
Jul. 75   83    644  703   349    605    643     400    180    537     723       The two-stage train has  been out of  service  from June 19 for general
                                                                                cleaning and  repair of a leak  In the first-stage scrubber.
Aug. 75  354    701  454   457    517    445     478    682    323     319       Scrubber unavailability  forced returning Boiler No. 6 to the scrubber
                                                                                bypass gas path to prevent  loss of boiler capacity.  Plugging and
                                                                                maintenance problems  have been encountered.  Evaluation of various
                                                                                recycle pumps 1s continuing.
Sep. 75  463    287  669   503    672    525      57    561    685     536       In October 1975, Phillips Initiated  thlosorblc lime scrubbing In their
Oct. 75  547    575  620   604    681    687     607    207    505     487       single-stage  modules  on  an  experimental basis.  The purpose Is to study
                                                                                compliance feasibility.   S02 removal efficiency, and quality of the  •
                                                                                sludge generated by the  single-stage modules.
Nov. 75   16    720  688    70    720    593     626    720      0      75       The utility concluded the thlosorblc lime testing program In mid-
Dec. 75  172    660  709     0    689    547     360    661    182     386       December.   Four boilers  were coupled to the scrubbing system during the
                                                                                run.   The utility 1s  now analyzing the data generated during the test
                                                                                program.   The scrubbers  have been put back on regular lime.  No unusual
                                                                                problems were encountered during the test run.
Jan. 76  222    722  639     0    662    661     277    536    101     707       The 2.5-month test program  with thlosorblc lime Included 1612 service
                                                                                hours  on one  train and 1309 hours on another train.  Results Indicate
                                                                                that the required degree of S02 removal (83 percent) can be obtained
                                                                                with an MgO content of 8-10 percent  In the lime with single-stage
                                                                                scrubbing.

                                                                                                                               PEOCo-ENVIRONMENTAL
                                                                         57

-------
                                                     PHILLIPS  POWER STATION (Continued)
Month
1
         Operating Hours
    Boiler
2345      6
  Scrubber-Absorber
101    201    301    401
Feb. 76  445
Mar. 76
      588  672
                  633    571
657
695
662
353
                                                    166
                                                    659
406
461
                         Comments

Plant operation 1s proceeding with a total  of 4 boilers  coupled  Into  the
scrubbing system (equaling 336 MM, which 1s 87 percent of the  total
plant capacity).  The FGO system operated on high calcium lime during
the report period.  The general operation mode at this facility  has one
of the four scrubbing trains out continually for repairs,  cleaning, and
preventatlve maintenance.   The utility 1s still  experiencing problems
with solids deposition In the venturl  throat of the scrubbing module,
causing movement Inhibition and greater pressure drops.  The FGD
system availability for the first quarter of 1976 was  72 percent.  The
sludge stabilization practices are still  continuing at this facility.
                                                                       58
                                                                                                                            PEDCo-ENVIRONMcrtfAL

-------
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  05/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCY,
  PARTICULATES

  S02

 WATER MAKE UP

 SLUDGE DISPOSAL

 UNIT COST
 OPERATIONAL
  EXPERIENCE
  33
 GENERAL  MOTORS
 CHEVROLET  PARMA  1  2  3  *  »
 PARMA OHIO
   32 MW
 COAL  2.5 PERCENT SULFUR
 KOCH
 DOUBLE ALKALI
 RETROFIT
  3/7H
 OPERATIONAL

 80 PERCENT

 90 PERCENT

 CLOSED LOOP

 UNSTABILIZED SLUUGE  DISPOSED IN UNLINEO POND

S3.2 MILLION CAPITAL  *  ftll.70 PER TON OF COAL ANNUALIZEO

 REFER TO BACKGROUND  INFORMATION SECTION IN TA?LE 3 OF THIS REPORT.  THIS
 FGO SYSTEM HAS BEEN  OPERATIONAL SINCE MARCH 1971. SYSTEM OPERABILITY
 DURING THE MONTHS OF MARCH AND APRIL WAS 17 AND 76 PERCENT RESPECTIVELY.
 SYSTEM OPERABILITY AVERAGED IN EXCESS OF 56 PERCENT DURING THE LAST EIGHT
 MONTHS.  CURRENTLY! A SCRUBBING SYSTEM CHARACTERIZATION STUDY.  SPONSORED
 BY THE EPA* IS BCING CONDUCTED BY A.D. LITTLE.
                                                         59
                                                                                                        PEDCO-ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                       THE CHEVROLET PARMA STEAM PLANT

     THE CHEVROLET PARMA PLANT OF GENERAL MOTORS IS LOCATED NEAR CLEVELAND. OHIO.  THE PLANT HAS FOUR SPREADER-STOKER BOILERS FIRED BY TRAVELING GRATES
AND PRODUCES A TOTAL RATED CAPACITY OF 32 MW.  THE BOILERS ARE RETROFITTED WITH A SOLUBLE ALKALI FGD SYSTEM.   THE COAL BEING BURNED AT THE  PLANT CONTAINS
ABOUT 2.5 PERCENT SULFUR.
     THE FGD SYSTEM SCRUBBING MODULES WERE SUPPLIED BY KOCK ENGINEERING.   INSTALLATION WAS COMPLETED ON FEBRUARY 28,  1974.   THE  SYSTEM CONSISTS  OF  FOUR
SCRUBBERS OPERATING IN PARALLEL.  EACH SCRUBBER IS MADE OF THREE BUBBLE-CAP ABSORPTION TRAYS AND A MESH MIST  ELIMINATOR.
     THE S02 CONTAINED IN THE FLUE GAS IS ABSORBED BY A REGENERATED CAUSTIC SOLUTION (0.1  MOLAR NAOH),  FORMING SOLUBLE SODIUM SALTS.   THE SPENT  CAUSTIC
IS THEN REGENERATED BY REACTING THE SOLUTION WITH SLAKED LIME, RESULTING  IN THE FORMATION OF CALCIUM SULFITE  AND SULFATE  SOLIDS, WHICH ARE  SEPARATED
OUT OF THE SOLUTION.  NEXT, SODA ASH IS ADDED TO THE SOLUTION IN ORDER TO MAKE UP FOR SODIUM LOSSES AND MINIMIZE THE  SCALE  POTENTIAL  FROM THE CALCIUM
WHICH REMAINS IN SOLUTION.  THE REGENERATED CAUSTIC FORMED IS THEN RECYCLED BACK TO THE SCRUBBER FOR ADDITIONAL S0? REMOVAL,  THE SLUDGE WHICH RESULTS
IS DEWATERED AND HAULED AWAY BY TRUCK TO AN OFF-SITE LANDFILL.
PROBLEMS AND SOLUTIONS
     THE SYSTEM WAS STARTED UP ON FEBRUARY 28, 1974 AND BY APRIL 31  IT HAD OPERATED FOR 624 HOURS.   THERE WERE TWO SCHEDULED  SHUTDOWNS DURING THIS
PERIOD FOR EQUIPMENT INSPECTION.  THE SECOND SHUTDOWN REVEALED THAT SOLIDS WERE NOT BEING DISCHARGED FROM THE PRIMARY  CLARIFIER RAPIDLY ENOUGH.  AS A
RESULT, THE CLARIFIER RAKE JAMMED.  A PIPING CHANGE WAS MADE TO BLEND THE CAUSTIC FEED IN WITH  THE  RECYCLE  LIQUOR.  THIS  HAS  IMPROVED  PERFORMANCE BUT
NOT COMPLETELY ELIMINATED THE PROBLEM.   PREMATURE CAKE CRACKING IN THE VACUUM FILTERS REQUIRED  THE  PRESENCE OF AN OPERATOR  DURING OPERATION.  G.M.
ANTICIPATES THAT THE CHANGE TO NYLON FROM POLYPROPYLENE WILL SOLVE THIS PROBLEM.
     CAKE WASHING TO REDUCE SODIUM LOSSES WAS NOT INITIALLY SUCCESSFUL BECAUSE THE SPRAY WATER  TENDED TO KNOCK THE CAKE OFF THE DRUM.   ALTERATIONS
IN SPRAY PATTERN AND OTHER MEASURES HAVE APPARENTLY SOLVED THIS PROBLEM.   THERE HAS BEEN NO EVIDENCE OF  CORROSION OR ABRASION  IN THE PUMPS OR PIPING.
     THE SYSTEM WAS SHUT DOWN FROM MAY 1  TO MAY 28, 1974,  BECAUSE OF UNEXPECTED BUILDUP OF SOLIDS  IN THE CLARIFIER, WITH  SUBSEQUENT OVERFLOW INTO
THE SCRUBBER.  THE PROBLEM WAS SOLVED BY 1) USING A POLYMERIC FLOCCULATION AGENT TO ATTAIN BETTER SETTLING  AND 2) WITHDRAWING SLUDGE FROM THE CLARIFIER
                                                                                                                               PEDCo-ENVIRONMENTAL
                                                                       60

-------
CHEVROLET PARMA (continued)
AT MORE FREQUENT INTERVALS.   SYSTEM AVAILABILITY TO THE BOILER WAS 87  PERCENT  IN APRIL 1974. LESS THAN 10 PERCENT IN MAY. AND 100 PERCENT IN JUNE.

JULY, AND AUGUST AFTER THE SYSTEM VMS RESTARTED.  PLUGGING BY CaC03 DEPOSITS IN THE OVERFLOW LINE BETWEEN THE CLARIFIERS AND IN THE LINE FROM

CLARIFIER NO. 2 TO THE NIX TANKS WAS CORRECTED BY RELOCATING A CHEMICAL FEED LINE AND REPLACING SOME PIPING.  THE SYSTEM WAS DOWN THROUGHOUT JULY AND

AUGUST FOR REPLACEMENT OF GRAVITY FLOW LINES WITH AN OPEN FLUME THAT CAN BE EASILY CLEANED.
                                                                                                                            PEDCo-ENVIRONNtwTAl
                                                                      61

-------
                                                              CHEVROLET PARMA
                      Operating  Hours
              Boiler
Month.     12341
Jun. 75
Jul. 75
Aug. 75
Sep. 75
Oct. 75
Nov. 75
Dec. 75
2331*
    2135
                        FGD system
                          2      3
                                       0 **  0
                                 0
                                 0
         1848*
1250
                   0
                   0
                               Qperabmty (X)
                         1234
0
0
                                             59
0
0

79
0
0
0
0
               Comments
Recent operation has been Intermittent.  Tests have been
conducted for analysis of partlculate  loading at  the boiler
outlet.  The system was  restarted  In May but was  shut down
because of a plugged chemical  feed line to  clarlfler.  After
restart about June 10, the system  was  shut  down because of
similar plugging In another part of the line.  Unit ran for
about 2 weeks 1n June.
FGD system was down 1n July and August for  replacement of
gravity flow lines with  an open flume.
FGD system restarted September 8,  and  operated during this
period at an availability factor of 80 percent.
The FGD system operated  during the report period  except
for a scheduled holiday  shutdown from  December 23 to
January 4, 1976.  Because of problems  with  solids and solids
carryover, G.M. conducted stream tests during December to
determine whether the sol Ids carryover is due to  a high
solids reclrculation rate.  The FGD system  was down most of
December because of these tests, which caused the low
operabillty factor.
* Note:  The figures given for September  and October represent
  the operation hours from September 8 to November 9 Inclusive.
                                                                                                                        PEDCo- ENVIRONMENTAL
                                                                     62

-------
                                                             CHEVROLET PARMA (continued)
               Operation hours
          Boiler                   FD6 system
Month   1234123
Jan. 76
Feb. 76           2997        1196
Mar. 76
1379
                               240
                                           Qperab1l1ty (X)
                               41234

                                    40

                                    17
Apr.
1084
                               847
                                     78
              Conments
G.M. has found solids concentration  1n  the clarlfler too high
for efficient system operation.  A.D. Little 1s scheduled to
conduct tests on the system 1n April as part of an EPA evaluation.
The low system operabillty during  the month of March resulted from
extensive modifications performed  on the  system by G.M.  During this
period the scrubber blowdown and scrubber flow Indication system was
revised.
From April 19 to the end of the month the system was operable 100X.
During this period all system modifications were completed and all
major problem areas corrected.
                                                                       63
                                                                                                                              PEOCo- ENVIRONMENTAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT.LOCATION

 UNIT RATING
 GULF POWER CO.

 SCHOLZ NO. 1A

 CHATTAHOOCHEE  FLORIDA

   20 MW
 FUEL  CHARACTERISTICS  COAL    3.0  PERCENT  SULFUR
 FGO  VENDOR
 PROCESS
 NEW  OR RETROFIT
 START UP  DATE
 FGD  STATUS
 EFFICIENCY,
 PARTICULATES
 ADL/COHBUSTXON EQUIP  ASSOCIATE

 DOUBLE  ALKALI

 RETROFIT

 2/75

 OPERATIONAL


 99.7 PERCENT
 S02


WATER HAKE UP
95 PERCENT
                      CLOSED LOOP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
UNSTABILIZED SLUDGE DISPOSED IN LINED POND
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
FGD SYSTEM HAS BEEN OPERATIONAL SINCE FEB. 1975. THE PROTOTYPE SYSTEM
OPERATED A TOTAL OF H7HH HRS. DURING 1975. TRANSLATING INTO AN ANNUAL
AVERAGE OPEHABILITY OF 39 PERCENT. THE SYSTEM WAS PUT BACK IN SERVICE
MARCH 12, 1976, FOLLOWING A SCHEDULED BOILER OVERHAUL. SYSTEM OPERABILITY
WAS 9<» PERCENT FOR THE DURATION OF THE MONTH.
                                                          64
                                                                                PEOCo- ENVIRONMENTAL

-------
                                                           BACKGROUND  INFORMATION
                                                                    ON
                                                        SCHOLZ NO.  1A  -  DOUBLE ALKALI

     THE SCHOLZ STEAM POWER PLANT OF GULF POWER COMPANY IS LOCATED  IN  CHATTAHOOCHEE, FLORIDA.  UNIT NO. 1 IS A COAL-FIRED BOILER DESIGNED FOR NOMINAL
LOAD OPERATIONS OF 40 MW AND PEAK CAPACITY OPERATION OF 47.5 MW.  THIS UNIT WAS  SCHEDULED TO BURN VARIOUS TEST COALS WITH AN AVERAGE HEATING VALUE OF
12,400 BTU/LB, 14 PERCENT ASH, AND SULFUR CONTENTS RANGING AS HIGH  AS  5  PERCENT.
     A 20 MW PROTOTYPE DUAL ALKALI SYSTEM WAS JOINTLY DEVELOPED,  DESIGNED, AND INSTALLED. BY COMBUSTION EQUIPMENT ASSOCIATES AND ARUTHRU D. LITTLE.  THE
PROTOTYPE SYSTEM AT THE SCHOLZ STEAM PLANT IS INSTALLED ON BOILER NO.  1,  A BABCOCK  ft UILCOX PULVERIZED-COAL-FIRED BOILER.  THE SYSTEM IS DESIGNED TO
HANDLE 50 PERCENT OF THE FLUE GAS FROM THE BOILER.  THE BOILER HAS  BEEN  RETROFITTED WITH A SECTIONALIZED, HIGH-EFFICIENCY ESP CAPABLE OF 99.7 PERCENT
PARTICULATE REMOVAL.  THE ESP CAN BE SELECTIVELY DE-ENERGIZED FOR STUDY  OF PARTICULATE  IMPACT ON THE FGD OPERATION.
     THE PROTOTYPE UNIT INCORPORATES A HIGH DEGREE OF FLEXIBILITY FOR  GENERATION OF DESIGN AND OPERATING INFORMATION FOR A WIDE VARIETY OF APPLICATIONS.
ALTHOUGH THE BASIC MODE OF SYSTEM OPERATION IS DUAL ALKALI WITH LIME REGENERATION,  THE  SYSTEM WAS DESIGNED TO ACCOMMODATE LIMESTONE REGENERATION
AND LIME/LIMESTONE REGENERATION.
     THE SYSTEM CONSISTS OF A VENTURI SCRUBBER AND AN ABSORPTION TOWER,  WITH  AN  ADDITIONAL STORAGE SILO FOR LIMESTONE. A MIX TANK. AND OTHER ASSORTED
TANKS. PUMPS. CONTROLLERS, AND PIPING.
     THE PROTOTYPE SYSTEM WAS COMPLETED AND PUT IN OPERATION BY CEA/ADL  IN EARLY FEBRUARY 1975.  IN MID-MAY AN EPA DUAL ALKALI TEST PROGRAM WAS
INITIATED BY SOUTHERN SERVICES, CEA. AND ADL.  THE SYSTEM WAS OPERATIONAL THROUGH EARLY JANUARY 1976. WHEN THE BOILER WAS SHUT DOWN FOR A SCHEDULED
OVERHAUL.  THE BOILER AND PROTOTYPE SYSTEM ARE SCHEDULED TO BE BACK IN SERVICE IN EARLY MARCH 1976.
                                                                                                                              PEDCo-ENVIRONMENTAL
                                                                        65

-------
                                                              SCHOLZ 1A - DOUBLE ALKALI
  Period
Feb. 75
  to
Jul. 75
Jul. 75
  to
Sep. 75

Sep. 75
Oct. 75
 Nov. 75
 Dec. 75
   Operating hours
BoilerFGD system
                2,600
                                                     FGD system
                                                    OperablHty (X)
                   83
                                     44
                                    100
 620
 732
560
732
 90
100
                                        Comments
                     Unit was placed  1n operation Feburary 8, 1975, and operated until July 18
                     when It was  shut down for 2 months modifications, repairs, and replacement
                     of parts.  The system was unavailable to the boiler for a 491-hour period
                     because of adjustments  and modifications required for the formal EPA test
                     program In mid-May.
                     The system was shut  down from  mid-July  to mid-September for mechanical
                     overhaul  Involving replacement parts for valves  that had failed.
The system was put back 1n operation  on  September 16, 1975.  From mid-
September to mid-October the air preheater was repaired and boiler op-
eration adjusted to reduce oxygen levels 1n  the  flue gas to the 5 to 6
percent range.  The system operated approximately 800 hours during this
period.
The system ran continuously for the remainder of the test  period through
January 2, 1976.  S02 levels during this period  ranged  from 800 to 1700
ppm.  The system operated in the concentrated mode  throughout  the
remainder of  the test period.  In the period from mid-September to
January 2, 1976, the system operated about 2100 hours,  with an
operability factor of 97 percent.
                                                                                                                             PEDCo-ENVIRONMENTAL
                                                                       66

-------
                                                        SCHOLZ 1A - DOUBLE ALKALI  (continued)
  Period
Jan. 76
Feb. 76
    Operating hours
Boiler        F6D system
                                                      FGD system
                                                    Qperabmty (I)
Mar. 76
                                         445
                    Comments
The FGD system and boiler underwent a  scheduled overhaul during the
report period.  System restart Is  scheduled for mid-March 1976, to con-
tinue till June.  During this operating period high-sulfur coal (3.5-4.0
percent) will be burned to allow evaluation of system performance on
high-sulfur coal.
The system was put back 1n service on  March 12, 1976.  The total number
of operating hours for the month of March was 445 hours.  This
translates Into a 94* operablllty  factor  since the March 12 restart.
                                                                         67
                                                                                                                      PEDCo- ENVIRONMENTAL

-------
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  OS/76
IDENTIFICATION NO.

UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY,
 PARTICULATES


 S02


WATER MAKE UP
                        35

                       GULF POWER CO.

                       SCHOLZ NO. 2A

                       CHATTAHOOCHEE  FLORIDA

                         20 MW

                       COAL   3.0 PERCENT SULFUR

                       FOSTER WHEELER

                       ACTIVATED CARBON

                       RETROFIT

                        2/76

                       OPERATIONAL


                       99.7 PERCENT


                       71.5 PERCENT  (DESIGN)


                       N/A   DRY ADSORPTION SYSTEM
 SLUDGE DISPOSAL
 UNIT COST
OPERATIONAL
 EXPERIENCE
                       REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THE
                       SYSUM SUPPLIFR AND TEST DIRECTOR (SOUTHERN SERVICES) REPORTED THREE
                       OPERATIONAL RUNS DURING THE REPORT PERIOD. PERFORMANCE OF THE FRONT-END
                       OF THE SYSTEM  (ADSORPTION AND REGENERATION) WAS CONSIDERED ADEQUATE. THE
                       RESOX SECTION  OPERATED INTERMITTENTLY DURING THE REPORT PERIOD BECAUSE OF
                       PLUGGING PROBLEMS IN THE SULFUR CONDENSER. TO DATE. THE SYSTEM S02
                       REMOVAL EFFICIENCY HAS EXCEEDED THE NOMINAL DESIGN VALUE (96 PERCENT).
                                                             68
                                                                                                    PEDCo- ENVIRONMENTAL

-------
                                                                BACKGROUND INFORMATION
                                                                          ON
                                                              SCHOLZ NO.  2A -  FWBF SYSTEM
     IN JANUARY 1973, THE SOUTHERN SERVICES COMPANY OF GULF POWER AWARDED A CONTRACT TO THE FOSTER WHEELER CORPORATION TO BUILD A 20 MW PROTOTYPE DRY
ADSORPTION SYSTEM FOR FLUE GAS DESULFURIZATION.  CONSTRUCTION ON THE FOSTER WHEELER PROCESS STARTED FEBRUARY  15,  1974, AT THE SCHOLZ STEAM POWER
PLANT IN CHATTACHOOCHEE, FLA.  CONSTRUCTION WAS COMPLETED AND A TESTING PROGRAM WAS INITIATED IN MAY 1975.
     THE SYSTEM AT THE SCHOLZ PLANT CONSISTS OF A 20-MW ADSORBER SECTION AND A 47.5-MW REGENERATION AND REDUCTION SECTION.  THE 20 MW ADSORBER IS
DEISGNED TO ACCEPT HALF OF THE MAXiMUM FLUE GAS FLOW FROM UNIT NO. 2.  THE COAL-FIRED BOILER IS RATED AT 40 MW (NOMINAL); IT FIRES COAL WITH A HEATING
VALUE OF 12,400 BTU/LB, ASH CONTENT IS 14 PERCENT, AND SULFUR CONTENT RANGING AS HIGH AS 5 PERCENT.
     THE PURPOSE OF THE ADSORPTION SECTION IS TO REMOVE SOg, NOX> AND PARTICULATE FROM THE FLUE GAS WITH ACTIVATED CHAR, CONVERTING THE CAPTURED
POLLUTANTS TO SULFURIC ACID.  THE REGENERATION SECTION PROVIDES CONTINUOUS ON-SITE REGENERATION OF THE CHAR,  WHICH HAS BEEN LOADED WITH SOg  IN THE  FORM
OF H2S04.  THE CHAR  IS REGENERATED AND A LOW-VOLUME, 50,,-RICH OFF-GAS STREAM IS FED FORWARD TO THE RESOX REACTOR, WHICH REDUCES THE SO., STREAM TO GASEOUS
ELEMENTAL- SULFUR THAT IS COLLECTED AND STORED  IN AN INSULATED TANK.
     THE DEMONSTRATION UNIT HAS TWO ROWS OF MODULES, EACH ROW CONSISTING OF SIX MODULES.  THE ADSORPTION SECTION IS A TWO-STAGE DESIGN CONSISTING
OF VERTICAL COLUMNS  OF PARALLEL LOUVER BEDS, WHICH SUPPORT AND CONTAIN THE ACTIVATED CHARCOAL.  S02 DIOXIDE,  OXYGEN, WATER  VAPOR, AND NOX ARE AD-
SORBED BY THE CHAR PELLETS FROM THE CROSS-FLOWING FLUE GAS AT 250 TO 300°F.  THE S02 THEN REACTS WTIH 02 AND H20 TO FORM  H2S04, WHICH IS  FIRMLY  •
RETAINED IN THE  INTERIOR PORE SYSTEM OF THE CHAR PELLETS.  THE CHAR  IS THEN REGENERATED IN THE REGENERATOR VESSEL BY HEATING TO 1200°F, DRIVING OFF
THE  ENTRAINED GASES, AND REDUCING SULFURIC ACID TO SO.,.  THE 50.,-RICH GAS  IS THEN PASSED THROUGH A VESSEL CONTAINING CRUSHED COAL,  RESULTING IN
REDUCTION TO GASEOUS ELEMENTAL SULFUR AND CARBON DIOXIDE.  THIS LATTER PROCESS IS CARRIED OUT AT 1200° TO 1500°F.
     THE INITIAL SHAKEDOWN ON FLUE GAS BEGAN AUGUST 11,  1975. AND PROCEEDED CONTINUOUSLY FOR 10 DAYS.  THE REGENERATION  SECTION WAS OPERATIONAL ABOUT
60 PERCENT OF THE TIME.  HOWEVER, THE. REDUCTION SECTION  HAS NOT YET  BEEN  INTEGRATED  INTO SYSTEM OPERATION.  S02 REMOVAL  WAS WELL  ABOVE  EXPECTATIONS
AND  PRESSURE DROP ACROSS THE ADSORBER WAS WELL BELOW  DESIGN LEVELS.  THE  SYSTEM WAS  SHUT DOWN FOR CORRECTION OF SEVERAL  OPERATING PROBLEMS,  EQUIPMENT
MODIFICATIONS, AND  EVALUATION OF  THE INTIAL OPERATING DATA.  OPERATION WAS RESUMED  IN  OCTOBER 1975, WHEN  TWO CONSECUTIVE RUNS  WERE  CONDUCTED WITH THE
REDUCTION  PORTION OF THE  SYSTEM PROCESSING FRONT-END  OFF-GAS AT FULL OPERATING TEMPERATURES.  A PROGRAM OF MODIFICATION WAS COMPLETED ON THIS SYSTEM
 IN  EARLY JANUARY 1976.  REPRODUCTION OF  FLUE GAS INTO  THE  INTEGRATED SYSTEM COMMENCED IN  FEBRUARY 1976.  THE SYSTEM IS CURRENTLY OPERATING THROUGH
4-MONTH TEST PROGRAM SPONSORED BY SOUTHERN SERVICES AND  FOSTER WHEELER.
                                                                                                                               PEDCo-ENVIRONMhNTAL

                                                                       69

-------
                          FKBF SYSTEM OPERATING HISTORY
                                                    t

Period                                               .          Comments
May 75                             Completion of .construction was  followed  by a  3-month commissioning period which
Jun. 75                            various pieces  of equipment  were operated Individually and then  1n combinations to
Jul. 75                            simulate subsystem operation.   Subsystem operations were  Integrated Into section
Aug. 75                            operations and  flue gas  was  passed  through the adsorber and regenerator for a 10-day
Sep. 75                            period beginning August.11.  RESOX  construction was Incomplete at this time.
Oct. 75                            Two consecutive runs were conducted on the RESOX portion  of the  system on front-end
                                   process off-gas at full  operating temperatures.  This operational period lasted 5
                                   days.
Nov. 5                             A program of modifications on the system began in  late August 1975 and continued
Dec. 75                            through January 1976, with the  exception of the 5-day RESOX operation In October.
Jan. 76                            Modifications were completed and pre-startup  testing was  conducted in late January
                                   and early February.   A 3-day continuous  dry run was successfully completed.
Feb. 76                            All materials-handling loops and RESOX loops  were  operated at full operating
                                   temperatures and pressures.  Reproduction of flue gas Into the system commenced,
                                   and a  4-month formal test program conducted by Southern Services and Foster Wheeler
                                   Is now In progress.
Nar. 76                            Three  operational  periods were  logged by the  prototype system during the report
Apr. 76                            months.  During these runs the  adsorption and regeneration sections performed
                                   adequately.  The RESOX section  operated  Intermittently because of plugging problems
                                   In the sulfur condenser. Also, the front end of the system was  taken down at one
                                   point  due to frequent high temperature excursions.  This  problem was corrected by
                                   modifying system operating procedures.   Currently, work 1s proceeding on the
                                   solution of the sulfur condenser problem.

                                                                                                 PEDCo-ENVIRONMENTAL

                                          70

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES


  S02
 36

GULF POWER CO.

SCHOLZ NOS. IB « 2B

CHATTAHOOCHEE FLORIDA

  23 MW

COAL 5.0 PERCENT SULFUR (HAX)

CHIYODA INTERNATIONAL

THOROUGHBRED 101

RETROFIT

 3/75

OPERATIONAL
           •»«

99.7 PERCENT


90 PERCENT
 WATER HAKE UP
 SLUDGE DISPOSAL
UNSTABILIZED SLUUGE DISPOSED IN DRY GYPSUM POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF REPORT.  THIS FGD
SYSTEM HAS BEEN OPERATIONAL SINCE MARCH 1975. THE TOTAL SYSTEM OPERABILI-
TY. INCLUDING SYSTEM COMMISSIONlNGi  EXTENDING FROM FEB. ll,1975i  TO
DECEMBER 31«1975. WAS 60 PERCENT. SYSTEM OPERA8ILITY FOR THE MONTHS OF
MARCH AND APRIL WAS 100 AND 1* PERCENT RESPECTIVELY. THE SYSTEM WAS TAKEN
OUT OF SERVICE ON APRIL 5 FOR A SCHEDULED SYSTEM'S DESIGN MODIFICATION.
                                                                                                     PEDCO- ENVIRONMENTAL
                                                         71

-------
                                                           BACKGROUND  INFORMATION
                                                                    ON
                                                       SCHOLZ  UNITS  1  AND 2 - CHIYODA

   .  THE SCHOLZ POWER PLANT IS LOCATED IN CHATTAHOOCHEE,  FLORIDA, ABOUT  50 MILES WEST OF TALLAHASSEE.  THE FGD SYSTEM WAS DESIGNED BY CHIYODA
INTERNATIONAL CORP. FOR TESTING AND PROCESS DEMONSTRATION ON A COAL-FIRED BOILER.  THE PROCESS IS USED IN JAPAN ONLY ON OIL-FIRED AND GAS-FIRED BOILERS.
AND TAIL GAS FROM CLAUS UNITS.
     THE SYSTEM AT SCHOLZ CAN HANDLE ONE-HALF THE LOAD (53,000 SCFM) FROM EITHER OF THE 47 MW BOILERS.  DESIGN ABSORBER INLET SOg CONCENTRATION IS
2250 PPM.  VARIOUS TEST COALS WITH SULFUR CONTENTS RANGING UP  TO 5 PERCENT ARE SCHEDULED FOR BURNING.
     THE PARTICULATE LOADS FROM NEWLY INSTALLED ELECTROSTATIC  PRECIPITATORS ON THE TWO UNITS RANGE FROM 0.02 TO 0.1 GR/SCF.  FLUE GAS FROM THE PRE-
CIPITATORS IS QUENCHED WITH COOLING WATER TO REMOVE ADDITIONAL FLY ASH AND TO COOL THE GAS BEFORE IT ENTERS THE S02 ABSORBER.
     S02 IS ABSORBED IN WATER AND CATALYTICALLY OXIDIZED WITH  AIR TO FORM SULFURIC ACID.  THE DILUTE ACID IS RECIRCULATED THROUGH THE ABSORBER.  A
PORTION OF THE ACID IS NEUTRALIZED WITH LIMESTONE TO PRODUCE GYPSUM  AS A BY-PRODUCT.
     BREAK-IN TESTS WERE INITIATED IN FEBRUARY 1975.  THE FIRST FEW  MONTHS SHAKEDOWN PERIOD WAS CHARACTERIZED BY MANY SMALL PROBLEMS RESULTING IN A
LOW OPERABILITY (3W FEBRUARY-MAY).  MANY OF THESE PROBLEMS WERE RESOLVED BY JUNE, AND OPERABILITY DURING JUNE AND JULY WAS SOMEWHAT IMPROVED (84X).
A SIX-WEEK OUTAGE STARTING IN AUGUST WAS THE RESULT OF UNBALANCING OF  THE GYPSUM CENTRIFUGES.  AFTER REPAIR OF THE CENTRIFUGES AND INSTALLATION ON
SEPTEMBER 15, THE OPERABILITY THROUGH DECEMBER. 1975 AVERAGED  ABOVE  97X.
                                                                                                                             PEDCo-ENVIRONMENTAL
                                                                   72

-------
          SCHLOZ IB AND 2B - CHIYOOA
               Boiler
Operating hours
                           ing
                            FG
         D system
  FGD system
OperaHlitv
     75
Jul. 75
Aug. 75
Sep* 75
Oct> 75

N°V' 75
De°' 75

Ja"' 76
Feb' ?6
Mar. 76
Apr< 76
                              45°
                             741
                              10°
                                0

                               45
                              100

                              10°
                               98

                               66
                               n
                              100
                               14
                                                Comments
                       This Is a pilot plant  size demonstration unit.  Engineering design began
                       September 1973.   Startup  occurred  In March 1975.  After Initial operation for
                       break-In tests,  unit will be shut  down for Internal Inspection.  Reliability. tests
                       will  then follow, starting July 1975.  Chemical performance was satisfactory.
                       Emission tests  have not been performed.  Some pump and Instrument failures have
                       occurred.
                       Unit  has been out of service for minor repairs throughout July.
                           operated at a 95 percent S02 removal efficiency during this period.
                      Gulf Power is attempting to upgrade this value to a higher efficiency  level.
                      Waste water discharge from this unit still a problem area.
                      Outage time was less than one hour during November operation due to a  broken
                      flue gas blower Inlet vane and repair of a pinhole In the  prescrubber  FRP
                      lining.
                      Scrubber outages during December resulted from continuing  repairs to a pinhole
                      in the prescrubber FRP lining.
                      Outage time 1n January-February was  primarily  for repair and modification of
                      the suction and discharge piping on  the  absorbent circulation pumps.  These FRP
                      lines broke in January at some  weak  field Joints.  S02 removal efficiency has been
                      as high as  95%.

                      ""it was stopped  April  5 for a  scheduled shut down to allow installation and
                                                                                PEDCo- ENVIRONMENTAL
                         73

-------
                                                  SCHOLZ  IB AND 2B - CHIYODA (Continued)



„   u               Operating hours              FGD system
Honth         Boiler      FGP system          OperabfHty (X)
                                                                                            Comments

                                                                    modifications for reducing the quantity of liquid waste from the system.  Start-up

                                                                    and testing of this modification was planned for the first week In May.   A fire

                                                                    at the plant, however, necessitated a delay In system restart for an additional

                                                                    3 to 4 week period.
                                                                                                                      PEDCo-ENVIRONMENTAL
                                                                      74

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
  38

 KANSAS CITY  POWER  ft LIGHT

 HAWTHORN NO  3

 KANSAS CITY  MISSOURI

  1HO  MW
 FUEL CHARACTERISTICS  COAL   0.6- 3.0 PERCENT SULFUR
 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START  UP DATE

 FGD STATUS

 EFFICIENCY.
  PARTICULATES
 COMBUSTION  ENGINEERING

 LIMESTONE INJECTION «UET SCRUB

 RETROFIT

 11/72

 OPERATIONAL


 99 PERCENT
  S02
70 PERCENT
 WATER  MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
UNSTABILIZLD SLUDGE DISPOSED IN UNLINED POND
                     S19/KW CAPITAL*2.5 MILS/KWH OP
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
FGD SYSTEM HAS BEEN OPEHATIONAL SINCE NOVEMBER 1972. BOTH MODULES WERE
DOWN THROUGHOUT THE REPORT PERIOD. THE UTILITY IS CURRENTLY ELIMINATING
THE BY-PASS SEALS AND INSTALLING SLIDE-GATE DAMPERS. IN ADDITION, THE
B-MODULE WAS RECONVERTED TO AN UNDERBED SPRAY ARRANGEMENT BECAUSE OF
CONTINUING PLUGGING PROBLEMS.
                                                          75
                                                                                PEOCo-ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                   THE HAWTHORN POWER STATION:  UNIT NO. 3

      THE.HAWTHORN  POWER  STATION  IS LOCATED ON THE NORTH BANK OF THE MISSOURI RIVER IN EAST KANSAS CITY, MISSOURI.  THE PLANT HAS FIVE ELECTRIC
 GENERATING  UNITS WITH A  TOTAL  RATED CAPACITY OF 980 MW.  ONLY UNITS 3 AND 4 ARE RETROFITTED WITH FGD SYSTEMS.
      BOILER 3  IS A DRY-BOTTOM  PULVERIZED-COAL-FIRED UNIT, MANUFACTURED BY COMBUSTION ENGINEERING AND INSTALLED IN EARLY 1950.  THE PLANT BURNS TWO
 GRADES OF COAL:  THE COAL WITH HIGHER ASH CONTENT TYPICALLY CONTAINS 14 PERCENT ASH AND 3 PERCENT SULFUR. WITH A HEAT CONTENT OF 11,400 BTU/LB; THE LOWER
 ASH COAL HAS 11 PERCENT  ASH, 0.6 PERCENT SULFUR, AND A HEAT CONTENT OF 9800 BUT/LB.   •
      THE FGD SYSTEM OPERATES ON LIMESTONE FURNACE INJECTION FOLLOWED BY A FLUE GAS WET-SCRUBBING SYSTEM IN WHICH BOTH THE S02 AND THE FURNACE CALCINED
 LIMESTONE ARE  SCRUBBED AND ALLOWED TO REACT IN A REACTION TANK.
      THE FGD SYSTEM CONSISTS OF TWO IDENTICAL MODULES, EACH CAPABLE OF TREATING 500,000 ACFM OF FLUE GAS AT 300°F.   BYPASSING OF THE MODULES IS
 POSSIBLE THROUGH A  SYSTEM OF DUCTWORK AND DAMPERS AROUND EACH MODULE.  EACH MODULE CONSISTS OF A GLASS MARBLE BED,  A CHEVRON TYPE FIBERGLASS DEMISTER,
 AND A FINNED TUBE  REHEATER.  THE DEMISTER WASH SYSTEM USES A SET OF EIGHT WATER LANCES THAT TURN ON AUTOMATICALLY. TO WASH MUD FROM THE DEMISTERS
 WHENEVER THE DAMPERS CLOSE.
      THE SPENT LIMESTONE SLURRY FROM THE MODULES IS DISCHARGED INTO A CLARIFIER TANK,  AND THE UNDERFLOW IS PUMPED.  UNSTABILIZED, TO A 160-ACRE
 UNLINED POND. WHICH IS ALSO USED FOR DISPOSAL OF FLY ASH FROM THE OTHER BOILERS.
 PROBLEMS AND SOLUTIONS
      THE MAJOR PROBLEMS ENCOUNTERED WITH THE TWO FGD SYSTEMS ON UNITS 3 AND 4 AT THE HAWTHORN POWER STATION HAVE BEEN IDENTICAL.
      BECAUSE MAINTAINING THE SOLIDS IN THE REACTION TANKS IN SUSPENSION WAS DIFFICULT, BUILDUP OF MUD OCCURRED IN THE CORNERS  OF THE TANK.   THE
 PROBLEM WAS  SOLVED  BY ROUNDING THE BOTTOM CORNERS, INSTALLING FRESH WATER FLUSHING NOZZLES ON EACH WALL,  AND INCREASING THE  HORSEPOWER OF THE  TANK
MIXERS.
      SEDIMENT BUILDUP OCCURRED IN THE DRAIN POTS HORIZONTAL HEADERS.  ALSO, FREQUENT DISLOCATION OF THE MARBLE BED  DRAIN  POT COVERS  AND CONSEQUENT
LOSS  OF MARBLES WAS SOLVED BY  INSTALLING NEW STAINLESS STEEL DRAIN POTS  WITH EXPANDED  METAL COVERS AND MODIFYING THE  DRAIN PIPING.   OTHER MODIFI-
CATIONS INCLUDED INSTALLING A NEW WASH SYSTEM TO CONTROL DEMISTER PLUGGING. CHANGING THE FLUSHING SEQUENCE WITHIN THE WATER  SEAL  TO  ELIMINATE  BYPASS
SEAL  PLUGGING. AND REPLACING SPRAY NOZZLES.   THESE MODIFICATIONS WERE COMPLETED BY FEBRUARY 1974.   ADDITIONAL  MODIFICATIONS  AND  SYSTEM DESIGN  CHANGES
ARE CONTAINED IN THE COMMENTS SECTION OF THE OPERATING HISTORY SUMMARY FOR THIS INSTALLATION.

                                                                                                                            PEDCO-ENVIRONMENTAL
                                                                         76

-------
                                                               HAWTHRON NO. 3

                              Operating Hours          FGD Operablllty (X)
Month      Boiler      .  Module 3A     .Module 3B    Module AModule B                        Comments
Jul. 75      584             0                          0                       Problems with Module 3A Included a leak In city water line, a plugged
                                                                                duct to the  I.D. fan, and a malfunctioning outlet damper from the
                                                                                scrubber.
                                           247                       42         Marbles were lost from the bed and a spray header was broken.
Aug< 75        o             0               00             0         Lost I.D. fan for half of the boiler.  Carryover of July problems.
Sep. 75      358           247              81         69            23         Outage due to cleaning and mechanical repairs.  Pots, covers, and marbles
                                                                                In  the marble bed of module 3B were replaced.
Oct. 75      180           117             145         65         >  81         Module 3A outage was due largely to replacement of a recycle pump motor.
                                           :JV                                   A scheduled  boiler overhaul reduced boiler operation hours.
Nov. 75        0             0               0          0             0         Boiler and scrubbers were shut down for a scheduled turbine overhaul.
Ogc. 75   •    o             0               00             0         The system Is scheduled to go back on-Hne 1n January 1976.
Jan  76        0             0               00             0         System was down all month because of frozen equipment and lines and a
                                                                                manpower shortage due to a boiler and turbine overhaul on another unit
                                                                                at  this station.
Feb. 76      503           148               7         37              1         Scrubber outages resulted from plugging 1n the scrubber bed. caused by
                                                                                conversion from an under-bed to over-bed spray system.
Mar. 76        0             0               00             0         Reconversion of Module 3B's spray system arrangement has been completed.
Apr< 76        0             0               00             0         Also, the bypass system has been modified and changed to a slide-gate
                                                                                damper arrangement.
                                                                                                                              PEDCo-ENVIRONMENTAL
                                                                       77

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.


 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY!
  PARTICULATES



  S02



 WATER HAKE UP



 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
  39


 KANSAS CITY POWER 8 LI6HT


 HAWTHORN NO 4


 KAriSAS CITY MISSOURI


  100 MW


 COAL   0.6- 3.0 PERCENT SULFUR


 COMBUSTION ENGINEERING


 LIMESTONE INJECTION IWET SCRUB


 RETROFIT


  8/72


 OPERATIONAL



 99 PERCENT



 70 PERCENT
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
S19/KU CAPITAL*2.2 MILS/KWH OP
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS  REPORT.  THIS
 FGO SYSTEM HAS BEEN OPERATIONAL SINCE AUGUST 1972. OPERABILITY FOR
 MODULES A AND B WAS 0 AND 3 PERCENT RESPECTIVELY IN MARCH AND «2  AND
 HO PERCENT RESPECTIVELY IN APRIL. DURING THE REPORT PERIOD  THE UNIT'S
 BY-PASS SEALS WERE REPLACED WITH SLIDE-GATE DAMPERS.
                                                          78
                                                                                                      PEDCo- ENVIRONMENTAL

-------
                                                           BACKGROUND  INFORMATION
                                                                    ON
                                                   THE HAWTHORN POWER  STATION:   UNIT NO. 4

     THE HAWTHORN POWER STATON IS LOCATED ON THE NORTH BANK OF THE MISSOURI  RIVER  IN EAST KANSAS CITY, MISSOURI.  THE PLANT HAS FIVE ELECTRIC
GENERATING UNITS WITH A TOTAL RATED CAPACITY OF 980 MW.  ONLY UNITS 3  AND 4  ARE  RETROFITTED WITH FGD SYSTEMS.
     BOILER 4 IS A BOTTOM PULVERIZED-COAL-FIRED UNIT MANUFACTURED BY COMBUSTION  ENGINEERING AND INSTALLED  IN EALRY 1950.  THE PLANT BURNS TWO GRADES
OF COAL:  THE COAL WITH HIGHER ASH CONTENT TYPICALLY CONTAINS 14 PERCENT ASH AND 3 PERCENT SULFUR, WITH A  HEAT CONTENT OF 11.400 BTU/LB; THE LOWER-
ASH COAL HAS LL PERCENT ASH, 0.6 PERCENT SULFUR, AND A HEAT CONTENT OF 9800  BUT/LB.
     ORIGINALLY THE FGD SYSTEM OPERATED ON FURNACE INJECTION OF LIMESTONE FOLLOWED BY  FLUE GAS WET-SCRUBBING SYSTEM  IN WHICH BOTH THE S02 AND THE
FURNACE CALCINED LIMESTONE ARE SCRUBBED AND ALLOWED TO REACT IN A REACTION TANK.  BECAUSE OF  FURNACE TUBES PLUGGING. WHICH WAS ATTRIBUTED TO LIMESTONE
INJECTION, THE SYSTEM WAS CONVERTED IN 1972 TO TAILEND INJECTION, IN WHICH LIMESTONE  IS INJECTED  INTO THE  GAS DUCT BETWEEN THE AIR HEATER AND THE
SCRUBBER VESSEL.
     THE FGD SYSTEM CONSISTW OF TWO IDENTICAL^ODULES, EACH CAPABLE OF TREATING  500,000 ACFM  OF FLUE GAS AT 300°F.   BYPASSING OF THE MODULES IS
POSSIBLE THROUGH A SYSTEM OF DUCTWORK AND DAMPERS AROUND EACH MODULE.   EACH  MODULE CONSISTS OF A  GLASS MARBLE BED, A CHEVRON TYPE FIBERGLASS DEMISTER,
AND A FINNED TUBE REHEATER.
     THE DEMISTER WASH SYSTEM USES A SET OF EIGHT WATER LANCES THAT TURN ON  AUTOMATICALLY TO  WASH MUD FROM THE DEMISTERS WHENEVER THE DAMPERS CLOSE.
     THE SPENT LIMESTONE SLURRY FROM ALL MODULES IS DISCHARGED INTO A CLARIFIER  TANK,  AND THE UNDERFLOW  IS PUMPED. UNSTABILIZED. TO A 160-ACRE
UNLINED POND, WHICH IS ALSO USED FOR DISPOSAL OF FLY ASH FROM THE OTHER BOILERS.
     BECAUSE OF CONTINUED OPERATIONAL PROBLEMS SINCE START-UP, THE AVAILABILITY  FACTOR FOR  THE  SYSTEMS HAS BEEN  LOW, (IN THE .RANGE OF 30 PERCENT TO
40 PERCENT).  AVAILABILITY OF THE FGD SYSTEM HAS BEEN  HAMPERED BY MANY PROBLEMS  ATTRIBUTED  TO DRY LIMESTONE INJECTION.
OPERATING  HISTORY
     APART FROM THOSE ENTAILED  IN SWITCHING OF UNIT 4  FROM FURNACE  INJECTION TO TIAL GAS INJECTION,  THE  MAJOR PROBLEMS  ENCOUNTERED WITH THE FGD
SYSTEM  ON  BOILERS 3 AND 4 AT THE HAWTHORN POWER STATION HAVE BEEN  IDENTICAL.
     DIFFICULTY  IN MAINTAINING  SOLIDS IN THE REACTION  TANKS  IN SUSPENSION CAUSED BUILDUP OF MUD IN THE  CORNERS OF THE REACTION TANK.  THE PROBLEM WAS
SOLVED  BY  ROUNDING THE BOTTOM CORNERS,  INSTALLING  FRESH WATER FLUSING NOZZLES ON EACH WALL, AND INCREASING THE HORSEPOWER  OF THE TANK MIXERS.
      IN LATE  1972, BECAUSE OF BOILER TUBE PLUGGING, WHICH WAS ATTRIBUTED TO FURNACE-LIMESTONE INJECTION, THE UNIT WAS CONVERTED TO A TAILEND
LIMESTONE  INJECTION  SYSTEM.   SEDIMENT BUILDUP  OCCURRED IN THE DRAIN POTS HORIZONTAL HEADERS.  ALSO, FREQUENT DISLOCATION OF THE MARBLE  BED DRAIN POT
                                                                                                                                PEDCo-ENVIRONMENTAL
                                                                         79

-------
HAWTHORN UNIT NO. 4 (Continued)

COVERS AND CONSEQUENT LOSS OF MARBLES  WAS  SOLVED BY INSTALLING NEW STAINLESS STEEL DRAIN POTS  WITH  EXPANDED METAL COVERS AND MODIFYING THE POTS
DRAIN PIPING.  OTHER MODIFICATIONS INCLUDED  INSTALLING A NEW DEMISTER WASH SYSTEM TO CONTROL DEMISTER  PLUGGING, CHANGING THE FLUSHING SEQUENCE WITHIN
THE WATER SEAL TO ELIMINATE BYPASS SEAL  PLUGGING. AND REPLACING SPRAY NOZZLES.  THESE MODIFICATIONS WERE COMPLETED BY APRIL 1974.  ADDITIONAL
MODIFICATIONS AND SYSTEM DESIGN  CHANGES  ARE  CONTAINED IN THE COMMENTS SECTION OF THE OPERATING HISTORY SUMMARY FOR THIS INSTALLATION.
                                                                                                                           PEDCo-ENVIRONMENTAL
                                                                       80

-------
                                                               HAWTHORN NO. 4

                  Operating Hours                        FGD OperablHty (%)
Month          BoilerModule 4A      Module 4B      Module AModule B                          Comments
Jul. 75         518          41            128             8         25         Marble bed plugging and strainer problems  on  both modules.
Aug. 75                     168            212                                  Lost half of boiler due to No.  48 I.D.  fan outage.  Both  FGD modules were
                                                                                shut down to ensure against the loss  of the entire unit.  New
                                                                                chemistry - attempting to run at 100% blowdown and near 0 percent
                                                                                solids.   Emphasis on participate control.   Maintaining pH at 5 without
                                                                                limestone Injection.
Sep.            395         206            210            52         S3         Scrubber modules were returned  to service  on  Sept. 21 after replacement
                                                                                of the original  I.D. fan on module 4B side.
                                                                                New process design - marbles removed  from  scrubber bed of Module A
                                                                                and replaced with a stainless steel perforated bed.  The  marbles were
                                                                                removed  because  of continuing operational  difficulties.   Very good
                                                                                performance resulted 1n Increased availability and continuation of
                                                                                high participate removal  efficiency (97 percent).
Oct. 75         721         429            656            60         91         Minor boiler restriction on the Module  4A  side between the economizer
                                                                                and the  Inlet draft ductwork caused reduction of gas velocity.  New
                                                                                chemistry process modification  of running  at  100 percent  blowdown and
                                                                                zero percent solids 1s still  1n progress.   SOg removal efficiency in the
                                                                                50 to 60 percent range.  KCP&L  1s concentrating heavily on particulate
                                                                                emission control.
Nov. 75         720           0            713             0         99         Module 4A was shut down during  the report  period because  of loss of
                                                                                draft through the ductwork from the economizer to the air preheater.
                                                                      01
                                                                      81

-------
                                                        HAWTHORN NO. 4 (Continued)

                  Operating Hours                       FGD Operabllity (%)
Month          BoilerModule 4A      Module 4B      Module AModule B                          Comments
                                                                               The reheater plugged frequently  until  the system was shut down.
Dec. 75         640           0            103             0         16         Boiler outage of 5 days was due  to a scheduled overhaul.
Jan. 76           0           0             0             0          0         The system was down all month  because  of frozen equipment and lines;
                                                                               manpower was assigned to a boiler and  turbine overhaul on another unit.
Feb- 76         579           0            450             0         78         Module 4A was shut down the entire month because of continuing loss
                                                                               of draft through the ductwork  from the economizer to the air preheater.
                                                                               Marble bed plugging and loss of  a recycle pump occurred on Module 4B.
Mar. 76         706           0            24             0          3.4   .    During the report period the unit's bypass seals were replaced with
Apr. 76         550         231            2£0            42         40         slide-gate dampers.
                                                                                                                       PEDCo-ENVIRONMENTAL
                                                                      82

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME'

 UNIT LOCATION

 UNIT RATING
   HO


 KANSAS CITY POWER ft LIGHT


 LA CYGNE NO 1


 LA CYGNE KANSAS


   620 MW
 FUEL CHARACTERISTICS  COAL 5.0 PERCENT SULFUR
 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START  UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULARS
 BABCOCK ft WILCOX


 LIMESTONE SCRUBBING


 NEW


  2/73


 OPERATIONAL
             <*.


 98 PERCENT
  S02
 76 PERCENT
 WATER  MAKE UP
 CLOSED LOOP
 SLUDGE  DISPOSAL
 UNSTABILIZED SiUDGE DISPOSED IN UNLINED POND
UNIT COST
S52/KH CAPITAL * 1.26 MILLS/  KWH
OPERATIONAL
 EXPERIENCE
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS REPORT.  THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE FEBRUARY 1973. DURING 1975 THE
 TOTAL AVAILABILITY OF THE FGD SYSTEM AVERAGED IN EXCESS OF 04  PERCENT
 (INCLUDING BOTH WORKING AND RESERVE HOURS).  DURING THE FIRST QUARTER OP
 1976 SYSTEM AVAILABILITY HAS AVERAGED 63i92, AND 91 PERCENT FOR  THE
 MONTHS OF JANUARY, FEBRUARY, AND MARCH RESPECTIVELY. THE SYSTEM  WAS
 BROUGHT DOWN ON APRIL 6 FOR A SCHEDULED BOILER AND AIR PREHEATER
 OVERHAUL.
                                                          83
                                                                                                   PEDCo-ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                             LA CYGNE UNIT NO.  1

    . THE LA CYGNE POWER STATION OF KANSAS CITY POWER AND LIGHT COMPANY BEGAN COMMERCIAL OPERATION ON JUNE 1M973,  AS A JOINT PROJECT OF KANSAS"GAS"
AND ELECTRIC COMPANY AND KANSAS CITY POWER & LIGHT COMPANY.  THE STATION IS LOCATED ABOUT 55 MILES SOUTH OF  KANSAS  CITY, IN LINN COUNTY. KANSAS.
     ELECTRIC POWER GENERATING FACILITIES CONSIST OF ONE 820 MW COAL-FIRED BASE-LOAD BOILER WITH ASSOCIATED  STEAM TURBINES AND ELECTRIC GENERATORS.
THE PLANT HAS THREE OIL-FIRED BOILERS, USED PRIMARILY FOR STARTUP OF THE LARGE  UNIT.  THEIR COMBINED CAPACITY  IS  EQUIVALENT TO 28 MW.
     THE BOILER AT LA CYGNE, DESIGNED BY BABCOCK AND WILCOX, IS A DRY-BOTTOM, PULVERIZED-COAL-FIRED CYCLONE  UNIT.   THE COAL BURNED IS  LOW-GRADE,
SUBBITUMINOUS, WITH AN AS-FIRED HEATING VALUE OF 9000 TO 9700 BTU/LB AND ASH AND SULFUR CONTENTS OF 25  PERCENT AND  5  PERCENT,  RESPECTIVELY.   POLLUTION
CONTROL EQUIPMENT ON THIS BOILER CONSISTS OF SEVEN FGD MODULES, BUILT BY BABCOCK AND WILCOX AS AN INTEGRAL PART OF  THE POWER GENERATING FACILITIES.
BYPASSING OF THE BOILER'S FLUE GAS AROUND THE FGD SYSTEM IS NOT POSSIBLE.
PROBLEMS AND SOLUTIONS
     THE FGD INSTALLATION HAS BEEN PLAGUED WITH NUMEROUS PROBLEMS SINCE THE FIRST TRIAL OPERATION ON DECEMBER  26. 1972.   SOME  OF THESE PROBLEMS, SUCH AS
VIBRATIONS OF THE INDUCED-DRAFT FANS AND THEIR SENSITIVITY TO IMBALANCE, OCCURRED EVEN BEFORE THE BOILER WAS FIRED.
     AS THESE FABRICATION PROBLEMS WERE CORRECTED AND THE FGD SYSTEM WENT INTO  OPERATION,  TWO OTHER TYPES OF PROBLEMS APPEARED.   THE FIRST TYPE,
ASSOCIATED WITH THE WET LIMESTONE PROCESS, INCLUDES PLUGGING OF THE DEMISTER AND STRAINERS,  WEARING OF  SPRAY NOZZLES, AND CORROSION OF REHEATER TUBES.
PROBLEMS OF THE SECOND TYPE MAY BE UNIQUE TO THE LACYGNE INSTALLATION;  THEY CONCERN THE EFFECT OF THE SCRUBBED FLY ASH ON VISCOSITY AND FLOW  CHARACTER-
ISTICS OF THE RECIRCULATED SLURRY, WHICH RESTRICTS MOBILITY OF THE BALLS IN THE TCA TOWER.
     FLY ASH CONTENT OF THE FLUE GAS (DUE TO LACK OF PRIMARY PARTICULATE CONTROLS)  IS LARGELY RESPONSIBLE FOR  BOTH TYPES  OF  PROBLEMS.   SEVERAL MODIFICA-
TIONS HAVE BEEN MADE:  THE ORIGINAL TURBULENT CONTACT ABSORBER'S FLOATING BED WAS REPLACED WITH  SIEVE TRAYS; ALSO TO  REDUCE  THE  EROSIVE  EFFECT OF FLY
ASH AND LARGE-SCALE PARTICLES, AND TO EXTEND THE LIFE OF THE LIMESTONE  SLURRY SPRAY NOZZLES  ON THE VENTURI SCRUBBERS,  A HYDROCLONE WAS  INSTALLED IN THE
SLURRY RECIRCULATION LINE OF EACH MODULE TO CENTRIFUGALLY SEPARATE AND  REMOVE THESE PARTICLES FROM THE  SYSTEM.
     THE CORROSION ASSOCIATED WITH CONDENSATION OF ACID VAPORS FROM THE GAS ON  THE  REHEATER  TUBE BUNDLES  WAS CONTROLLED BY  INJECTION OF  SLIP STREAMS OF
HOT AIR FROM THE BOILER'S COMBUSTION AIR HEATER INTO THE SCRUBBED FLUE  GASES AT THE INLET  TO THE REHEATER UNITS.  THIS PRACTICE HAS REDUCED THE MAXIMUM
GENERATING CAPACITY OF THE BOILER BY LIMITING THE AIR AVAILABLE FOR COAL COMBUSTION.
                                                                                                                           PEDCO- ENVIRONMENTAL
                                                                        84

-------
LA CYGNE UNIT NO. 1 (Continued)







     BECAUSE THE FGD SYSTEM INCLUDES NO SPARE MODULES AND IT CANNOT BE BYPASSED, OUTPUT OF THE BOILER  IS TOTALLY CONTROLLED BY PERFORMANCE AND



AVAILABILITY OF THE FGD MODULES.   PRESENT  PROCEDURES CALL FOR CLEANING ONE MODULE EACH NIGHT ON A ROTATIONAL SCHEDULE AND KEEPING ALL MODULES AVAILABLE



DURING THE DAYTIME PEAK PERIODS.   CLEANOUTS  REQUIRE THREE MEN FOR A PERIOD OF 10 TO 12 HOURS.  RECENT  MODIFICATIONS BY THE UTILITY ON THE SCRUBBER



INSTALLATION HAVE RESULTED IN PLANS FOR PROLONGED OPERATIONAL PERIODS. WITH MODULES STAYING ON-LINE  CONTINUOUSLY FOR PERIODS UP TO 3 WEEKS.
                                                                                                                        PEDCo-ENVIRONMENTAL




                                                                      85

-------
FGD SYSTEM AVAILABILITY
  LA CYGNE UNIT NO. 1
Month Boiler Hours A
Jan.
Feb.
Mar.
Apr.
May
Jun.
Jul.
Aug.
Sep.
Oct.
Nov.
Dec.
Jan.
Feb.
Mar.
Apr.
74
74
74

74
74
74
74
74
74
74
74
75
75
75 694
75
May 75 683
Jun.
Jul.
Aug.
Sep.
75 667
75 590
75 630
75 610
49
66

67
69
92
75
90
69
90
90



82

95
88
78
75
78
B
32
68

70
83
84
80
90
' 88
71
71



96

85
85
90
88
84
C
44
59

75
78
83
80
73
73
60
60
•


90

94
84
90
87
84
D
87
76
Boiler
88
85
90
81
~81
76
61
61
Boiler
Boiler
Boiler
76
5 Days
90
85
84
78
85
™w
E
23
52
f
37
100
G
81
65
Average
50
69
Shutdown
74
78
82
85
81
83
84
84
100
84
83
79
78
89
85
85
88
80
87
77
99
86
84
84
80
80
86
80
85
81
76
76
Shutdown
Shutdown
Shutdown
93
of
90
84
85
92
79
92
Operation
89
86
87
85
78
96

83
89
85
83
74
90

89
86
86
84
80
                                                      Comnents
                             Modules A and D are used for research tests.
                             One module Is shut down each evening for cleaning.
                             System shutdown Oct. 16. 1975 owing to problems with
           86
                                                               PEDCo- ENVIRONMENTAL.

-------
                    FGD SYSTEM AVAILABILITY (continued)
                            LA CYGNE UNIT NO. 1
Percent Avallablllty-by Module
                           -            •                                         Comments
nontn BOI ler nours
Oct. 75 231
Nov. 75 346
Dec. 75 597

Jan. 76
Feb. 76
Mar. 76
Apr. 76
inn \t U t i M n»«.i »a»
66 77 46 74 72 73 65 68
93 90 80 93 96 89 94 91
91 87 81 85 87 89 84 86

83
92
91

generator and I.D. air fan. System remained Inoperative
throughout the month.
Availability figures for October and November do not Include
the outage time from October 16 to November 13. Boiler outages
of 80. 50, and 11 hours, totaling 141 hours, occurred during
December.



The system was shot down on April 6 for a scheduled boiler and
                                                        air preheater overhaul.  During this outage some maintenance
                                                        Is being performed on the scrubber ductwork because of
                                                        corrosion problems.

                                                        Note:  The 1974 figures are based on actual operating hours of
                                                               each module divided by hours of boiler operation.
                                                             « During reduced boiler load operation, some  of  these
                                                                modules were not needed and were shut down, although
                                                                they were available.  Availability was therefore
                                                                higher than some of these figures Indicate.  The 1975
                                                                figures are based on the hours the module  was In
                                                                service or available for service divided by the total
                                                                hours In the month.
                                                                                          PEDCo- ENVIRONMENTAL
                                       87

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  05/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT- LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP UATE
 FGD STATUS
 EFFICIENCYt
  PARTICULATES
  S02
 WATER HAKE UP
 SLUDGE DISPOSAL
 43
KANSAS POWER ft LIGHT
LAWRENCE NO 4
LAWRENCE KANSAS
 125 MW
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE INJECTION ftUET SCRUB
RETROFIT
12/68
OPERATIONAL

99 PERCENT

75 PERCENT
UNSTADILIZED SLUOGE DISPOSED IN UNLtNED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
FGO SYSTEM HAS BEEN OPERATIONAL SINCE DECEMBER 1966. THIS UNIT IS CUR-
RLNTLY BURNING LOW SULFUR WYOMING COAL. THE OPERATION OF THE SCRUBBER HAS
BEEN MORE EFFICIENT AND ECONOMICAL FOR THIS COAL TYPE BECAUSE A LESSER
DEGREE OF S02 REMOVAL IS REQUIRED FOR COMPLIANCE. THE UTILITY PLANS TO
REPLACE THIS SCRUBBING SYSTEM WITH A VCNTRI-ROD AND SPRAY TOWER SCRUBBING
SYSTEM.
                                                                                                    PEDCo-ENVIRONMENTAL
                                                          88

-------
                                                            BACKGROUND INFORMATION
                                                                      ON
                                                    THE LAWRENCE POWER STATION:   UNIT NO.  4

      LAWRENCE POWER STATION'S UNIT NO. 4 IS A CYCLIC LOAD STEAM BOILER EQUIPPED TO BURN COAL,  NATURAL GAS SUPPLEMENTED WITH OIL. OR COMBINATIONS OF
 THESE THREE FUELS.  THE BOILER WAS BUILT BY COMBUSTION ENGINEERING AND PLACED IN SERVICE  IN  1959.  GENERATING CAPACITY VARIES FROM 125 MW TO 143 MM WITH
 THE TYPE OF FUEL BEING BURNED.  RETROFITTING WITH AN FGD SYSTEM IN NOVEMBER  1968 INTRODUCED  ADDITIONAL PRESSURE DROP IN THE FLUE GAS SYSTEM AND
 REDUCED BOILER CAPACITY TO 115 MW.
      THE COAL NOW BURNED AT THE LAWRENCE POWER PLANT IS A LOW-SULFUR  SOUTHEAST  WYOMING COAL, HAVING AN AVERAGE HEATING VALUE OF 10,000 BTU/LB AND SULFUR
 AND ASH CONTENTS OF 0.5 AND 11 PERCENT RESPECTIVELY.
      THE BOILER HAS TWO MODULES,  EACH  DESIGNED TO HANDLE ROUGHLY 150,000 SCFM OF FLUE GAS.   EACH MODULE CONSISTS OF A SINGLE-STAGE MARBLE BED SCRUBBER
 FOLLOWED BY A CHEVRON-TYPE DEMISTER AND AN  INDIRECT  C.S.  REHEATER.  ORIGINALLY. BOTH MODULES WERE FITTED WITH BYPASS DUCTS AND HYDRAULIC SEAL DAMPERS.  .
 WHICH WERE  LATER REMOVED BECAUSE  OF EXTENSIVE' CORROSION  AND PLUGGING.
      THE PLANT HAS  FACILITIES  FOR STORING AND  MILLING THE LIMESTONE. WHICH CONTAINS 93 PERCENT CALCIUM CARBONATf,  6 PERCENT SILICA. AND 1  PERCENT
 MAGNESIUM CARBONATE.
      SPENT  SLURRY FROM  THE UNIT,  ALONG  WITH THE SLURRY FROM UNIT NO. 5. IS SENT  TO THREE  INTERCONNECTED UNLINED  SLUDGE DISPOSAL PONDS OF  16.  28 AND 4
 ACRES.   KANSAS  RIVER WATER IS ADDED TO  THE 4-ACRE POND.  THE CLARIFIED WATER FROM THIS POND IS RECYCLED.  THE SLUDGE IS NOT TREATED FURTHER AND IS
 REPORTED TO SET AND SOLIDIFY IN THE PONDS.
 PROBLEMS AND SOLUTIONS
      PROBLEMS WITH THE FGD SYSTEM ON BOILER NO. 4 HAVE INCLUDED BUILDUP AND PLUGGING OF THE INLET DUCT WHERE  HOT GASES ENTER THE SCRUBBERS. EROSION
OF SCRUBBERS WALLS. CORROSION OF SCRUBBERS INTERNALS, BUILDUP  ON ID FAN ROTORS.  AND PLUGGING  OF DRAIN LINES,  MARBLE  BEDS. AND DEMISTERS.  LOW SO  REMOVAL
WAS CAUSED BY OVERBURNING OF THE LIMESTONE AND DROPOUT OF THE  LIME  WITH THE ASH  IN  THE BOTTOM OF THE SCRUBBER.                                  *
     THE SCRUBBERS WERE MODIFIED IN 1969 BY RAISING THE DEMISTER AND ADDING SOOT BLOWERS IN THE INLET DUCT AND REHEATER TO REDUCE PLUGGING.  NEW SPRAY
NOZZLES WERE ALSO INSTALLED.  REHEATER  PLUGGING WAS ELIMINATED BY REPLACING COPPER  REHEAT COILS WITH A CARBON STEEL UNIT HAVING WIDELY SPACED FINS.
                                                                      89                                                   PEDCo-ENVIRONMENTAL

-------
 LAWRENCE UNIT NO. 4  (Continued)

     MAJOR MODIFICATIONS IN 1970 WERE SANDBLASTING AND COATING OF THE INTERIOR OF THE SCRUBBERS,  REPLACEMENT OF ALL  INTERNAL STEEL PIPES WITH PLASTIC
 AND FIBERGLASS, AND  REPLACEMENT OF STAINLESS STEEL DEMISTERS WITH FIBERGLASS.  *SINCE  DEMISTER  PLUGGING WAS NOT COMPLETELY ELIMINATED. THE UNIT WAS
 WASHED MANUALLY EVERY NIGHT TO MAINTAIN THE REQUIRED OUTPUT.
     THE MODIFICATIONS IN THE SUMMER OF 1972 ON THE TWO FGD MODULES INCLUDED ENLARGEMENT OF THE CRYSTALLIZATION TANK, AND INSTALLATION OF NEW
 PLASTIC SPRAY NOZZLES, NEW SLURRY PUMPS AND STRAINERS, AND NEW MULTIPLE MIXERS IN THE TANK.
     PROBLEMS REMAINING ARE CORROSION, UNSATISFACTORY DAMPER OPERATION. EXPANSION JOINT FAILURE,  DEMISTER FOULING. RAPID WEARING OF THE SLURRY PUMP.
 AND VALVE FAILURE.  OPERATION OF THE FGD SYSTEM SINCE THE FALL OF 1973 HAS  BEEN THE MOST SUCCESSFUL TO DATE.
     OPERATION OF THE SCRUBBER SYSTEM ON THE WYOMING COAL HAS PROVED TO BE  MORE EFFICIENT AND  ECONOMICAL THAN EARLIER OPERATIONS BECAUSE A LESSER DEGREE
 OF S02 REMOVAL IS REQUIRED FOR COMPLIANCE.   THE SCRUBBER SYSTEM IS STILL OPERATING IN THE HIGH-SOLIDS MODE AS AN SOg AND PARTICULATE REMOVAL SYSTEM.
 NORMAL MANUAL CLEANING REQUIREMENTS HAVE BEEN REDUCED TO TWO-4-HOUR SHIFTS  PER SCRUBBER PER WEEK.
     IN 1974 THIS UNIT WAS AVAILABLE FOR OPERATION 343 DAYS.   FIFTY PERCENT OF THE FUEL CONSUMED WAS COAL, 2 PERCENT FUEL OIL, AND 48 PERCENT NATURAL
 GAS.  DURING 1975 THIS UNIT WAS AVAILABLE FOR OPERATING 333 DAYS.   SIXTY-FOUR  PERCENT OF THE FUEL CONSUMED WAS COAL, 3 PERCENT FUEL OIL, AND 33 PERCENT
NATURAL GAS.
     BY 1977, THE TWO FGD MODULES WILL BE REPLACED BY TWO NEW C.E.  UNITS. EACH CONSISTING OF A VENTURI ROD UNIT AND A SPRAY CHAMBER.   A NEW ELECTRO-
STATIC PRECIPITATOR IS ALSO TO BE INSTALLED.
                                                                                                                             PEDCo-ENVIRONMENTM.
                                                                      90

-------
                                                              LAURENCE NO. 4
Month
Jul. 75
Aug. 75

Sep. 75
Oct. 75
Nov. 75
Dec. 75
Jan. 76
Feb. 76
 Mar.  76
 Apr.  76
Boiler
                           HoduteA
                      erating hours
                              lule B
Operating h
ule A   VfoS
                    Not logged
                    Not logged

                    Not logged
                    Not logged
                    Not Logged
                    Not logged
                    Not logged
                    Not logged
   Availability
HoduTeTModule B
                                                                                                             Comments
                                                         The FGD system has operated satisfactorily for over a  year.
                                                         Availability is reported to be adequate for the operation of
                                                         this station.  Station load is reduced to 50 percent every
                                                         night.  Therefore, one of the modules can be taken off-line
                                                         nightly for cleaning or repair.  Wyoming coal (0.5 percent
                                                         sulfur is being burned in this boiler/  Some natural gas has been
                                                         burned since June 20.
                                                         Burned coal 100 percent of time.  Each module shut down once per
                                                         week for inspection and cleanup.  No boiler outages In July  and
                                                         August.
                                                          Present projections  by  the utility call for this unit to be
                                                          available 330 days-during 1976.  The fuel comsumptlon will be 80
                                                          percent coal, 12  percent natural gas, and 8 percent fuel oil.
                                                          The utility is replacing this scrubber system with a venturi
                                                          rod-section followed by a spray tower.
                                                                        91
                                                                                                                            PEDCO-ENVIRONMENTAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  OS/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F6D VENDOR

 PROCESS

 NEW OR  RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCY,
 PARTICULATES


 502


 WATER MAKE UP


 SLUDGE DISPOSAL


UNIT COST
OPERATIONAL
 EXPERIENCE
 KANSAS POWER 8 LIGHT

 LAWRENCE NO 5

 LAWRENCE KANSAS

  too MW

 COAL 0.5 PERCENT SULFUR

 COMBUSTION ENGINEERING

 LIMESTONE INJECTION  4WET  SCRUB

 NEW

 11/71

 OPERATIONAL


 99  PERCENT


 65  PERCENT
UNSTABILIZED SLUDGE DISPOSED IN UNLINEO POND
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.  THIS
FGD SYSTEM HAS BEEN OPERATIONAL SINCE NOVEMBER 1971.  THIS UNIT IS CUR-
RENTLY BURNING LOW SULFUR WYOMING COAL. THE OPERATION OF THE SCRUBBER HAS
BEEN MORE EFFICIENT AND ECONOMICAL FOR THIS COAL TYPE BECAUSE A LESSER
DEGREE OF S02 REMOVAL IS REQUIRED FOR COMPLIANCE. THE UTILITY PLANS TO
REPLACE THIS SCRUBBING SYSTEM WITH A VENTRI-ROO AND SPRAY TOWER SCRUBBING
SYSTEM.
                                                           92
                                                                                                     PEDCo-ENVIRONMENTAL

-------
                                                            BACKGROUND INFORMATION
                                                                      ON
                                                    THE LAWRENCE POWER STATION:   UNIT NO.  5

      UNIT NO. 5 AT LAWRENCE POWER STATION IS A CYCLIC-LOAD STEAM BOILER EQUIPPED TO BURN  COAL,  NATURAL  GAS  SUPPLEMENTED WITH OIL. OR COMBINATIONS OF
 THESE FUELS.  THE BOILER, PLACED IN SERVICE IN 1971,  HAS A RATED CAPACITY  OF  400 MW WHEN  BURNING COAL AND NATURAL GAS.
      THE COAL NOW BURNED AT THE LAWRENCE POWER PLANT  IS A LOW-SULFUR  SOUTHEAST WYOMING COAL, HAVING AN  AVERAGE HEATING VALUE OF 10.000 BTU/LB AND
 SULFUR AND ASH CONTENTS OF 0.5 AND 11  PERCENT RESPECTIVELY.
      THE BOILER'S FGD SYSTEM WAS BUILT BY COMBUSTION  ENGINEERING AND  PLACED IN SERVICE IN  1971.  THE BOILER HAS EIGHT IDENTICAL MODULES, EACH DESIGNED
 TO HANDLE ROUGHLY 150,000 SCFM OF FLUE GAS.   EACH MODULE CONSISTS OF  A  SINGLE-STAGE MARBLE BED SCRUBBER FOLLOWED BY A CHEVRON-TYPE DEMISTER AND AN
 INDIRECT C.S.  REHEATER.   ALL THE MODULES ARE  FITTED WITH BYPASS  DUCTS AND HYDRAULIC SEAL DAMPERS.  THE PLANT FACILITIES FOR STORING AND MILLING THE
 LIMESTONE,  WHICH  CONTAINS 93 PERCENT CALCIUM  CARBONATE,  6 PERCENT SILICA, AND 1 PERCENT MAGNESIUM CARBONATE.
      SPENT  SLURRY FROM THE UNIT ALONG  WITH THE SLURRY FROM UNIT  NO. 4 IS SENT TO THREE INTERCONNECTED UNLINED SLUDGE DISPOSAL PONDS OF  16.  28,  AND
 4  ACRES.  COOLING TOWER  BLOWDOWN SUPPLIES MAKE-UP WATER  TO THE POND SYSTEM.  CLARIFIED POND WATER IS RECYCLED.  THE SLUDGE IS NOT  TREATED FURTHER
 AND IS  REPORTED TO SET AND SOLIDIFY IN  THE PONDS.
 PROBLEMS  AND SOLUTIONS
      PROBLEMS WITH THE FGD  SYSTEM ON BOILER NO. 5 WERE SIMILAR PROBLEMS TO THOSE  OF THE SYSTEM ON BOILER NO. 4:   LOCALIZED CORROSION IN SOME EQUIPMENT.
 UNSATISFACTORY DAMPER  OPERATION, DEMISTER FOULING. EXPANSION JOINT FAILURE. AND RAPID WEAR OF  SLURRY-RECIRCULATING  PUMPS.   IN ADDITION TO THESE
 PROBLEMS. BOILER No. 5 IS PLAGUED WITH POOR FLUE GAS DISTRIBUTION TO THE EIGHT FGD MODULES WHICH. UNLIKE THE MODULES ON BOILER NO. 4 ARE ALL INTER-
 CONNECTED TO A COMMON STACK.
     FGD SYSTEM AVAILABILITY IS REPORTED TO BE ADEQUATE FOR OPERATION  OF THIS  STATION.  BECAUSE  STATION  LOAD IS REDUCED TO 50 PERCENT EVERY NIGHT.
AS MANY AS FOUR MODULES CAN BE SHUT DOWN FOR CLEANING  AND REPAIR EACH  EVENING.
     OPERATION OF THE SCRUBBER SYSTEM ON WYOMING COAL  HAS PROVED TO  BE MORE EFFICIENT AND  ECONOMICAL BECAUSE OF THE  LESSER  DEGREE OF SO  REMOVAL
REQUIRED.
                                                                                                                               PEDCo- ENVIRONMENTAL
                                                                        93

-------
LAURENCE UNIT NO.  5  (Continued)



     IN 1974 THE UNIT WAS AVAILABLE FOR OPERATION  338 DAYS:  66 PERCENT OF THE FUEL  CONSUMED WAS NATURAL GAS. 27 PERCENT COAL. AND 6 PERCENT FUEL OIL.

DURING 1975 THE UNIT WAS AVAILABLE FOR OPERATION 352 DAYS. FUEL CONSUMPTION.WAS 45 PERCENT NATURAL GAS. 42 PERCENT COAL. AND 13 PERCENT FUEL OIL.
                                                                                                                           PEDCo- ENVIRONMENTAL
                                                                    94

-------
                                                               LAURENCE NO. 5
 Months
                  Operating hours
  Open
BoTTer
FGD modules
                                                                                                    Comments
Jul. 75
Aug. 75
Sep. 75
Oct. 75
Nov. 75
Dec. 75
Jan. 76
Feb. 76

Mar. 76
Apr. 76
          Not  logged

          Not  logged

          Not  logged

          Not  logged
          Not  logged
                                      Wyoming coal  Is being burned In this unit.  FGD system availability Is reported to be
                                      adequate for  operation of this station.  Since station load 1s reduced to 50 percent
                                      every night,  as many as four modules can be shut down for cleaning and repair each
                                      evening.
                                      FGD units were off-line'most of June for major rebuilding of the spray systems 1n  all
                                      modules.  Some oil was burned to allow bypassing of the repair.
                                      011 and gas were burned In July and August.  No FGD operation.

                                      Gas and oil burned on a part-time basis during September and October.   Boiler outage
                                      was due to Inspection, turbine repair,  and replacement of the slurry tank screen.
                                      Projections by the utility for this  unit  call  for  330 days of operation 1n 1976 with
                                      fuel consumption being 60 percent coal. 25  percent fuel oil. and 15 percent natural
                                      gas.  Like Unit 4, this unit will  be converted to  a venturl-rod and spray tower system.
                                                                                                                           PEDCo-ENVIRONMENTAL
                                                                        95

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FRO STATUS

 EFFICIENCY!
  PARTICULATES


  S02
 KENTUCKY UTILITIES

 GREEN RIVER   UNITS 1 AND 2

 CENTRAL CITY KENTUCKY

   64 nw

 COAL  3.8 PERCENT SULFUR

 AMERICAN AIR FILTER

 LIME SCRUBBING

 RETROFIT

  9/75

 OPERATIONAL
            *«
             »M

 99.7 PERCENT '


 60 PERCENT GUARANTEE
 WATER MAKE UP
 SLUDGE DISPOSAL
 CLOSED LOOP
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S64/KU CAPITAL


 REFER TO BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.  THIS
 SYSTEM BECAME OPERATIONAL SEPTEMBER 13. 1975.  THE OPERATIONAL DATA
 SUPPLIED BY THE UTILITY FOR THE REPORT PERIOD  SHOWS THAT SYSTEM
 AVAlLABILITYt KELIABILITYt OPERABILITY. AND UTILIZATION WAS 97. 95, 85,
 AND 52 PERCENT RESPECTIVELY FOR THE MONTH OF MARCH AND 90. 100. lOOi AND
 77 PERCENT RESPECTIVELY FOR THE MONTH OF APRIL.
                                                                                                PEDCo-ENVIRONMENTAL
                                                          96

-------
                                                                 BACKGROUND INFORMATION
                                                                           ON
                                                                GREEN RIVER POWER  STATION
      THE GREEN RIVER POWER STATION OF THE  KENTUCKY  UTILITIES  COMPANY  IS  SITUATED ON  GREEN RIVER, NEAR CENTRAL CITY, IN MUHLENBERG COUNTY. KENTUCKY.
      THE STATION CONSISTS OF TWO POWER GENERATING UNITS AND FOUR  BOILERS.  THE POWER GENERATORS ARE PEAK LOAD UNITS.  THE BOILERS PROVIDING STEAM
 TO THE GENERATORS ARE NORMALLY  OPERATIONAL  5  DAYS PER WEEK, WITH  ONE  OR  MORE OFTEN OPERATING AT REDUCED CAPACITY.
      THE S02  AND PARTICULATE CONTROL  SYSTEMS  FOR BOILERS  1, 2, AND 3  CONSIST OF MECHANICAL COLLECTORS AND A TAIL-END LIME SCRUBBING SYSTEM.
      A CONTRACT FOR  THE LIME SCRUBBING SYSTEM WAS AWARDED TO  AMERICAN AIR FILTER IN  JUNE 1973.  CONSTRUCTION WAS COMPLETED AND THE SYSTEM STARTED
 UP SEPTEMBER  13,  1975.  THE  SYSTEM WAS DESIGNED TO  TREAT  FLUE GAS FROM BOILERS 1, 2, AND 3, WHICH HAVE A COMBINED RATED CAPACITY OF 64 MW.  THE FUEL
 IS PRIMARILY  A HIGH-SULFUR  (3.5 TO 4.0 PERCENT) WESTERN KENTUCKY  COAL.
      THE FGD  SYSTEM  CONSISTS  OF ONE SCRUBBER  MODULE DESIGNED  TO HANDLE A MAXIMUM GAS CAPACITY OF 360,000 ACFM AT 300°F.  THE FLUE GAS IS DRAWN FROM THE
 EXISTING BREECHING THROUGH A  GUILLOTINE-TYPE'ISOLATION DAMPER AND DUCT SYSTEM TO THE SCRUBBER FAN.   THE GASES THEN FLOW THROUGH AN ADJUSTABLE-THROAT
 VENTURI  SCRUBBER AND FLOODED  ELBOW, WHICH WAS PROVIDED PRIMARILY  FOR PARTICULATE REMOVAL.  S02 IS REMOVED BY REACTION WITH THE LIME SLURRY IN THE MOBILE
 BED CONTACTOR, WHICH  CONSISTS OF TEN COMPARTMENT SECTIONS WITH OVERHEAD SLURRY SPRAYS AND UNDERBED DAMPERS TO ACCOMMODATE GAS VOLUME TURNDOWN.
     THE SLURRY/RECYCLE SYSTEM CONSISTS OF A PARTITIONED REACTANT TANK WITH RECYCLE PUMPS FOR SUPPLYING THE CONTACTOR AND VENTURI, A LIME SLURRY SLAKING
AND FEED SYSTEM. AND A BLEED SYSTEM DISCHARGING TO A SETTLING POND.   RETURN WATER FROM THE POND IS  USED AS PRIMARY MAKE-UP.
                                                                       g?

-------
                                                           FGD SYSTEM AVAILABILTY
                                                          GREEN RIVER NOS.  1  AND 2
 Period
 Dec.  75
   Total
period (hr)
    744
Availability = 74X
Reliability « 78%
Operablllty « 65X
Utilization = 35%
Jan. 76      744
Availability = 42X
Reliability = 14X
Operablllty = 11X
Utilization = 9X
Feb. 76      696
Availability - 70X
Reliability » 42*
Operablllty = 42X
Utilization = 30X
Mar. 76      744
Availability - 97X
Reliability = 95X
Operablllty • 85X
Utilization - 52X
   Boiler
operation (hr)
     398
     Module
availability (hr)
     550
No. hr. module
called upon
to operate
   331
Hr. module
 operated
   257
                   572
                      312
                       456
                                                                        64
                  499
                     486
                      499
                                                                       211
                  450
                     722
                      409
                                                                       386
                    Comments
System became operational September 13,  1975,  on  a  half-
load basis because of turbine overhaul.   The half-load
mode continued throughout the report period.  Logging of
operating data began December 1975.
                                  System was down a total of 432 hours 1n January.   Major
                                  problems were failure of the recycle pumps and feed
                                  tank agitator, thawing and repair of numerous frozen
                                  lines, and shutdown of sump pumps.

                                  The system was Inoperative a total of 210 hours in
                                  February.  Outage was due to repairs of tank agitators,
                                  recycle pumps, and reactant pumps and to cleanout  of
                                  reactant pumps, slurry pumps, slake tanks, and mix-hold
                                  tank.
                                  During the report period all the rubber-lined Impellers
                                  were replaced in the pumps.
                                                                                                                            PEOCo-ENVIRONMENTAL
                                                                       98

-------
                                                    FGD SYSTEM AVAILABILITY (Continued)

                                                         GREEN RIVER NOS. 1 AND 2



                                                           No. hr. module
            Total          Boiler             Module         called upon   •    Hr. module
Period,   period (hr)    operation (hr)   a vail ability (hr)    to operate         operated                           Comments

Apr. 76      720           552              648              552               552          The utility made a prior commitment to run at 100 percent

AvaiUblllty » 90S                                                                          operablllty during the month of April.

Reliability - 100X

Operablllty - 100X

Utilization - 77%
                                                                                                                       PEDCo- ENVIRONMENTAL
                                                                     99

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
 FGD VENDOR

 PROCESS

 NCW OR RETROFIT
 START UP DATE

 FGD STATUS
 EFFICIENCY,
  PARTICULATES
 KEY WEST UTILITY BOARD

 STOCK ISLAND PLANT

 KLY WEST FLORIDA

   37 MW
 FUEL CHARACTERISTICS  OIL
        2.1 PERCENT SULFUR
 ZURN AIR SYSTEMS

 LIMESTONE SCRUBBING

 NEW

 10/72

 OPERATIONAL


 90 PERCENT
  S02


 WATER  MAKE UP
 65 PERCENT-ESTIMATED
 MAKE UP RATE ESTIMATED 100 GPM
 SLUDGE  DISPOSAL
                                 UNLINED POND
UNIT COST
S 21.6/KW CAPITAL COST
OPERATIONAL
 EXPERIENCE
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS REPORT.  THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE OCTOBER 1972.  THE FGD SYSTEM  HAS
 BEEN OUT OF SERVICE SINCE JANUARY 2Btl975. MODIFICATIONS AND REPAIRS  ARE
 CURRENTLY IN PROGRESS.  SYSTEM RESTART IS STILL INDEFINITE. A CHECKOUT
 OF ALL SYSTEM MOTORS AND PUMPS MUST BE COMPLETED BEFORE STARTUP  CAN
 COMMENCE.
                                                          100
                                                                                                       PEDCo-ENVIRONMtrtTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                             STOCK ISLAND PLANT
     THE UTILITY  BOARD OF THE CITY OF KEY WEST OPERATES AN OIL-FIRED 37 MW POWER PLANT ON STOCK ISLAND, ADJACENT TO THE  ISLAND CITY OF KEY WEST.  THIS
STEAM GENERATOR BURNS A HIGH SULFUR FUEL OIL (2.4 - 2.75% SULFUR) GENERATING 210,000 CFM OF FLUE GAS AT 390°F.   TO REMOVE THE SULFUR DIOXIDE FROM THE
FLUE GAS A SCRUBBING SYSTEM, CONSISTING OF TWO MODULES, HAS BEEN DESIGNED BY ZURN AIR SYSTEMS.   THE SYSTEM USES  PULVERIZED CORAL AND SEAWATER.  THE CORAL
IS  INITIALLY GROUND TO A FINE POWDER IN A HAMMER-MILL CRUSHER. THEN MIXED WITH SEAWATER TO FORM A DILUTE SLURRY  AND TRANSFERRED TO THE SCRUBBING SYSTEM
TO  ABSORB SULFUR  DIOXIDE.  THE CLEANED GAS IS DISCHARGED TO ATMOSPHERE AND THE SPENT SLURRY IS  PUMPED TO A SETTLING POND.  THE CLARIFIED SEAWATER IS
DISCHARGED INTO THE GULF.
     THE TWO SCRUBBER.MODULES ARE DESIGNED TO HANDLE A COMBINED TOTAL OF 126,950 CFM AT 150°F.   FLUE GASES FROM  TEH BOILER ARE DRAWN THROUGH AN INDUCED
DRAFT FAN AND FORCED EITHER THROUGH THE BYPASS DUCT OR THROUGH ONE OR BOTH SCRUBBERS VIA THREE  SETS OF DAMPERS BETWEEN THE INDUCED-DRAFT FAN AND THE
STACK.  BEFORE ENTERING THE SCRUBBING SYSTEM THE GAS IS COOLED FROM 360°F TO 160°F BY SEAWATER  SPRAYS.   THIS COOLING PROTECTS THE FIBERGLASS COMPONENTS
OF THE SCRUBBER MODULES.   A PRESSURE DROP OF 12 TO 14 INCHES WATER GAUGE IS THE NORMAL OEPRATING RANGE FOR THE SCRUBBERS.
     THE FGD SYSTEM WAS PLACED IN OPERATION IN OCTOBER 1972.   THE SYSTEM WAS SHUT  DOWN ON JANUARY 28.  1975. FOR REPAIR OF THE BOILER FOUNDATION AND
DUCTWORK BAFFLES.   OTHER  IMPORTANT MODIFICATIONS TO BE COMPLETED ARE:   REPLACING SPRAY TREES AND OTHER STAINLESS STEEL PARTS WITH MONEL;  MODIFYING  AND
SEALING INLET DAMPERS;  REPAIRING THE INDUCED-DRAFT FAN;  AND  REPAIRING HOLE  IN HOPPER WALL AND DUCT FLOOR.
                                                                                                                             PEDCo-ENVIRONMENTAL
                                                                          101

-------
                                               STOCK ISLAND
Operating hours
FGD system
Month Boiler FED system
Jul.
Aug.
Sep.
Oct.
Nov.
Dec.
Jan.
Feb.
Mar.
Apr.
75
75
75
75
75
75
76
76
76
76
0
0
0
0
0
0
0
0
0
0
Availability
0
0
0
0
0
0
0
0
0
0
                                                                                        Comments
                                                     FGD system was shut down on January 28, 1975, because of damaged ductwork baffles.
                                                     Spray trees and other stainless steel  parts have been replaced with Monel.
                                                     FGD system Is still out of service but Is scheduled  for  restart In early October.
                                                     Boiler has been down since August 30 for repairs of  the  Induced-draft fan.
                                                     FGD system 1s still out of service.   Date of system  restart  1s Indefinite.

                                                     FGD system Is still out of service.  The utility Is  replacing dampers and various
                                                     system parts.  Date of system restart  Is still  Indefinite.
                                                     Repairs to outlet damper are complete.   All  holes In the hopper wall and ductwork
                                                     have been patched.  New spray trees  have been Installed.  The utility Is still
                                                     repairing the Inlet damper.   The system will  not restart for at least another
                                                     month pending checkout of all  pumps  and motors.
                                                     The FGD system restart has been delayed because  of boiler-related problems.   Date
                                                     of system restart Is still Indefinite.
                                                                                                             PEDCo-ENVIRONMENTAL
                                                       102

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  OS/76
 IDENTIFICATION NO.


 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS


 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 LOUISVILLE GAS ft ELECTRIC


 PADDYS RUN NO 6


 LOUISVILLE KENTUCKY


   65 HW


 COAL  3.5-t.O PERCENT SULFUR


 COMBUSTION ENGINEERING


 LIME SCRUBBING


 RETROFIT


  «»/73


 OPERATIONAL



 99 PERCENT  DESIGN
  S02



 WATER MAKE UP




 SLUDGE DISPOSAL



 UNIT COST
 80 PERCENT (DESIGN)
 33 GAL/LB MOLE S02 REMOVED
 UNSTABILIZEO SLUDGE DISPOSED IN UNLINEO POND
S57/KW CAPITAL
 OPERATIONAL
  EXPERIENCE
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.  THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE APRIL 1973. OPERABILITY WAS 100
 PERCENT IN JANUARY. S02 REMOVAL EFFICIENCY WAS 99 PERCENT DURING THIS
 OPERATING PERIOD. THE SYSTEM WAS SHUTDOWN IN EARLY FEBRUARY IN PREPARA-
 TION FOR THE EPA SCRUBBER AND SLUDGE STUDY WHICH MAY COMMENCE IN JUNE OR
 JULY OF 1976.  THE SCRUBBER WILL NOT BE OPERATED UNTIL THIS TIME UNLESS
 THE NEED ARISES (PEAK LOAD DEMAND). CURRENTLY* THE UTILITY IS COMPLETING
 MODIFICATIONS ON THIS UNIT IN ANTICIPATION OF THE STUDY PROGRAM.
                                                            103
                                                                                                     PEDCo-ENVIRONMENTAL

-------
                                                                BACKGROUND INFORMATION
                                                                          ON
                                                              PADDY'S RUN POWER STATION

      PADDY'S  RUN  POWER  STATION  IS LOCATED  IN LOUISVILLE, KENTUCKY.  THE PLANT HAS SIX ELECTRIC POWER GENERATING UNITS WITH A TOTAL RATED CAPACITY OF
320 MW.  UNIT NO. 6  IS  RETROFITTED WITH A  CARBIDE LIME-BASE FGD SYSTEM.
      UNIT NO. 6 IS A PEAK LOAD  COAL-FIRED  BOILER, MANUFACTURED BY FOSTER WHEELER AND INSTALLED IN 1950.   IN 1973,  THE BOILER BURNED COAL WITH  A GROSS
HEATING VALUE OF  11,500 BTU/LB  AND AVERAGE SULFUR AND ASH CONTENTS OF 3.7 PERCENT AND 13 PERCENT, RESPECTIVELY.
      THE FGD  SYSTEM  CONSISTS OF TWO MODULES.  EACH HANDLES 175,000 ACFM OF 350°F FLUE GAS.  EACH MODULE  IS MADE UP OF TWO STAGES  OF 3-INCH MARBLE
BEDS, FOLLOWED BY A  TWO-STAGE CHEVRON-TYPE DEMISTER.  THE GAS IS REHEATED BY DIRECT COMBUSTION OF NATURAL GAS.   S02 REMOVAL EFFICIENCY  IS REPORTED
TO  BE 80 PERCENT.
     THE LIME USED CONTAINS 90  TO 92.0 PERCENT CALCIUM HYDROXIDE, 2.0 TO 2.5 PERCENT SILICA, 3.0 TO 8.0  PERCENT CALCIUM  CARBONATE,  AND  0.1 PERCENT
MAGNESIUM OXIDE.
     THE UNIT OPERATES  ON A CLOSED-LOOP MODE:  THE S02 IS ABSORBED IN THE MARBLE BED BY A SLURRY OF CALCIUM SULFITE TO FORM A MIXTURE OF CALCIUM
SULFITE/BISULFITE.   EFFLUENT FROM THE MARBLE-BED TOWER IS CONVERTED IN THE REACTION TANK TO CALCIUM SULFITE BY  THE ADDITION OF CALCIUM  HYDROXIDE.  HALF
OF  THE REACTION TANK EFFLUENT IS RETURNED  TO THE S02 TOWERS, WHILE THE OTHER HALF IS FED TO A CLARIFIER  TANK.   THE CALCIUM SULFITE  CRYSTALS PRE-
CIPITATE WITH THE AID OF A FLOCCULANT, WHICH IS ADDED AT THE RATE OF 4 TO 7 PPM.  THE OVERFLOW IS RETURNED TO THE  REACTION TANK;  THE UNDERFLOW,
CONTAINING 22 TO 24  PERCENT SOLIDS, IS STABILIZED BY MIXING IT WITH LIME.   ABOUT 60 TO 100 POUNDS OF LIME ARE USED PER TON OF DRY SOLIDS OF SLUDGE.
THE FIXED SLUDGE IS  TRANSPORTED BY TRUCKS TO A 10-ACRE OFF-SITE SUMP FOR USE AS  LANDFILL.
     DURING THE INITIAL 45 DAYS OF OPERATION ONLY ONE ABSORBER WAS PLACED IN SERVICE, ALLOWING OPERATORS TO OBSERVE THE  EQUIPMENT AND TO DETERMINE ANY
NEEDED MODIFICATIONS.  BEGINNING MAY 19, 1974,  THE SYSTEM WAS SHUT DOWN FOR A MONTH FOR MODIFICATIONS, THE MOST SIGNIFICANT  BEING INSTALLATION OF
EQUIPMENT FOR INJECTING A FLOCCULATING AGENT INTO THE CLARIFIER TANK.   DURING THE PERIOD JUNE  19 TO JULY 11, INCONSISTENT  SIZING  OF SLURRY ADDITIVE
MATERIAL AS RECEIVED CAUSED MALFUNCTION OF THE  ADDITIVE CONTROL VALVES AND UNDUE PLUGGING  OF SLURRY LINE STRAINERS.  THESE PROBLEMS WERE  CORRECTED
BY  INSTALLATION OF A DISINTEGRATOR IN THE SLURRY ADDITIVE SYSTEM.   FROM AUGUST 19 TO SEPTEMBER 5,  THE UNIT WAS  SHUT DOWN TO  ENLARGE THE CLARIFIER'S
OVERFLOW SYSTEM.   ANOTHER MODIFICATION MADE WAS LOWERING OF THE SLURRY pH  TO REMOVE SULFITE SCALING FORMED ON THE  UPPER BED  PERFORATED SUPPORT
PLATE AND ON THE  MARBLES.
     OPERATING DATA. DESIGN MODIFICATIONS,  PROBLEMS AND SOLUTIONS  SINCE THE SYSTEM START-UP ARE  PRESENTED AND DISCUSSED IN THE FOLLOWING TABLE.

                                                                                                                               PEDCo-ENVIRONMENTAL
                                                                             104

-------
                                                               FGD SYSTEM AVAILABILITY
                                                               PADDY'S RUN UNIT NO. 6

                         QperabHlty {*)
Month                  Module A  Module B                              .                       Comments
Apr.'73                  18        56                  Modules were operated one at a time, with frequent shutdowns for Inspection of equipment  and
                                                       minor  repairs.
May  73                  11        65                  Single-module operation continued through May 19, when the unit was shut down for modifications.
                                                       The  most significant modification was Installation of equipment for Injection of a flocculating
                                                       agent  Into  the  clarifier tank.
jun. 73                   0.1       6                  Operation was Intermittent from June 19 to July 11 because of mechanical problems with the slurry
                                                       pumps.
jul. 73                  21        21                  During a scheduled outage from July 12 through August 1, several repairs were made to the lime
                                                       slurry makeup system.  A disintegrator unit was Installed to reduce plugging of strainers .and
                                                       slurry control  valves.
Aug. 73                  53        64                  The  operation was continuous from August 2 to August 18 except for a brief shutdown due to a
                                                       boiler-related  problem.  From August 19 to September 5. the system was shut down to replace the
                                                       clarifier1s underflow  line with one of larger diameter and to Install additional pump capacity In
                                                       the  clarifier's overflow system.
Sep. 73                  85        72                  The  unit operated continuously between September £ and September 20 except for a 7-hour shutdown
                                                       to repair a marble bed support plate.  The unit was shut down the remainder of the month because
                                                       of trouble  in the boiler's turbine generator.
Oct. 73                  49        94                  The  FGD system  was  In  service through December 20 after which the boiler (and the scrubbers)  were
Nov. 73                  35       100                  shut down because of  "no demand" (this 1s a peaking-load boiler).
Dec. 73                  44        78
Jan. 74                   00                  Boiler shut down because of  "no demand."
through
Jun. 74
                                                                                                                             PEDCo-ENVlRONMENTAt

                                                                        105

-------
                                                                FGD SYSTEM AVAILABILITY
                                                          PADDY'S RUN UNIT NO.  6 (tontlnued)

                         Operablllty (%)
Month                  Module A  Module B                                                     Comnents
Jul. 74                  51        81                  Boiler and FGD system resumed operation July 10. 1974.
Aug. 74                  50        77                  Unit has been on and off frequently due to fluctuation In power demand.
Sep. 74                   0         0                  Boiler Is down because of "no demand."
Oct. 74                 100       100                  Boiler turned on specifically to perform limestone tests on FGD system.
Nov. 74                   0         0                  Boiler Is down because of "no demand."
through
Aug. 75
SeP- 75                 100       TOO                  Boiler and FGD system operational all of September and first two weeks 1n October.  System outage
Oct- 75                 100       100                  during the last two  weeks  of October was due primarily to breeching In the boiler section.  Opera-
                                                       blllty for both modules  during the operational period was 100 percent (based upon LG&E's Peak Load
                                                       Determination).   S02 removal was reported to be over 98 percent.
Nov- 75                 10°       TOO                  Boiler and scrubber  system ran most of the report period on a Monday-through-Friday basis.  Two
Dec- 75                  90        90                  minor  outages  1n December were due to malfunction and repair of the dual  strainer switch shaft Into
                                                       bottom of the  scrubber module.
Jan- 76                 100       100                  S02  removal efficiency was reported to be 99 percent during January.   The system was  shut down In
Feb- 76                   00                  early  February 1n preparation for an EPA scrubber/sludge study scheduled  for June or  July.   The
                                                       scrubber will  not be operated until the start of the study program unless the boiler  1s  required
                                                       for  peaking power demands.  Highlights of the scrubber/sludge study program are  as follows:
                                                           0     6 month duration.
                                                           0     One  scheduled shutdown for test modifications.
                                                           0     Scrubber will run on carbide Hrne and commercial  lime.
                                                           •     Determination of minimum retention times.
                                                                                                                                PEDCo-ENVIRONMENTAL
                                                                              106

-------
                                                               FGD SYSTEM AVAILABILITY
                                                         PADDY'S RUN UNIT NO.  6 (Continued)

                         QperabllUy (*)                                                            Comments
Month                  HoduleA  HoSule B                                                          Con-nents
                                                           0    Deliberate high chloride concentration operation.
                                                           •    MgO Innoculatlon.
                                                           •    Extensive sludge study:  Fixation, leachates,  seasonal variations.
     7fi                  00                  The  unit did not operate during the report period in anticipation of  the EPA scrubber/sludge
                         00                  study.  The utility 1s now completing system modifications for the  operation of the test program.
    • *o

                                                       Note:   Since Paddy's Run No. 6 Is a peak load boiler, it operated for less  than a day on several
                                                              occasions 1n July and August 1974.  During these short boiler  runs,  the FGD system was
                                                              not  turned  on and was bypassed although it was available.
                                                                                                                        PEDCo-ENVIRONMENTAL
                                                                        107

-------
                   TABLE 3
PERFORMANCE: DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  os/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
  56

 MONTANA POWER CO,

 COLSTRIP NO 1

 COLSTRIP MONTANA

  360 MM
 FUEL CHARACTERISTICS  COAL   0.6 PERCENT SULFUR
 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY.
  PARTICULATES
COMBUSTION EQUIP. ASSOCIATES

 LIME/ALKALINE FLYASH SCRUBBING

 NEW

 10/75

 OPERATIONAL


 99 PERCENT
  S02
 60 PERCENT
 WATER MAKE UP
 CLOSED LOOP
 SLUDGE DISPOSAL
 UNSTABILIZED SLUUGE DISPOSED IN UNLINED POND
 UNIT COST
S50/KW CAPITAL
 OPERATIONAL
  EXPERIENCE
 THE COLSTRIP PLANT IS A MINE MOUTH INSTALLATION. CONSTRUCTION ON THIS
 UNIT WAS COMPLETED BEHIND SCHEDULE. THE FGD SYSTEM STARTED UP IN LATE
 197b AND PROCEEDED THROUGH A SHAKEDOWN AND DEBUGGING OPERATION PHASE. THE
 UNIT IS NOW OPERATING AT FULL COMMERCIAL CAPACITY. OPERATING DATA AC-
 CUMULATED TO-DATE IS IN THE PROCESS OF BEING EVALUATED BY- THE UTILITY FOR
 PRESENTATION TO STATE REGULATORY AGENCIES.
                                                          108
                                                                                                        PEDCo-ENVIRONMENTAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
  PARTICIPATES


  S02
 NEVADA POWER

 REID GARDNER NO 1

 MOAPA NEVADA

  125 MW

 COAL   0.5- 1.0 PERCENT SULFUR

 COMBUSTION EBUIP. ASSOCIATES

 SODIUM CARBONATE SCRUBBING

 RETROFIT
 OPERATIONAL
 99 PERCENT
 65 PERCENT
 WATER MAKE UP
 SLUD6E DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 190 6PM
 UNSTAHILIZED SLUDGE DISPOSED IN UNLINED POND
$«tt/KW CAPITAL (1974 DOLLARS) SfeOOtOOO ANNUALlZED
 REFLK TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.   THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE APRIL 1974. SYSTEM OPERABlLlTY FOR
 THE MONTHS OF MARCH AND APRIL WAS 72 AND 91 PERCENT RESPECTIVELY.  ONE
 FORCED SCRUBBEK OUTAGE OCCURRED DURING THE REPORT PERIOD BECAUSE OF A
 VENTURI LEAK. THE BOILER WAS SHUTDOWN APRIL 5 FOR A VALVE AND COAL CON-
 DUIT INSPECTION.
                                                         109
                                                                                 PEDCo-ENVIRONMENTAL

-------
                                                                 BACKGROUND INFORMATION
                                                                           ON
                                                                 REID GARDNER UNIT NO. 1
      THE REID GARDNER POWER STATION IS LOCATED NEAR MOAPA, NEVADA, ABOUT 50 MILES NORTH OF LAS VEGAS.  THE STATION HAS TWO ELECTRIC POWER GENERATING
 UNITS, (REID GARDNER 1  AND 2)  EACH RATED AT 125 MW.   BOTH UNITS ARE RETROFITTED WITH SODIUM CARBONATE BASED FGD SYSTEMS.  THE COAL BURNED AT THE
 PLANT HAS AN AVERAGE GROSS HEATING VALUE OF 12,450  BTU/LB, AND ASH AND.SULFUR CONTENTS OF 8 AND 0.5 PERCENT RESPECTIVELY.
      THE FGD SYSTEM ON  REID GARDNER 1  WAS MANUFACTURED BY COMBUSTION EQUIPMENT ASSOCIATES AND PLACED IN OPERATION IN APRIL 1974.   SYSTEM DESIGN WAS BASED
 ON DATA GATHERED FROM OPERATION  OF AN  8000-ACFM PILOT PLANT AT THE REID GARDNER POWER STATION IN 1971 AND 1972.
      THE FGD SYSTEM CONSISTS OF  A  SINGLE MODULE, DESIGNED TO HANDLE 473,000 ACFM OF GAS AT 350°F.  THE MODULE IS MADE UP OF A TWIN VARIABLE-THROAT
 VENTURI SCRUBBER,  FOLLOWED BY  A  SINGLE-STAGE WASH TRAY.  BYPASSING OF THE MODULE IS POSSIBLE THROUGH A GUILLOTINE-TYPE BYPASS VALVE.   A COMMON  FACILITY
 FOR TRONA (SODIUM  CARBONATE ORE) STORAGE AND SAND REMOVAL SERVES BOTH FGD MODULES ON REID GARDNER UNITS 1  AND 2.  SO, REMOVAL EFFICIENCY IS  REPORTED
 TO BE 85 PERCENT.
      IN THIS  SODIUM CARBONATE  PROCESS, HOT FLUE GAS FROM THE BOILER PASSES FIRST THROUGH MECHANICAL COLLECTOR (MULTICYCLONE),  WHERE ABOUT  75 PERCENT
 OF THE  FLY ASH  IS  REMOVED.   PRESSURE IS  THEN BOOSTED BY AN INDUCED-DRAFT FAN BEFORE THE GAS STREAM SPLITS  AS  IT ENTERS THE  TWIN-THROAT VENTURI
 SCRUBBER.  THE  HOT FLUE GAS  IS QUENCHED  BY A SHOWER OF CIRCULATED SODIUM BASE LIQUOR.   THE GAS  THEN ENTERS THE WASH  TRAY  AND  BUBBLES THROUGH THE RADIAL-
 VANE MIST ELIMINATOR, WHERE THE REMAINING LIQUID DROPLETS CARRIED OVER  WITH THE  GAS ARE TRAPPED AND REMOVED.
     EFFLUENT FROM THE FGD SYSTEM  IS FROM TWO SOURCES:  THE  SLIP  STREAM OF  SPENT LIQUOR DISCHARGED FROM THE RECIRCULATION TANK, AND THE ALKALINE
 CLARIFIER UNDERFLOW, WHICH SERVES TO NEUTRALIZE THE pH OF THE  COMBINED  LIQUOR  BEFORE IT IS  DISCHARGED TO THE SLUDGE SETTLING PONDS.  THE SPENT LIQUOR
 IS PUMPED INTO ONE OF TWO SETTLING PONDS.  THE OVERFLOW FROM THIS  POND  IS PUMPED TO  A LARGER 45-ACRE POND. WHERE THE BRINE IS EVAPORATED.  THE FGD
SYSTEM OPERATES ON AN OPEN WATER LOOP WITH NO LIQUOR RECYCLED  TO THE MODULES FROM THE PONDS. '
                                                                                                                           PEDCo-ENVIRONMENTAL
                                                                       110

-------
                                                               REID GARDNER 1
                   Operating Hours
Month           Boiler    FGD system     Operablllty (%}         	Comnents
                                                                 During February the FGD  system operated with  95 percent availability on trona
                                                                 supplemented  with  soda ash.   Availability  1n  January was only about 65 percent because
                                                                 of frozen sodium carbonate  feed lines.  Problems  1n February Included a 2-day lack of
                                                                 chemicals.  No  significant  problems occurred  In March.  The unit ran April 1 through
                                                                 April  12 with 100  percent availability.  The  boiler was then shut down for routine
                                                                 maintenance.  The  system was  placed back on line  May 12.   .Second performance test was
Jul. 75                                         851              passed.   Problems  Included  an abrasion of  rubber-lined pipes and routine mechanical and
                                                                 Instrumental  problems.   High ash content, up to  20 percent, had no effect on
                                                                 emissions.
Aug. 75
Sep. 75           716       559                 77               Of four forced  outages,  three were caused  by  scrubber malfunctions.
Oct. 75           303       106                 35               Low operating time was due  to scheduled boiler maintenance.  One outage was due to the
                                                                 malfunction of  a soda ash blower.
Nov. 75           654       394                 60               The utility reports system  performance in  terms of the operabillty Index.  Unit No. 1
Dec. 75                                                          operabillty was low for  the month of November because of delays In delivery of repair
                                                                 materials.
Jan. 76           646       186                 29               Three  forced  outages during the month were due to reheater steam leaks, collapse
                                                                 of a venturi  strainer, and  a  frozen carbonate line.  The system was shut down for 16
                                                                 days for completion of piping conversion;  this outage was not due to scrubber
Feb. 76           664       520                 78               malfunction.  The  utility reported five scrubber  inoperative periods during the month
                                                                 of February,  three of which were scrubber  related outages.  The forced scrubber
                                                                 occurred because of guillotine damper unit switch problems, depletion of chemical,
                                                                 chemical line plugging and  seal  water problems.
Mar. 76           398       287                 72               Only one scrubber-related outage occurred  during  the month, because of a venturi leak.

                                                                                                                             PEDCo-ENVIRONMENT
                                                                       Ill

-------
                                                          REID GARDNER 1  (Continued)
                  Operating Hours
Month          Bo Her   FGD system    OperablHtv (%)        	Comments
Apr. 76          106        97             91                The boiler was taken out of service on April 5 for Inspection of valves and coal

                                                            conduits.
                                                                 112                                               PEDCO-ENVIR0NMHWAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  OS/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 F6D VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICIPATES

  S02

 WATER HAKE UP

 SLUDGE DISPOSAL
 UNIT  COST
 OPERATIONAL
  EXPERIENCE
  65
 NEVADA POWER
 REID GARDNER NO 2
 MOAPA NEVADA
  125 nw
 COAL   0.5- 1.0 PERCENT SULFUR
 COMBUSTION EQUIP. ASSOCIATES
 SODIUM CARBONATE SCRUBBING
 RETROFIT
 OPERATIONAL

 99 PERCENT

 65 PERCENT

 190 6PM

 UNSTABILIZEO SLUUGE DISPOSED IN UNLINED POND
S<»t/KW(1974 DOLLARS)* S600 t OOOANNUALIZEO
 KEFEK TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.  THIS
 FGO SYSTEM HAS BEEN OPERATIONAL SINCE APR. 197<*. SYSTEM OPERABILXTY FOR
 THE MONTHS OF MARCH AND APRIL WAS 60 AND 77 PERCENT RESPECTIVELY. DURING
 THE REPORT PERIOD SEVERAL FORCED SCRUBBER OUTAGES WERE XEPORTEDt
 PRIMARILY CAUSED BY PLUGGED SENSING LINES* REHEATER REPAIRS.
 AND MALFUNCTIONS IN THE TRAY SYSTEM.
                                                                                                         PEDCo-ENVIRONMENTAL
                                                            113

-------
                                                            BACKGROUND INFORMATION
                                                                      ON
                                                            REID GARDNER UNIT  NO.  2
      THE REID GARDNER POWER STATION IS LOCATED NEAR HOAPA,  NEVADA. ABOUT  50 MILES NORTH OF LAS VEGAS.  THE STATIONS HAS TWO ELECTRIC POWER GENERATING
 UNITS, (REID GARDNER 1 AND 2) EACH RATED AT 125 MW.   BOTH UNITS ARE RETROFITTED WITH SODIUM CARBONATE BASED FGD SYSTEMS.  THE COAL BURNED AT THE
 PLANT HAS AN AVERAGE GROSS HEATING VALUE OF 12,450  BTU/LB,  AND ASH AND SULFUR CONTENTS OF 8 AND 0.5 PERCENT RESPECTIVELY.
      THE FGD SYSTEM ON REID GARDNER WAS MANUFACTURED BY COMBUSTION EQUIPMENT ASSOCIATES AND PLACES IN OPERATION IN APRIL 1974.  SYSTEM DESIGN WAS
 BASED ON DATA GATHERED FROM OPERATION  OF AN 8000 ACFM PILOT PLANT AT THE REID GARDNER POWER STATION IN 1971 AND 1972.
      THE FGD SYSTEM CONSISTS OF A  SINGLE MODULE, DESIGNED TO HANDLE 473,000 ACFM OF GAS AT 350°F.   THE MODULE IS MADE  UP OF A TWIN VARIABLE-THROAT
 VENTURI  SCRUBBER,  FOLLOWED BY A SINGLE-STAGE WASH TRAY.  BYPASSING OF THE MODULE IS POSSIBLE THROUGH A GUILLOTINE-TYPE BAYPASS VALVE.   A COMMON FACILITY
 FOR  TRONA (SODIUM  CARBONATE ORE) STORAGE AND SAND REMOVAL SERVES BOTH FGD MODULE ON REID GARDNER UNITS 1  AND 2.   S02 REMOVAL EFFICIENCY IS REPORTED TO
 BE 85 PERCENT.
      IN  THIS  SODIUM CARBONATE PROCESS,  HOT  FLUE GAS FROM THE BOILER PASSES FIRST THROUGH A MECHANICAL COLLECTOR  (MULTICYCLONE),  WHERE ABOUT 75  PERCENT
 OF THE FLY ASH IS  REMOVED.   PRESSURE IS  THEN BOOSTED BY AN  INDUCED DRAFT FAN  BEFORE  THE GAS STREAM SPLITS AS IT  ENTERS THE  TWIN  THROAT  VENTURI  SCRUBBER.
 THE  HOT  FLUE GAS IS QUENCHED BY A SHOWER OF CIRCULATED SODIUM BASE LIQUOR.  THE  GAS  THEN ENTERS  THE WASH  TRAY AND  BUBBLES THROUGH  THE WATER ON  THE  SIEVE
 TRAY.  THE SCRUBBER GAS, WHICH IS ESSENTIALLY FREE OF FLY ASH AND  SULFUR DIOXIDE,  PASSES THROUGH THE  RADIAL  VANE MIST  ELIMINATOR.  WHERE THE REMAINING
 LIQUID DROPLETS CARRIED OVER WITH THE GAS ARE TRAPPED AND REMOVED.
     EFFLUENT FROM THE FGD SYSTEM IS FROM TWO SOURCES:  THE  SLIP STREAM  OF SPENT LIQUOR DISCHARGED FROM THE RECIRCULATION TANK, AND THE ALKALINE
CLARIFIER UNDERFLOW, WHICH SERVES TO NEUTRALIZE THE  pH OF  THE COMBINED LIQUOR BEFORE  IT IS  DISCHARGED TO  THE SLUDGE SETTLING PONDS.  THE SPENT LIQUOR
 IS PUMPED INTO ONE OF TWO SETTLING PONDS.  THE OVERFLOW FROM THIS  POND IS  PUMPED TO A LARGER 45 ACRE POND WHERE THE BRINE IS EVAPORATED.  THE FGD
SYSTEM OPERATES ON AN OPEN WATER LOOP WITH NO LIQUOR RECYCLED TO THE MODULES FROM THE PONDS.
                                                                                                                            PEDCo-ENVIRONMENTAL
                                                                          114

-------
                                                                REID GARDNER 2

                Operating Hours
                                         FGD  System
 Month     Boiler      FGD system  .   OperabllUv  (*)                                           Comments
                                                            During February the FGD system operated with 90 percent operabillty on trona supplemented
                                                            with soda ash.  Problems Included a plugged recycle line strainer,  seal  water filters,
                                                            and boiler controls.  Unit has restarted after shutdown for 5-year  turbine overhaul.
 Ju1'  75                                   85X               Second performance test was passed.  Problems Included abrasion of  rubber-lined pipes and
                                                            routine mechanical and instrumental problems.  High ash content, up to 20%,  had no effect
                                                            on emissions.
 Aug.  75
 Sep.  75     645          496              77^               Three forced outages were due to strainer plugging, broken  bucket elevator,  worn re-
                                                            circulation piping, and rubber liner leakage.
 Oct.  75     531          464              87                Three forced outages during October were due to pump repair,  Instrument  plugging, and
                                                            repair of piping  leakage.
 Nov.  75     603          596              99                The utility reports system performance in terms of  the  operabllity  Index.
 Dec.  75
 Jan.  76     691          458              66                Boiler was out of  service  a total of 3 days  during  the  month.  Scrubber outages were
                                                            caused by  frozen carbonate lines, plugged pressure-sensing  lines, and overhaul of a tray
                                                            recycle pump.
 Feb. 76     675          578              86                The utility reported four  scrubber  Inoperative  periods during the month, three of which  were
                                                            scrubber-related outages.   The forced  scrubber  outages occurred because of plugging in a
                                                            venturi pump,  depletion of  chemical, chemical line plugging, and seal water problems.
Mar. 76     660          395              60                The utility reported that the FGD system was operational over 395 hours during this period.
                                                                                                                          PEDCO-ENVIRONMENTAL
                                                                          115

-------
                                                       REID GARDNER 2  (Continued)

               Operating Hours
                                       FGD System
Honth     Boiler      FGD system     OperabHlty (X)                                          Comments
                                                           One  scrubber-related outage occurred during  the month, because of plugging 1n the tray
                                                           system and  subsequent overhaul  of the tray recycle pumps.
Apr. 76     629          488              77                Four forced scrubber outages, totaling over  98 hours, were reported by the utility for the
                                                           month of April.  The scrubber has been 1n operation 8711 hours since startup.
                                                                                                                            PEDCo- ENVIRONMENTAL
                                                                         116

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  OS/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL .CHARACTERISTICS

 F6D VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY.
  PARTICULATES
 NORTHERN STATES POWER CO.

 SHEKBURNE NO 1

 BECKER MINNESOTA

  660 MU

 COAL 0.8 PERCENT SULFUR

 COMBUSTION ENGINEERING

 LIMESTONE SCRUBBING

 NEW

  3/76

 OPERATIONAL


 99 PERCENT GUARANTEE
  502
 50 PERCENT GUARANTEE
 WATER MAKE UP
 SLUDGE DISPOSAL
                                 UNLINED POND
 UNIT COST
S60/KW CAPITAL
 OPERATIONAL
  EXPERIENCE
 A PRELIMINARY SYSTEM CHECKOUT BY PASSING WATER  AND AIR  THROUGH THE  EQUIP-
 MENT WAS SUCCESSFULLY COMPLETED BY  THE UTILITY. THE SYSTEM WAS PUT  IN
 SERVICE ON MAKCH 16i 1976t  TREATING FLUE GAS FROM BOILER  N0.lt WHICH
 FIRES A LOW SULFUR WESTERN  COAL. FOLLOWING  THE  3/16 STARTUP THE SYSTEM
 WAS TESTED ON VARIOUS LOAD  CAPACITIES AND IS CURRENTLY  OPERATING AT FULL
 COMMERCIAL LOAD. A SO-DAY VENDOR RELIABILITY TEST PROGRAM IS SCHEDULED
 TO COMMENCE IN MID-SUMMER 1976.
                                                                                                        PEDpo-ENVIRONNpUL
                                                             117

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT .LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR  RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCYt
 PARTICULATES

 S02

 WATER MAKE UP

 SLUDGE DISPOSAL

UNIT COST
OPERATIONAL
 EXPERIENCE
   76

  PENNSYLVANIA POWER CO.

  BRUCE MANSFIELD NO. 1

  SHIPPINGPORT PENNSYLVANIA

   635 MW

  COAL  
-------
                                                           BACKGROUND  INFORMATION
                                                                    ON
                                                         BRUCE  MANSFIELD  UNIT NO.  1

     THE BRUCE MANSFIELD PLANT IS A 2700-HW. THREE-UNIT.  COAL-FIRED FACILITY LOCATED ON THE OHIO RIVER IN THE BOROUGH OF SHIPPING PORT. PENNSYLVANIA.
THIS NEW FACILITY IS BEING BUILT BY PENNSYLVANIA POWER CO., WHICH  IS ACTING ON  ITS OWN BEHALF AND AS AGENT FOR THE OTHER PARTICIPATING COMPANIES -
CLEVELAND ELECTRIC ILLUMINATING CO.. DUQUESNE LIGHT CO..  OHIO EDISON CO.. AND TOLEDO EDISON CO.
     BRUCE MANSFIELD NO. 1 IS A COAL-FIRED. ONCE-THROUGH. SUPERCRITICAL STEAM GENERATOR WHICH FIRES 333 TONS/HR. OF COAL, NEARLY 6.5 MM LB/HR.
OF STEAM AT 3.785 PSIG, 1005°F/1005°F.  THE EMISSION CONTROL EQUIPMENT REQUIRED FOR THIS UNIT IS DESIGNED TO MEET STATE EMISSION REGULATIONS OF
0.6 LBS S02/106 BTU OF HEAT INPUT AND 0.0175 GR/SCF OF PARTICULATE WHEN BURNING 11,900 BTU/LB COAL HAVING AVERAGE ASH AND SULFUR CONTENTS OF 12.5
AND 4.3 PERCENT.
     IN LATE 1970, AN INTENSIVE INVESTIGATION OF MORE THAN 30 POTENTIAL DESULFURIZATION SYSTEMS WAS INITIATED.  THE SYSTEM ULTIMATELY CHOSEN FOR
THE REMOVAL OF FLY ASH AND SULFUR OXIDES WASTHE VENTURI  WET-SCRUBBING SYSTEM,  MANUFACTURED BY CHEMICO AIR POLLUTION CONTROL CO.. EMPLOYING DRAVO
CORPORATION'S THIOSORBIC LIME.
     THE DESIGN FEATURES OF THE SCRUBBING SYSTEM CALLS FOR EACH SCRUBBING TRAIN TO CONSIST OF A SCRUBBING VESSEL, A 9000-HP I.D. FAN, AND
AN ABSORBER VESSEL.  THERE ARE 6 SCRUBBER TRAINS PER UNIT, 5 OF WHICH  ARE REQUIRED TO HANDLE THE FLUE GAS FLOW FROM THE BOILER AT FULL LOAD (3.35 MM
ACFM AT 285°F).  THE SCRUBBER/ABSORBER TRAINS ARE ARRANGED IN TWO  GROUPS  OF THREE. THE TREATED FLUE GAS, WHICH HAS PASSED THROUGH THE SCRUBBING
SYSTEM. IS DUCTED THROUGH A COMMON REHEAT CHAMBER AND THEN EXHAUSTED UP THE 950-FT. STACK.
     THE ADJUSTABLE VENTURI THROAT SCRUBBING MODULE REMOVES NEARLY ALL OF THE FLY  ASH CONTAINED IN THE FLUE GAS.  THE ABSORBER MODULE. WHICH IS A
FIXED-THROAT VENTURI, REMOVES THE REMAINING FLY ASH.  SOg IS ABSORBED  IN  BOTH THE  SCRUBBER AND ABSORBER BY DROPLETS OF LIME SLURRY. CONTAINING
2 TO 6 PERCENT MgO.
     THE SCRUBBER-RECYCLE BLEED IS THEN COMBINED WITH A FLY ASH SLURRY FROM THE BOILER AND A FLOCCULANT AND PUMPED TO A 200 FT. DIAMETER THICKENER.
SLUDGE FROM THE THICKENER IS THEN PUMPED TO A WASTE DISPOSAL SYSTEM WHERE IT IS MIXED WITH A STABILIZING AGENT (CALCILOX) AND THEN PUMPED
APPROXIMATELY 7 MILES TO THE LITTLE BLUE RUN RAVINE FOR LAND FILL.
                                                                           1]g                                              PEOCo-ENVIRONMENTAL

-------
                                                           BRUCE MANSFIELD NO.  1

                              Operating  Hours
Month     Boiler                FGD Modules""                                            Comnents
                         12        34       56
Dec- n                                                              Initial operation (shakedown and debugging)  for part of the system commenced 1n
                                                                     December 1975.
Jan. 76
Feb. 76
Mar. 76
Apr' 76                 260°   290°   230°   110°     40°            The Installation began full  commercial operation In April.  The scrubbing system
                                                                     Is currently handling flue gas  at a  total equivalent capacity of 840 to 850-MW
                                                                     (gross).  The total  module by module operation  hours logged to-date are
                                                                     posted 1n the accompanying table.
                                                                                                                         PEDCo-ENVIKUNMtNTAL
                                                                        120

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME '

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES


  S02


 WATER MAKE UP


 SLUDGE DISPOSAL
  60
               •
 PHILADELPHIA ELECTRIC CO.

 EDOYSTONE NO 1A

 EODYSTONE PENNSYLVANIA

  120 MW

 COAL   2.5 PERCENT SULFUR

 UNITED ENGINEERS

 MAGNESIUM OXIDE SCRUBBING

 RETROFIT

  9/75

 OPERATIONAL
 UNIT COST
$17 MILLION CAPITAL
 OPERATIONAL
  EXPERIENCE
 THE SOS SCRUBBER HAS BEEN TEMPORARILY  SHUTDOWN BECAUSE THE  ACID  PLANT  RE-
 GENERATION FACILITY AT THE OLIN CHEMICAL  SULFURIC  ACID PLANT  IN  PAULSBORO
 NEW JERSEY HAS PERMANENTLY CEASED OPERATIONS.  CONSIDERATIONS  ARE NOW
 BEING blVCN TO THE RELOCATION OF THE REGENERATION  FACILITY. ONCE THIS  DE-
 CISION IS MADE A MINIMUM PERIOD OF SIX MONTHS  WILL BE REQUIRED TO RELO-
 CATE THE REGENERATION FACILITY. THE PARTICULATE SCRUBBERS ARE CONTINUING
 TO OPERATE. THE UTILITY IS STILL EXPERIENCING  PROBLEMS WITH THE  FANS,  RE-
 HEAT BURNERS,  DAMPERS, AND EXPANSION JOINTS.
                                                                                                       PEDCo-ENVIRONMENTAL
                                                            121

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  05/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
  83

 PUBLIC SERVICE CO OF COLORADO
 VALMONT NO. 5
 VALMONT COLORADO
   50 HW
 FUEL CHARACTERISTICS  COAL  0.72 PERCENT  SULFUR
 F60 VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP  DATE
 FGD STATUS
 EFFICIENCY,
 PARTICULATES
 UOP / PUB SERVICE OF COLORADO
 LIMESTONE SCRUBBING
 RETROFIT
 OPERATIONAL

 95 PERCENT
 S02

WATER MAKE UP

SLUDGE DISPOSAL

UNIT COST
85 PERCENT
CLOSED LOOP
UNSTABILIZED SLUDGE DISPOSED IN LINED POND
OPERATIONAL
 EXPERIENCE
KEFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
SYSTE.M HAS BEEN OPERATIONAL SINCE NOVEMBER l97«t. THE FGD SYSTEM CURRENTLY
OPERATIONAL AT THIS STATION IS AN EXPERIMENTAL UNIT, ORIGINALLY DESIGNED
BY UNIVERSAL OIL PRODUCTS FOR PARTICULATE REMOVAL ONLY. ONE OF THE TWO
PARALLEL SCRUBBING MODULES WAS CONVERTED TO LIMESTONE SCRUBBING FOR
EXPERIMENTAL PURPOSES ONLY.
                                                                                                    PEDCo-ENVIRONMENTAL
                                                           122

-------
                                                           BACKGROUND  INFORMATION
                                                                    ON
                                                                VALMONT  NO.  5

     THE VALMONT POWER STATION OF THE PUBLIC SERVICE COMPANY OF  COLORADO IS  LOCATED  IN VALMONT, COLORADO, APPROXIMATELY 20 MILES NORTH OF DENVER.
VALMONT'NO. s is A COAL-FIRED UNIT BURNS THAT FIRES GAS A FEW MONTHS DURING  THE YEAR.  THE COAL GENERALLY EMPLOYED FOR THIS UNIT is WYOMING ROSEBUD,
WHICH HAS AN AVERAGE GROSS HEATING VALUE OF 10,780 BUT/LB WITH ASH  CONTENT IN THE 6  TO 7 PERCENT RANGE AND SULFUR CONTENT LESS THAN 1 PERCENT.
     THE FGD SYSTEM BEING TESTED AT THIS STATION IS AN EXPERIMENTAL UNIT ORIGINALLY  DESIGNED BY UNIVERSAL OIL PRODUCTS FOR PARTICULATE REMOVAL ONLY.
THIS TCA UNIT CONSISTS OF TWO PARALLEL MODULES WITH A COMBINED CAPABILITY OF TREATING APPROXIMATELY 50 PERCENT OF THE TOTAL FLUE GAS LOAD OR THE
EQUIVALENT OF APPROXIMATELY 100 MW GENERATING CAPACITY (50 MW PER MODULE).   THIS SYSTEM WAS COMPLETED AND OPERATIONAL IN 1971 AND RAN UNTIL OCTOBER
1974.  PARTICULATE REMOVAL EFFICIENCY WAS MEASURED AT 95 PERCENT, S02  REMOVAL EFFICIENCY WAS 45 PERCENT, AND AVAILABILITY WAS APPROXIMATELY 70 PERCENT.
FREQUENT SCRUBBER OUTAGES WERE CAUSED PRIMARILY BY SUPERSATURATED CALCIUM SULFATE IN THE SCRUBBING LIQUOR.  TO MINIMIZE CLEANOUTS AND RECTIFY THE
SCALING PROBLEM, A pH CONTROL PROGRAM WAS IMPLEMENTED FOR ONE OF THE SCRUBBING MODULES WITH ADDITION OF LIMESTONE TO THE SCRUBBING LIQUOR.  THIS
MODIFICATION WAS EXPECTED TO MINIMIZE SCALING. DECREASE SCRUBBER OUTAGES FOR CLEANOUTS, AND INCREASE AVAILABILITY.  THE EXPECTED RESULTS DID NOT
MATERIALIZE.  SCALE BUILDUP CONTINUED AND AVAILABILITY DECREASED.  TESTS DURING THE  pH CONTROL PROGRAM SHOWED PARTICULATE REMOVAL EFFICIENCY AT 95
PERCENT.  S02 REMOVAL EFFICIENCY INCREASED TO 85 PERCENT, AND AVAILABILITY DROPPED TO 70 PERCENT.  THE UNSTABILIZED SLUDGE GENERATED DURING THIS
OPERATION WAS PUMPED TO A LINED POND.  THE OPERATIONAL DATA GENERATED  FROM THE LIMESTONE MODIFICATION PROGRAM ARE PRELIMINARY, BASED ON A 4.5-MONTH
TESTING PROGRAM.
                                                                                                                           PEDCo- ENVIRONMENTAL
                                                                       123

-------
                                                               VALMONT NO. 5
Month
Sep. 75
Oct. 7.5
Nov. 75
Dec. 75

Jan. 76
Feb. 76

Mar. 76
Apr. 76
Boiler
  0
  0
  0
  0

  0
  0
Operating Hours
        FGD System
            0
            0
            0
            0

            0
            0

            0
            0
  FGD System
Qperablllty (X)
      0
      0
      0
      0
      0
      0

      0
      0
                         Comments
This facility has been Inactive  since  September  1,  1976, because of a turbine gen-
erator failure.   The unit 1s  scheduled to  go on  line again In December 1975.
This unit Is still Inactive because  of a boiler  overhaul.  The scrubber/absorber
train Is available and will be coupled Into the  system when the boiler goes back
on-line.
The boiler overhaul has been  completed.  The unit Is available in the partlculate
removal mode only.  The utility  is suspending resumption of the limestone modification
operation for an Indefinite period.
The experimental limestone scrubbing program was Inactive during the report period.
Resumption of the program Is  considered Indefinite  at the present time.
                                                                                                                        PEDCo-ENVIRONMENTAL
                                                                      124

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGU VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCYi
  PARTICULATES


  S02
 90

RICKENBACKER AFB

RICKENBACKER

COLMBUS OHIO

  20 MW

COAL 3.6 PERCENT SULFUR

RESEARCH COTTRELL

LIME SCRUBBING

RETROFIT

 3/76

OPERATIONAL


99 PERCENT


90 PERCENT
 WATER HAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
THE SYSTEM SUPPLIER REPORTED THAT THE FGO SYSTEM BECAME OPERATIONAL  ON
MARCH 11. 1976. SYSTEM OPERABILITY MAS REPORTED TO BE 97 PERCENT FOR THE
DURATION OF THE MONTH. THE SYSTEM WAS BROUGHT DOWN ON APRIL It BECAUSE
OF PUMP PROBLEMS. A 1.5 WEEK OUTAGE RESULTED BECAUSE OF A SPARE PART
SHIPMENT. S02 INLET CONCENTRATIONS HAVE BEEN AT THE 1800 PPM LEVEL.  LIME
UTILIZATION HAS BEEN GOOD. THE S02 REMOVAL EFFICIENCY WAS REPORTED TO BE
AS HIGH AS 96 PERCENT.
                                                                                                     PEDCo-ENVIRONMENTAL
                                                            125

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  05/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR  RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCY!
 PARTICIPATES


 S02


 WATER MAKE UP


 SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
  98

 TENNESSEE VALLEY AUTHORITY

 SHAWNEE NO.IDA

 PADUCAH KENTUCKY

   10 MM

 COAL 2.9 PERCENT SULFUR

 UNIVERSAL OIL PRODUCTS

 LIME/LIMESTONE SCRUBBING

 RETROFIT

  */72

 OPERATIONAL
KEFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
TURBULENT CONTACT ABSORBER(TCA) LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN
OPERATIONAL SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA.
TVA IS THE CONSTRUCTOR AND FACILITY OPERATOR.  THE BECHTEL CORP. OF SAN
FRANCISCO IS THE MAJOR CONTRACTOR, TEST DIRECTOR, AND REPORT WRITER.
                                                           126
                                                                                                         PEDCo- ENVIRONMENTAL

-------
                   TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  05/76
 IDENTIFICATION NO,
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR  RETROFIT
 START UP  DATE
 FGD STATUS
 EFFICIENCY,
 PARTICULATES
 S02
  99
 TENNESSEE VALLEY AUTHORITY
 SHAUNEE N0.10B
 PAOUCAH KENTUCKY
   10  MW
 COAL  2.9 PERCENT SULFUR
 CHEMICO
 LIME/LIMESTONE SCRUBBING
 RETROFIT
  «»/72
 OPERATIONAL
WATER MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
REFEK TO BACKGKOUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
VENTURI/SPRAY TOWER LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN OPERATIONAL
SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA.  TVA IS THE
CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN FRANCISCO IS
THE MAJOR CONTRACTOR,TEST DIRECTORt AND REPORT WRITER.
                                                                                                        PEDCo-ENVIRONMENTAL
                                                           127

-------
                                                            BACKGROUND  INFORMATION
                                                                     ON
                                                        SHAWNEE NOS. IDA, 10B. AND IOC

      IN JUNE 1968,  THE EPA INITIATED A PROGRAM TO TEST  PROTOTYPE LIME AND LIMESTONE SYSTEMS FOR REMOVAL OF SULFUR DIOXIDE AND PARTICULATES FROM
 COAL-FIRED BOILER FLUE GASES.   THE  PROGRAM WAS CARRIED  OUT  IN A TEST FACILITY INCORPORATED INTO THE FLUE GAS DUCTWORK OF UNIT NO. 10, A COAL-FIRED BOILER
 AT THE TVA SHAWNEE  POWER STATION. PAOUCAH, KENTUCKY.    TVA  IS THE CONSTRUCTOR AND FACILITY OPERATOR; BECHTEL CORP. IS THE MAJOR CONTRACTOR. TEST
 DIRECTOR.  AND REPORT WRITER.
      THE TEST FACILITY CONSISTS OF  THREE PARALLEL SCRUBBER  SYSTEMS OF PROTOTYPE SIZE. TREATING PART OF THE FLUE GAS FROM THE BOILER.  EACH SCRUBBER
 TRAIN IS CAPABLE  OF TREATING APPROXIMATELY 30.000 ACFM  OR THE EQUIVALENT OF APPROXIMATELY 10 MW OF POWER PLANT GENERATING CAPACITY.
      THREE PARALLEL WET SCRUBBER SYSTEMS WERE  SELECTED  FOR  THE TEST PROJECT:  1) A VENTURI WITH A SPRAY TOWER AFTER ABSORBER; 2} A TURBULENT CONTACT
 ABSORBER (TCA) AND  3)  A MARBLE-BED  ABSORBER.   THE VENTURI SYSTEM. MANUFACTURED BY CHEMICAL CONSTRUCTION CO.. CONTAINS AN ADJUSTABLE THROAT THAT PERMITS
 CONTROL AND VARIATION  OF PRESSURE DROP  UNDEUl.A WIDE RANGE OF FLOW CONDITIONS.  THE TCA UNIT, MANUFACTURED BY UNIVERSAL OIL PRODUCTS, INCORPORATES
 A  FLUIDIZED BED OF  LOW DENSITY  PLASTIC  SPHERES THAT ARE FREE TO MOVE BETWEEN RETURNING GRIDS.   THE MARBLE-BED ABSORBER. SUPPLIED BY  COMBUSTION
 ENGINEERING CO.,  USES  A PACKING OF  3/4-INCH GLASS MARBLE SPHERES AND A TURBULENT LAYER OF LIQUID AND GAS ABOVE THE MARBLE LAYER TO ENHANCE MASS TRANSFER.
      IN JUNE  1974.  THE EPA  INITIATED A  3-YEAR  ADVANCED TEST PROGRAM AT THE  SHAWNEE FACILITY WITH THESE MAJOR GOALS:   (1)  CONTINUATION OF  LONG-TERM
 TESTING. EMPHASIZING RELIABLE OPERATION OF MIST ELIMINATION SYSTEMS AT INCREASED GAS VELOCITY.  (2) INVESTIGATION  OF  ADVANCED PROCESS AND  EQUIPMENT
 DESIGN  VARIATIONS FOR  IMPROVING SYSTEM RELIABILITY AND PROCESS ECONOMICS. AND (3) LONG-TERM RELIABILITY TESTING ON PROMISING PROCESS AND  EQUIPMENT  DESIGN
 VARIATIONS.
     THE TWO  PARALLEL  SCRUBBING SYSTEMS OPERATING DURING THE ADVANCED  PROGRAM ARE THE  VENTURI/SPRAY  TOWER SYSTEM  AND THE  TCA UNIT.   OPERATION OF THE
 MARBLE-BED ABSORBER UNIT HAS BEEN PERMANENTLY DISCONTINUED.
     EACH OF THE SCRUBBING SYSTEMS CONTAINS ITS OWN SLURRY HANDLING FACILITIES AND CAN TREAT APPROXIMATELY 30.000 ACFM  OF GAS AT 300°F CONTAINING
 1800 TO 4000 PPM OF SOg AND 2 TO 4 GRAINS/SCF OF PARTICULATES.   BOILER  NO.  1  NORMALLY  BURNS A HIGH-SULFUR BITUMINOUS  COAL.
     FROM JUNE 1974 TO JANUARY. 1976, MIST ELIMINATION AND LIMESTONE UTILIZATION TESTS WERE CONDUCTED AT  THE SHAWNEE  FACILITY.  DURING THIS TEST PERIOD
THE VENTURI/SPRAY TOWER SYSTEM WAS OPERATED ON BOTH LIME AND LIMESTONE  AND  THE TCA SYSTEM WITH LIMESTONE.  TESTING WAS  PERFORMED UNDER A CLOSED LIQUOR
LOOP OPERATION MODE.  DURING THIS PERIOD THE  SLURRY SOLIDS CONTAINED APPROXIMATELY 40  TO 50 WEIGHT PERCENT FLY ASH BECAUSE OF RELATIVELY HIGH GAS INLET
PARTICULATE LOADING.  THIS TESTING PROGRAM IS SCHEDULED TO RUN TILL  JUNE 1977.

                                                                                                                                PEDCo- ENVIRONMENTAL
                                                                                                                                              •
                                                                         128

-------
                                                          SHAHNEE NOS.  10A AND  10B

                              FGD.System Operating Hours
Test Run Period                  wK          TW                                              Comnents
Sep. 75                                                     This experimental EPA-funded  operation  Is  proceeding with the test program.  Two absorber
Oct. 75                                                     modules are currently operational  (10 MW each);  the marble-bed absorber Is still Inoperative
                                                            (since July 1973).   Current experiments are  related to mist eliminator section.
Nov. 75                                                     Recent testing at Shawnee has shown that the chevron mist eliminators In both the spray
Dec. 75                                                     tower and the TCA can be kept free of solids buildup at high alkali utilization (greater
                                                            than 90 percent) using  only intermittent washing with available raw water.  This high
                                                            utilization is normally achieved with lime;  it has been achieved with limestone at reduced
                                                            scrubber Inlet slurry pH (about 5.2) and with three effluent tanks In series to simulate a
                                                            plug-flow reactor.
                                                            Testing Is continuing to determine the  effects of process variables on mist eliminator per-
                                                            formance and on limestone utilization.   Future plans include:  (1) factorial testing
                                                            with lime and limestone to determine the effects of process variables on S02 removal and
                                                            (2) testing the oxidation of  sludge to  gypsum in the venturi/spray tower system using air
                                                            sparging of an acidified slurry bleed stream.
Jan. 75                                                     The advanced test program is  continuing.   Highlights of this prgram are as follows:
                                                            0    Evaluate scrubber  operabillty during  variable load operation.
                                                            0    Continue long-term reliability testing.
                                                            0    Investigate methods for  improving  waste solids separation.
                                                            0    Continue sludge oxidation and sludge  fixation study programs.
                                                            0    Evaluate system performance at reduced  fly ash loadings.
                                                            •    Determine the  practical  upper limits  of S02 removal efficiency.
                                                            0    Evaluate addition  of magnesium ion to the scrubbing slurry.


                                                                                                                     PEDCo- ENVIRONMENTAL
                                                                      129

-------
                                                    SHAWNEE  NOS.  10A AND 10B (Continued)

                              FGD System Operating  Hours
Test Run Period               ~K£      C-W'                                             Consents
                                                            •    Characterize all stack gas emission  components.
                                                            •    Evaluate materials of construction of all  scrubber and plant-related components.
                                                            0    Develop a computer program for design and  cost analysis of full-scale lime/limestone
                                                                systems.
Mar' 76                                                     Bechtel reported that the factorial  test  program, evaluating the performance of the lime/
Apr< 76                                                     limestone scrubbing systems with and without magnesium addition, has been completed.   Cur-
                                                           rently, testing Is  proceeding on the evaluation of system performance as a function of low
                                                           residence times (1.5 to 5.0 minutes) In the recycle tanks.  In addition, a fly ash-free
                                                           duct Is being  Installed at the  test  facility, thus enabling evaluation of system per-
                                                           formance In the absence of fly  ash.
                                                                                                                   PEDCo-ENVIRONMENTAL
                                                                       130

-------
              Table 4
NUMBER AND TOTAL MW OF F6D SYSTEMS
             131

-------
               TABLE t
NUMBER AND TOTAL MU OF FGO SYSTEMS
      STATUS




   OPERATIONAL

   UNDER CONSTRUCTION

   PLANNING
     CONTRACT AWARDED
NO. OF
UNITS
  27

  19
                                  16

     LETTER OF INTENT              6

     REQUESTING/EVALUATING  BIOS     5

     CONSIDERING  ONLY FGD SYSTEMS  31

     TOTAL                .       108
 MU
 7562.


 73«H».

 3356.

 2467.

1S003.

41275.
                                                    133
                                                                                              PEDCo- ENVIRONMENTAL

-------
             Table 5
SUMMARY OF FGD SYSTEMS BY COMPANY
            135

-------
                                         TABLE 5
                                SUMMARY OF FGD SYSTEMS BY COMPANY
         UTILITY

ALABAMA ELECTRIC COOP
ALLEGHENY POWER SYSTEM
ARIZONA ELECTRIC POWER COOP
ARIZONA PUBLIC SERVICE
BASIN ELECTRIC POWER COOP
BRAZOS ELECTRIC POWER COOP
CENTRAL ILLINOIS LIGHT CO.
CENTRAL ILLINOIS PUBLIC SERV
CINCINNATI GAS & ELECTRIC CO.
COLUrBUS X SOUTHERN OHIO ELEC.
COMMONWEALTH EDISON
DETROIT EDISON
DUQUESNE LIGHT
GENERAL MOTORS
GULF POWER CO.
INDIANAPOLIS POWER & LIGHT CO.
KANSAS CITY POWER & LIGHT
KANSAS POWER & LIGHT
KENTUCKY UTILITIES
KEY WEST'UTILITY BOARD
LOUISVILLE GAS & ELECTRIC
MINNHOTA POWER COOPERATIVE   ,
MONTANA POWER CO.            j
NEVADA POWER
NEW ENGLAND ELEC SYSTEM
NORTHERN INDIANA PUB SERVICE
NORTHERN STATES POWER CO.
PENNSYLVANIA POWER CO.
PHILADELPHIA ELECTRIC CO.
PUBLIC SERVICE CO OF COLORADO
PUBLIC SERVICE CO OF NEW MEX.
PUBLIC SERVICE INDIANA
RICKENBACKLR AFB
S. CAROLINA PUR SERV AUTHORITY
S. MISSISSIPPI ELEC PWR ASSOC
SOUTHERN CALIFORNIA EDISON
SOUTHERN ILLINOIS POWER COOP
SPRINGFIELD CITY UTILITIES
TENNESSEE VALLEY AUTHORITY
TEXAS UTILITIES Co.
UNITED POWER ASSOCIATION
UTAH POWER ft LIGHT CO.
TOTAL
OPERATIONAL
CONSTRUCTION

CONTRACT
AWARDED
NO.
2
2
2
5
5
1
3
1
2
4
2
1
2
1
3
'-•I
a
4
1
1
a
i
4
10
i
3
2
3
4
1
4
2
1
1
2
2
1
1
3
4
2
2
MW
450.
1250.
405.
1675.
2550.
too.
857.
600.
1100.
1550.
592.
180.
920.
32.
63.
530.
1060.
1885.
64.
37.
2213.
450.
2120.
3000.
650.
705.
1360.
2505.
846.
50.
1715.
1300.
20.
140.
360.
1410.
184.
200.
570.
2379.
1090.
815.
NO.
0
0
0
2
0
0
0
0
0
0
1
0
2
1
3
0
3
2
1
1
1
0
1
2
0
0
1
1
1
1
0
0
1
0
0
0
0
0
2
0
0
0
MW
0.
' 0.
0.
275.
0.
0.
0.
0.
0.
0.
167.
0.
920.
• 32.
63.
0.
1060.
525.
64.
37.
65.
0.
360.
250.
0.
0.
680.
835.
120.
50.
0.
0.
20.
0.
0.
0.
0.
0.
20.
0.
0.
0.
NO.
0
0
0
1
0
0
1
0
0
1
0
1
0
0
0
1
0
0
0
0
3
1
1
1
0
1
1
1
0
0
0
0
0
0
0
0
0
1
1
2
0
1
MW
0.
0.
0.
250.
0.
0.
100.
0.
0.
400.
0.
180.
0.
0.
0.
530.
0.
0.
0.
0.
7R6.
450.
360.
125.
0.
115.
6AO.
835.
0.
0.
0.
0.
0.
0.
0.
0.
0.
200.
550.
1586.
0.
HIS.
NO.
2
2
0
0
0
1
0
0
0
1
1
0
0
0
0
0
0
2
0
0
1
0
0
0
0
0
0
1
0
0
2
0
0
1
2 :
0 *
1
0
0
0
0
1
MW
450,
1250.
0.
0.
0.
400.
0.
0.
0.
400.
425.
0.
0.
0.
0.
0.
0.
1360.
0.
0.
425.
0.
0.
0.
0.
0.
0.
835.
0.
0.
715.
0.
0.
140.
360.
0.
184.
0.
0.
0.
0.
400.
LETTER OF REQUESTING/
INTENT
NO.
0
0
2
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
1
0
2
0
0
0
0
0
0
0
0
2
0
0
MW
0.
0.
405.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
125.
0.
0.
0.
0.
240.
0.
1000.
0.
0.
0.
0.
0.
0.
0.
0.
793.
0.
0.
EVAL.
NO.
0
0
0
0
0
0
0
1
1
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
2
0
BIOS
MW
0.
0.
0.
0.
0.
0.
0.
600.
500.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
277.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
1090.
0.
CONSIDERING
FGO
NO.
0
n
0
9
R
0
9
0
1
2
0
0
0
0
0
n
0
0
0
0
9
0
a
6
i
9
n
0
9
0
0
9
0
0
0
2
0
0
0
0
0
0
SYSTEMS
MW
0.
0.
0.
1350.
2550.
0.
757.
0.
600.
750.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
660.
0.
1400.
2500.
650.
590.
0.
0.
486.
0.
0.
1300.
0.
0.
0.
1410.
0.
0.
0.
0.
0.
0.
   TOTALS
                                   108  40482.   27   554S.   19   7562.   16   7344.    6   2563.
2467.   31  15003.
                                                                                                        PEDCo-ENVIRONMENTAL
                                                             137

-------
             Table 6
SUMMARY OF FGD SYSTEMS BY VENDOR
           139

-------
           TABLE 6
SUMMARY OF FGD SYSTEMS  BY VENDOR

TOTAL
MANUFACTURER/PROCESS
AOL/COMBUSTION EQUIP ASSOCIAiE
DOUBLE ALKALI
TOTAL, ADL/COMBUSTION EQUIP ASS
AMERICAN AIR FILTER
LIME SCRUBBING
TOTAL, AMERICAN AlR FILTER
BABCOCK & WILCOX
LIMESTONE SCRUBBING
TOTAL* BABCOCK & WILCOX
CHEMICO
LIME SCRUBBING
LIME/LIMESTONE SCRUBBING
TOTAL, CHEMICO
CHIYOOA INTERNATIONAL
THOROUGHBRED 101
TOTAL, CHIYOOA INTERNATIONAL
COMBUSTION ENGINEERING
LIME SCRUBBING
LIMESTONE INJECTION 8MET SCRUB
LIMESTONE SCRUBBING
TOTAL, COMBUSTION ENGINEERING
COMBUSTION EQUIP. ASSOCIATES
SODIUM CARBONATE SCRUBBING
TOTAL, COMBUSTION EQUIP. ASSOCI
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
TOTAL, DAVY POWERGAS/ALLIEO CHE
FOSTER WHEELER
ACTIVATED CARBON
TOTAL, FOSTER WHEELER
KOCH
DOUBLE ALKALI
TOTAL* KOCH
NO.

1
1

3
3

2
2

5
1
6

1
1

2
H
2
8

3
3

1
1

1
1

1
1
MU

20.
20.

667.
667.

987.
987.

3005.
10.
4fll5.
*
23.
23.

2>,8.
765.
1360.
2373.

375.
375.

115.
115.

20.
20.

32.
32.
OPERATIONAL CONSTRUCTION
NO.

1
1

1
1

2
2

3
1
t»

1
1

1
it
1
6

2
2

0
0

1
1

1
1
MU

20.
20.

61.
6H.

987.
987.

1755.
10.
1765.

23.
23.

65.
765.
680.
1510.

250.
250.

0.
0.

20.
20.

32.
92.
NO.

• o
0

2
2

0
0

2
0
2

0
0

1
0
1
2

1
1

1
1

0
0

0
0
MU

0.
0.

603.
603.

0.
0.

1250.
0.
1250.

0.
0.

183.
0.
680.
863.

125.
125.

115.
115.

0.
0.

0.
0.
                                     141
                                                                            PEDCo-ENVIRONMENTAL

-------
           TABLE 6
SUMMARY OF FGO SYSTEMS  BY VENDOR

TOTAL
MANUFACTURER/PROCESS
COMBUSTION EQUIP. ASSOCIATES
LIME/ALKALINE FLYASH SCRUBBING
TOTAL. COMBUSTION EQUIP. ASSOCZA
PEABODY ENGINEERING
LIMESTONE SCKUDBlNG
TOTAL, PEAPODY ENGINEERING
RESEARCH COTTRELL
LIME SCRUBBING
LIMESTONE SCRUBBING
TOTAL, RESEARCH COTTRELL
RILEY STOKER/ENVIRONEERING
LIMESTONE SCRUBBING
TOTAL, RILEY STOKER/ENVIRONEERI
SCE
LIME SCRUBBING
TOTAL, SCE
TENNESSEE VALLEY AUTHORITY
LIMESTONE SCRUBBING
TOTAL, TENNESSEE VALLEY AUTHOR!
UNITED ENGINEERS
MAGNESIUM OXIDE SCRUBBING
TOTAL, UNITED ENGINEERS
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
LIME/LlhESTUUE SCRUBBING
LIMESTONE SCRUBBING
TOTAL, UNIVERSAL OIL PRODUCTS
UOP / PUB SERVICE OF COLORADO
LIMESTONE SCRUBBING
TOTAL, UOP / PUB SERVICE OF COL
ZURN AIR SYSTEMS
LIMESTONE SCRUBBING
TOTALi ZURN AIR SYSTEMS
NO.

3
9

1
1

1
4
5

1
1

1
1

1
1

1
1

1
1
2
4

1
1

1
1
MW

1170.
1170.

180.
160.

20.
1951.
1971.

100.
1-4)0.

160.
160.

550.
550.

1*0.
120.

too.
10.
730.
1140.

50.
50.

37.
37.
OPERATIONAL CONSTRUCTION
NO.

1
1

0
0

1
1
2

0
0

1
1

0
0

1
1

0
1
0
1

1
1

1
1
MW

360.
360.

0.
0.

20.
115.
135.

0.
0.

160.
160.

0.
0.

120.
120.

0.
10.
0.
10.

50.
50.

37.
37.
NO.

'. 2
2

1
1

0
3
3

1
1

0
0

1
1

0
0

1
0
2
3

0
0

0
0
MW
•
810.
810.

180.
180.

0.
1836.
1636.

100.
100.

0.
0.

550.
550.

0.
0.

too.
0.
730.
1130.

0.
0.

0.
0.
      46 13105.
27  5543.
19  7562.
                                                                            PEDCo-ENVIRONMENTAL
                                    142

-------
                      Table 7



SUMMARY OF NEW AND RETROFIT FGD SYSTEMS BY PROCESS
                    143

-------
                                                    TABLE 7
                                  SUMMARY OF NEW AND RETROFIT FGD SYSTEMS BY PROCESS

                                          MW CAPACITYCNO. OF PLANTS)
             PROCESS

 LIME SCRUBBING
 LIME/ALKALINE  FLYASH SCRUBBING
  (PROCESS  NOT  SELECTED)

 LIME/LIMESTONE
  (PROCESS  NOT  SELECTED)

 LIME/LIMESTONE SCRUBBING
  (PROCESS  NOT  SELECTED)

 LIMESTONE  SCRUBBING
  SUBTOTAL - LIME/LIMESTONE
ACTIVATED CARBON
DOUBLE ALKALI
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
REGENERABLE NOT SELECTED
SODIUM CARBONATE SCRUBBING
THOROUGHBRED 101
WELLMAN LORD
WELLMAN LORD/ALLIED CHEMICAL
          TOTALS
  LIME/LIMESTONE  X  OF  TOTAL  MW
NEW OR OPERATIONAL
RETROFIT

N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
NO.
1
6
1
0
0
0
0
2
4
6
'4*5:
0
1
0
'• 2
0
1
0
0
0
0
0
2
0
1
0
0
0
0
6.
21.
100
81
MW
635
1229
360
0
0
0
0
20
1937
697
3132.
1946.
0
20
0
52
0
120
0
0
0
0
0
250
0
23
0
0
0
0
3132.
CONSTRUCTION CONTRACT
AWARDED
NO.
3
3
1
1
0
0
0
0
7
2
11.
6.
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
1
12.
7.
MW
1660
776
450
360
0
0
0
0
3346
730
5456.
1866.
0
0
0
0
0
0
0
0
0
0
125
0
0
0
0
0
0
115
5561.
1981.
NO.
5
0
0
0
0
0
0
0
10
1
is.
1.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1
1
16.
2.
98
94
1/IC
MW
2475
0
0
0
0
0
0
0
3729
425
6204.
425.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
375
340
6579.
769.
94
56
LETTER OF
INTENT
NO.
0
0
0
0
0
0
0
0
4
0
4.
0.
0
0
0
0
0
1
0
0
0
0
1
0
0
0
2
0
0
0
7.
1.

MW
0
0
0
0
0
0
0
0
1196
0
1198.
0.
0
0
0
0
0
240
0
0
0
0
125
0
0
0
1000
0
0
0
2323.
240.
52
0^
REQUESTING/ CONSIOERINfi
EVAL. BIDS FGO SYSTEM
NO.
0
0
0
0
2
0
0
0
0
0
2.
0.
.0
0
0
0
0
0
2
1
0
0
0
0
0
0
0
0
0
0
i!

MW
0
0
0
0
1090
0
0
0
0
0
1090.
0.
0
0
0
0
0
0
1100
277
0
0
0
0
0
0
0
0
0
0
2190.
277.
50
0
NO.
0
2
0
0
0
0
• 0
2
1
0
1.
4.
0
0
0
0
0
2
18
5
0
1
0
0
o
0
0
0
0
0
19.
12.

MW
0
660
0
0
0
0
o
1410
400
0
400.
2070.
0
0
0
0
o
486
9100
2297
0
650
0
0
0
0
0
0
0
0
9500.
5503.
4
38
• TOTAL NO.
OF PLANTS
NO. MW
9 4970
11 2665
2 610
1 360
2 1090
0 0
0 0
4 1430
26 10610
9 1852
39. 17460.
25. . 6307.
0 0
1 20
0 0
2 52
0 0
4 846
20 10200
6 2574
0 0
1 650
2 250
2 250
0 0
1 23
2 1000
0 0
1 375
2 455
64. 29305.
44. 11177.
60
56

-------
                             Table 8
SUMMARY OF OPERATING FGD SYSTEMS BY PROCESS AND GENERATING UNITS
                             147

-------
                       TABLE B
           SUMMARY OF  OPERATING FGD SYSTEMS BY
           PROCESS AND GENERATING UNITS AS OF 05/76
  PROCESS/GENERATING UNITS         FGO/MW  STARTUP  EXPERIENCED.)



        ACTIVATED CARBON

SCHOLZ NO. 2A                         20     2-76               3

                                     20.                        3


        DOUBLE ALKALI

CHEVROLET PARMA 123*4             32     3-7«f              26
SCHOLZ NO. 1A                         20     2-75              15

                                     52.                     " 41


        LIME SCRUBBING              '-}.

BRUCE MANSFIELD NO* 1                835     4-76               1
ELRAMA                       .        510    10-75               7
FOUR CORNERS NO. 5A                 -160     2-76               3
GREEN RIVER   UNITS 1 AND 2           64     9-75               8
PADDYS RUN NO 6                       65     4-73              37
PHILLIPS                             410     7-73              34
RICKENBACKER                          20     3-76               2

                                   2064.                       92


        LIME/ALKALINE FLYASH SCRUBBING

COLSTRIP NO 1               .         360    10-75               7

                                    360.                        7


        LIME/LIMESTONE SCRUBBING

SHAWNEE N0.10A                        10     4-72              49
SHAWNEE N0.10B                        10     4-72              49

                                     20.                       96
                                                               149
                                                                                                      PEDCo-ENVIRONMENUl

-------
                      TABLE 6
           SUMMARY OF OPERATING FGD SYSTEMS BY
           PROCESS AND GENERATING UNITS AS OF 05/76
  PROCESS/GENERATING UNITS         FGO/MW  STARTUP  EXPERIENCED.)
        LIMESTONE SCRUBBING

HAWTHORN NO 3                        140    11-72              42
HAWTHORN NO 4                        100     6-72              45
LAWRENCE NO 4                        125    12-68              69
LAWRENCE NO- 5                        400    11-71              54
CHOLLA NO 1                          115    10-73              31
LA CYGNE NO 1                        620     2-73              39
SHERBURNE NO 1                       660     3-76               2
STOCK ISLAND PLANT                    37    10-72              43
VALMONT NO. 5                         50    10-74              19
WILL COUNTY NO 1                     167     2-72              51
                                   2634.                      415


        MAGNESIUM OXIDE SCRUBBING

EDOYSTONE NO 1A                      120     9-75               6

                                    120.                        6


        SODIUM CARBONATE SCRUBBING

REID GARDNER NO 1                    125     4-74              25
REID GARDNER NO 2                    125     4-74              25
                                    250.                       50


        THOROUGHBRED 101

SCHOLZ NOS. IB I 2B                   23     3-75              14
                                  • ••»•••                     ••»»
                                     23.                       14
                                                                                                       PEDCo- ENVIRONMENTAL'
                                                             150

-------
                             Table 9



SUMMARY OF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL FGD SYSTEMS
                              151

-------
                            TABLE 9
        SUMMARY OF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL FGD SYSTEMS AS OF  05/76



PROCESS/GENERATING UNIT             "SLUDGE"      —SLUDGE—      —POND—      	POND--
                                    STABILIZED    UNSTABILIZED        LINED          UNLZNEO
DOUBLE ALKALI
CHEVROLET PARMA 1234*
SCHOLZ NO. 1A
TOTAL

32 32
20 20
0. 52. 20. 32.
      LIME SCRUBBING

BRUCE MANSFIELD NO. 1                      835                                             635
ELRAMA                                     510                                             510
GREEN RIVER   UNITS i AND 2                 6*                                              '*
PADDYS RUN NO 6                                             *5                              65
PHILLIPS
      TOTAL                               1619.             65,              0.           188*.


     ' LIME/ALKALINE FLYASH SCRUBBING

COLSTRIP NO 1                                              360                             360

      TOTAL                                  0.            360.              0.            360.


      LIMESTONE SCRUBBING

HAWTHORN NO 3                                              1"*0                             1"»0
HAWTHORN NO "»                                              100                             100
LAWRENCE NO t                                              125                             125
LAWRENCE NO 5                                              *»00                             "*00
CHOLLA NO 1                                                115                             115
LA CYGNE NO 1                                              820                             820
SHERBURNL NO 1                                                                             6°0
STOCK ISLAND PLANT                                                                          37
VALMONT NO. 5                                               50              50
WILL COUNTY NO 1                           167                             167

      TOTAL                                167.           1750.            217.           2*17.


      SODIUM CARBONATE SCRUBBING
                                                                                                      PEDCo-ENVIRONMENTAL
                                                        153

-------
                            TABLE 9
        SUMMARY OF SLUDGE DISPOSAL PRACTICES  FOR  OPERATIONAL  F60  SYSTEMS AS OF  05/76
PROCESS/GENERATING UNIT
—SLUDGE-
STABILIZED
  —SLUDGE—
UNSTABILIZED
—POND-
  LINED
—POND—
 UNLINED
REID GARDNER NO 1
REID GARDNER NO 2

      TOTAL
                       125
                       125

                       250.
                                         129
                                         125

                                         250 e
      THOROUGHBRED 101

SCHOLZ NOS. IB * 2B

      TOTAL
                        23

                        29.
                          23

                          23.
                         0.
                                                                                                      PEDCo- ENVIRONMENTAL
                                                         154

-------
                       Table 10
SUMMARY OF F6D SYSTEMS BY PROCESS AND REGULATORY CLASS
                         155

-------
                                                   TABLC 10
                                 SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY  CLASS

                                         MM CAPACXTYtNO. OF PLANTS)
            PROCESS

Lint SCRUBBING
LIME/ALKALINE FLYASH SCRUBBING
 (PROCESS NOT SELECTED)
LIME/LIMESTONE
 (PROCESS NOT SELECTED)
LIME/LIMESTONE SCRUBBING
  (PROCESS NOT SELECTED)
LIMESTONE SCRUBBING
  SUBTOTAL - LIME/LIMESTONE

REGULATORY OPERATIONAL CONSTRUCTION
CLASS
NO. MW NO. MU
A o o 2 640
B 4 1915 2 1235
C 2 129 2 361

E
:NG A
B
C
o
E
A
B
C
0
E
A
B
C
0
E
A
B
C
0
E
A
8
C
D
E
o
1
0
o
1
o
0
o
o
o
o
:,V.O
"o
o
2
0
0
0
1*
3
2
1
0.
a.
a.
2.
2.
0
20
0
0
360
0
0
0
0
0
0
0
o
0
20
0
0
0
1035
1024
525
50
0.
2950.
1533.
525.
70.
0
0
1
1
0
0
0
0
0
0
0
0
0
0
0
0
0
5
2
1
0
1
a.
5.
3.
0.
1.
0
0
360
450
0
0
0
0
0
0
0
0
0
0
0
0
0
2416
930
550
0
180
3616.
2615.
911.
0.
160.
CONTRACT
AWARDED
NO. MW
4 2075
1 400
0 0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
6
3
1
0
1
10.
4.
1.
0.
1.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1134
2195
425
0
400
3209.
2595.
425.
0.
400.
LETTER OF REQUESTING/
INTENT EVAL. BIDS
NO. MW NO. MW
00 00
00 00
00 00
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
2
2
0
0
0
2.
2.
0.
0.
Q.
0
0
0
0
0
0
0
0
0
0
0
0
C
0
0
0
0
793
405
0
0
0
793.
405.
0.
0.
0.
0
0
0
0
0
0
0
2
0
0
0
0
0
0
0
0
0
0
0
0
0
0
2.
0.
0.
0.
0.
0
0
0
0
0
0
0
1090
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1090.
0.
0.
0.
0.
CONSIDERING
FGO SYSTEM
NO. MW
0 0
0 0
2 660
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
2
1
0
0
0
0
1.
0.
2.
0.
2.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1410
400
0
0
0
0
400.
0.
660.
0.
1410.
TOTAL NO.
OF PLANTS
NO. MU
6 2915
7 3550
6 1150
0
1
1
1
1
0
0
2
0
0
0
0
0
0
2
0
2
14
11
5
2
3
23.
19.
14.
2.
6.
u
20
360
450
360
0
0
1090
0
0
0
0
0
0
20
0
1410
4743
4565
1999
525
630
9106.
8565.
3529.
525.
2060.
   B*   BOILER  SUBJECTCTODSTATEESTANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
   ?!   BOILER  SUBJECT  TO  STATE STANDARD THAT IS E8UAL TO OR LESS STRINGENT THAN NSPS
   D.   OTHER
   E.   REGULATORY  CLASS UNKNOWN
PEDCo- ENVIRONMENTAL
                                                              157

-------
                                                   TABLE 10
                                 SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY CLASS

                                         HW CAPACITY(NO. OF PLANTSI
            PROCESS

ACTIVATED CARBON
DOUBLE ALKALI
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
REGENERABLE NOT SELECTED
                            REGULATORY OPERATIONAL
CLASS

   A
   B
   C
   D
   E

   A
   B
   C
   D
   E

   A
   B
   C
   0
   E

   A
   B
   C
   D
   E

   A
   B
   C
   D
   E
NOi
 0
 0
 1
 0
 0

 0
 1
 1
 0
 0

 0
 1
 0
 0
 0

 0
 0
 0
 0
 0

 0
 0
 0
 0
 0
  MU
  0
  0
 20
  0
  0

  0
 32
 20
  0
  0

  0
120
  0
  0
  0

  0
  0
  0
  0
  0

  0
  0
  0
  0
  0
NO.
 0
 0
 0
 0
 0

 0
 0
 0
 0
 0

 0
 0
 c.
 0
 0

 0
 0
 0
 0
 0

 0
 0
 0
 0
 0
flON CONTRACT
AWARDED
MW
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
MU
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
LETTER OF REQUESTING/
INTENT
NO.
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
MW
0
0
0
0
0
0
0
0
0
0
0
240
0
0
0
0
0
0
0
0
0
0
0
0
0
EVAL. BIOS
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1
0
1
1
0
0
0
0
0
0
MW
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
600
0
277
500
0
0
0
0
0
0
CONSIDERING
FGD SYSTEM
NO.
0
0
0
0
0
0
0
0
0
0
0
0
2
0
0
5
15
3
0
0
0
0
1
0
0
MW
0
0
0
0
0
0
0
0
0
0
0
0
486
0
0
3300
7150
9«f7
0
0
0
0
650
0
0
• TOTAL NO.
OF PLANTS

NO.
0
0
1
0
0
0
1
1
0
0
0
2
2
0
0
6
15
<*
1
0
0
0
1
0
0

MW
0
0
20
0
0
0
32
20
0
0
0
360
486
0
0
3900
7150
1224
500
0
0
0
650
0
0
  A.   BOILER CONSTRUCTED SUBJECT  TO  FEDERAL  NSPS
  B.   BOILER SUBJECT TO STATE STANDARD  THAT  IS  MORE  STRINGENT  THAN  THE FEDERAL NSPS
  C.   BOILER SUBJECT TO STATE STANDARD  THAT  IS  EQUAL TO  OR  LESS  STRINGENT THAN NSPS
  D.   OTHER
  E.   REGULATORY  CLASS  UNKNOWN
                                                            158
                                                                                                          PEDCo-ENVIRONMENTAL-

-------
                                                   TABLE 10
                                 SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY  CLASS

                                         MU CAPACITYINO. OF PLANTS)
            PROCESS

SODIUM CARBONATE SCRUBBING
THOROUGHBRED 101
WELLMAN LORD
WELLMAN LORD/ALLIED CHEMICAL
          TOTALS
  LIME/STONE » OF TOTAL MW
REGULATORY OPERATIONAL
CLASS
NO. MU
A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
0
2
0
0
0
0
0
1
0
0
0
0
0
0
:JV. °
'0
0
0
0
0
0
12
11
2
2





0
250
0
0
0
0
0
23
0
0
0
0
0
0
0
0
0
0
0
0
0.
. 3352.
. 1596.
525.
70.
0
68
96
100
100
CONSTRUCTION
NO. MU
0 0
1 125
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 . 0
0 0
0 0
0 0
0 0
1 115
0 0
0 0
8. 3616.
6. 2740.
4. 1026.
0. 0.
1. 180.
100
95
69
0
100
CONTRACT
AWARDED
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
2
0
0
0
10.
6.
1.
0.
1.





MU
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
715
0
0
0
3209.
3310.
425.
0.
400.
100
78
100
0
100
LETTER OF REQUESTING/
INTENT EVAL. BIDS
NO.
0
1
0
0
0
0
0
0
0
0
0
2
0
0
0
0
0
0
0
0
2.
6.
0.
0.
0.




e
MU
0
125
0
0
0
0
0
0
0
0
0
1000
0
0
0
0
0
0
0
0
793.
1770.
0.
0.
0.
100
23
0
0
0
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
3.
0.
1.
1.
0.





MW
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1690.
0.
277.
500.
0.
64
0
0
0
0
CONSIDERING
FGO SYSTEM
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
6.
15.
6.
0.
2.





MU
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
3700.
7150.
2743.
0.
1410.
11
0
24
0
100
TOTAL NO.
OF PLANTS
NO.
0
4
0
0
0
0
0
1
0
0
0
2
0
0
0
0
2
1
0
0
29.
45.
25.
3.
6.





MU
0
500
0
0
0
0
0
23
0
0
0
1000
0
0
0
0
715
115
0
0
13008,
18322,
6067,
1025,
2060,
70
47
56
51
100
  A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
  B.  BOILER SUBJECT To STATE STANDARD THAT IS MORE  STRINGENT  THAN  THE FEDERAL NSPS
  C.  BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO  OR  LESS  STRINGENT THAN NSPS
  D.  OTHER
  E.  REGULATORY CLASS UNKNOWN
                                                            lea
                                                                                                            PEDCo-ENVIRONMENTAL

-------
             Table 11
SUMMARY OF OPERATIONAL FGD SYSTEMS
                161

-------
                      TABLE 11
            SUMMARY OF OPERATIONAL FGD SYSTEMS AS OF 05/76
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  PROCESS/VENDOR
RETROFIT   UNIT (MM)
                                                                                       FUEL CHARACTERISTICS
                                                                                     .HO/YR
ARIZONA PUBLIC SERVICE
CHOLLA NO 1

ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 5A

COMMONWEALTH EDISON
WILL COUNTY NO 1

DUQUESNE LIGHT
PHILLIPS

OUQUESNE LIGHT
ELRAMA

GENERAL MOTORS
CHEVROLET PARMA 1 2 3 * "»

GULF POWER CO.
SCHOLZ NO. 1A

GULF POWER CO.
SCHOLZ NO. 2A

GULF POWER CO.
SCHOLZ NOS. IB ft 28

KANSAS CITY POWER ft LIGHT
LA CYGNE NO 1

KANSAS CITY POWER ft LIGHT
HAWTHORN NO t

KANSAS CITY POWER ft LIGHT
HAWTHORN NO 3

KANSAS.POWER ft LIGHT
LAWRENCE NO t

KANSAS POWER ft LIGHT
LAWRENCE NO 5

KENTUCKY UTILITIES
GREEN RIVER   UNITS 1 AND 2
R
R
R
R
R
R
*;
R
R
N
R
R
R
N
R
115
160
167
mo
510
32
20
20
23
820
100
110
125
400
6*
                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      SCE
                      LIME SCRUBBING

                      BABCOCK ft WILCOX
                      LIMESTONE SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      KOCH
                      DOUBLE ALKALI

                      AOL/COMBUSTION EQUIP ASSOCIATE
                      DOUBLE ALKALI

                      FOSTER WHEELER
                      ACTIVATED CARBON

                      CHIYODA INTERNATIONAL
                      THOROUGHBRED 101

                      BABCOCK ft WILCOX
                      LIMESTONE SCRUBBING

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION «WET SCRUB

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION &WET SCRUB

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION ftUET«SCRUB
                                               »
                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION ftWCT SCRUB

                      AMERICAN AIR FILTER
                      LIME SCRUBBING
                                                                                      COAL   O.Ht-1 PERCENT SuLFuR    10/73
COALi 0.7 PERCENT SULFUR
 2/76
COAL - 9463 BTUt   2.IK SULFUR   2/72
COAL   1.0- 2.8 PERCENT SULFUR   7/73
COAL  i.o • 2.a PERCENT SULFUR  10/75
COAL   2.5 PERCENT SULFUR
COAL   3.0 PERCENT SULFUR
COAL   3.0 PERCENT SULFUR
 3/74
 2/75
 2/76
COAL 5.0 PERCENT SULFUR (MAX)    3/75
COAL 5*0 PERCENT SULFUR
 2/73
COAL   0.6- s.o PERCENT SULFUR   8/72
COAL   0.6- s.o PERCENT SULFUR  11/72
COAL 0.5 PERCENT SULFUR
COAL 0.5 PERCENT SULFUR
COAL  3.8 PERCENT SULFUR
12/68
11/71
 9/75
                                                                                                           PEDCo-ENVIRONMENTAL
                                                             163

-------
                       TABLE 11
             SUMMARY  OF OPERATIONAL FGO SYSTEMS  AS OF  05/76
        UTILITY  COMPANY
         POWER STATION
 NEW OR   SIZE OF FGO  PROCESS/VENDOR
RETROFIT   UNIT (MW)
                                  FUEL CHARACTERISTICS
                                 MO/YR
 KEY  WEST  UTILITY  BOARD
 STOCK  ISLAND  PLANT

 LOUISVILLE  GAS  ft  ELECTRIC
 PADDYS RUN  NO 6

 MONTANA POWER CO.
 COLSTRIP  NO 1

 NEVADA POWER
 REID GARDNER  NO 2

 NEVADA POWER
 REID GARDNER  NO 1

 NORTHERN  STATES POWER CO.
 SHERE3URNE NO  1

 PENNSYLVANIA  POWER CO.
 BRUCE  MANSFIELD NQ. 1

 PHILADELPHIA  ELECTRIC CO.
 EODYSTONE NO  1A

 PUOLIC  SERVICE  CO OF COLORADO
 VALMONT NO. 5

 RICKENBACKER  AFB
 RICKENBACKER

 TENNESSEE VALLEY AUTHORITY
 SHAWNEE NO.IDA

TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10B
N
R
N
R
R
N
•"*
R
R
R
R
R
37
65
360
125
125
660
635
120
50
20
10
10
 ZURN AIR SYSTEMS
 LIMESTONE SCRUBBING

 COMBUSTION ENGINEERING
 LIME SCRUBBING

COMBUSTION EQUIP. ASSOCIATES
 LIME/ALKALINE FLYASH SCRUBBING

 COMBUSTION EQUIP. ASSOCIATES
 SODIUM CARBONATE SCRUBBING

 COMBUSTION EQUIP. ASSOCIATES
 SODIUM CARBONATE SCRUBBING

 COMBUSTION ENGINEERING
 LIMESTONE SCRUBBING

 CHEMICO
 LIME SCRUBBING

 UNITED ENGINEERS
 MAGNESIUM OXIDE  SCRUBBING

 UOP  / PUB SERVICE OF COLORADO
 LIMESTONE SCRUBBING

 RESEARCH COTTRELL
 LIME SCRUBBING

 UNIVERSAL OIL  PRODUCTS
 LIME/LIMESTONE SCRUBBING

 CHEMICO
 LIME/LIMESTONE SCRUBBING
 OIL     2.i»  PERCENT  SULFUR        10/72
COAL  3.5-
-------
                Table 12



SUMMARY OF FGD SYSTEMS UNDER CONSTRUCTION
                    165

-------
                      TABLE  12
            SUMMARY OF FGD SYSTEMS UNDER CONSTRUCTION AS OF 05/76
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  PROCESS/VENDOR
RETROFIT   UNIT (MW)
  FUEL  CHARACTERISTICS
                               •MO/YR
ARIZONA PUBLIC SERVICE
CHOLLA NO 2
CENTRAL ILLINOIS LIGHT CO.
OUCK CREEK NO.l

COLUMBUS ft SOUTHERN OHIO ELEC.
COMESVILLE NO 5
DETROIT EDISON
ST.CLAIR NO 6
INDIANAPOLIS POWER & LIGHT CO.
PETERSBURG NO 3
LOUISVILLE GAS & ELECTRIC
MILL CREEK NO 3
LOUISVILLE GAS 8 ELECTRIC
CANE RUN NO 5
LOUISVILLE GAS 8 ELECTRIC
CANE RUN NO H

MINNKOTA POWER COOPERATIVE
MILTON R. YOUNG NO. 2
MONTANA POWER CO.
COLSTRIP NO 2
NEVADA POWER
REID GARDNER NO 3
NORTHERN INDIANA PUB SERVICE
MITCHELL NO 11
NORTHERN STATES POWER CO.
SHERBURNE NO 2
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 2
SPRINGFIELD CITY UTILITIES
SOUTHWEST NOt 1
N
N
N
R
N
N
RJr.
1
R
N,

N
R
N
N
N
250
100
1*00
180
530
425
183

178
450
360
125
115
680
835
200
                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      RILEY STOKER/ENVIRONEERING
                      LIMESTONE SCRUBBING

                      UNIVERSAL OIL PRODUCTS
                      LIME SCRUBBING

                      PEABODY ENGINEERING
                      LIMESTONE SCRUBBING

                      UNIVERSAL OIL PRODUCTS
                      LIMESTONE SCRUBBING

                      AMERICAN AIR FILTER
                      LIME SCRUBBING

                      COMBUSTION ENGINEERING
                      LIME SCRUBBING

                      AMERICAN AIR FILTER
                      LIME SCRUBBING

                     COMBUSTION EQUIP.  ASSOCIATES
                      LIME/ALKALINE FLYASH SCRUBBING

                     COMBUSTION EQUIP.  ASSOCIATES
                      LIME/ALKALINE FLYASH SCRUBBING

                      COMBUSTION EQUIP.  ASSOCIATES
                      SODIUM CARBONATE  SCRUBBING

                      DAVY POWERGAS/ALLIED CHEMICAL
                      WELLMAN LORD/ALLIED CHEMICAL

                      COMBUSTION ENGINEERING
                      LIMESTONE SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      UNIVERSAL OIL PRODUCTS
                      LIMESTONE SCRUBBING
COAL    0.44-1 PERCENT SULFUR
COAL 2.5-3.0 PERCENT SULFUR
COAL  4.5 - 4.9 PERCENT SULFUR
COAL   3.7 PERCENT SULFUR
COAL  3.0-3.5 PERCENT SULFUR
COAL   3.5-
                PERCENT SULFUR
COAL   3.5-4.05 PERCENT SULFUR
COAL   s.5-4.05 PERCENT SULFUR
LIGNITE - 6.500 BTU. 0.7* S
COAL   0.8 PERCENT SULFUR
COAL   o.s- i.o PERCENT SULFUR
COAL   3.2- 3.5 PERCENT SULFUR
COAL 0.8 PERCENT SULFUR
COAL   4.3 PERCENT SULFUR
COAL 3.5 PERCENT SULFUR
 6/77


 6/76


 6/76


 5/76


 9/77


 7/77


12/77


 6/76


 8/77


 7/76


 6/76


 5/76


 5/77


 4/77


 8/76
                                                              167
                                                                                                      PEDCo-ENVIRONMENTAL

-------
                      TABLE 12
            SUMMARY OF F60 SYSTEMS UNDER CONSTRUCTION AS OF  05/76
       UTILITY COMPANY
        POWER STATION
TENNESSLE VALLEY AUTHORITY
WIDOWS CREEK NO 8

TEXAS UTILITIES CO.
MARTIN LAKE NO. 1

TEXAS UTILITIES CO.
MARTIN LAKE NO. 2

UTAH POWER ft LIGHT CO.
HUNTIN6TON NO.l
 NEW OR   SIZE OF FGD  PROCESS/VENDOR
RETROFIT   UNIT (MW)
    R


    N
550      TENNESSEE VALLEY AUTHORITY
         LIMESTONE SCRUBBING

795      RESEARCH COTTRELL
         LIMESTONE SCRUBBING

799      RESEARCH COTTRELL
         LIMESTONE SCRUBBING

415      CHEMICO
         LIME SCRUBBING
 FUEL CHARACTERISTICS           MO/YR



COAL   3.7 PERCENT SULFUR        2/77


COAL   1.0 PERCENT SULFUR        1/77


COAL   1.0 PERCENT SULFUR       10/77


COAL  0.5 PERCENT SULFUR         6/77
                                                               168
                                                                                                        PEDCo-ENVIRONMENJAl

-------
           Table 13
SUMMARY OF PLANNED FGD SYSTEMS
              169

-------
                   TABLE 13
            SUMMARY OF PLANNED FGD SYSTEMS AS OF 05/76
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGO  VENDOR/PROCESS*
RETROFIT   UNIT 
-------
            TABLE 13
     SUMMARY OF PLANNED FGD SYSTEMS AS OF 05/76
UTILITY COMPANY
 POWER STATION
 NEW OR
RETROFIT
                                          SIZE OF FGD
                                           UNIT (MW)
VENDOR/PROCESS
FUEL CHARACTERISTICS
                                                               MO/YR
PUBLIC SERVICE CO OF NEW MEX.       R
SAN JUAN NO. 2

SOUTHERN ILLINOIS POWER COOP        N
SOUTHERN* ILLINOIS POWER PT. 4

S. MISSISSIPPI ELEC PWR ASSOC       N
R.D. MORROW NO.l
             340      DAVY POWERGAS/ALLIED CHEMICAL
                      WELLMAN LORD/ALLIED CHEMICAL
                                               BABCOCK 1  WILCOX
                                               LIMESTONE  SCRUBBING
             180      RILEY STOKER/ENVIRONEERING
                      LIMESTONE SCRUBBING
                                                                               COAL    O.A  PERCENT  SULFUR         7/77
                                                      COAL                              1/76
                                                                              COAL  1 PERCENT SULFUR            11/77
            LETTER OF INTENT SIGNED

NEVADA POWER
REID GARDNER NO 4

ARIZONA ELECTRIC POWER COOP
APACHE NO 3

PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO IB

ARIZONA ELECTRIC POWER COOP
APACHE NO 2

TEXAS UTILITIES Co.
MARTIN LAKE NO. 3

TEXAS UTILITIES co.
MARTIN LAKE NO. 4

PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. 3

PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. ^
            REQUESTING/EVALUATING BIDS

CINCINNATI GAS 8 ELECTRIC CO.       N
MIAMI FORT NO 8

LOUISVILLE GAS ft ELECTRIC           R
CANE RUN NO 6

CENTRAL ILLINOIS PUBLIC SERV        N
NEWTON NO.l

UNITED POWER ASSOCIATION            N
COAL CREEK NO. 2
125
205
240
200
793
0
500
500
500
277
600
545
COMBUSTION EQUIP. ASSOCIA
SODIUM CARBONATE SCRUBBINl
RESEARCH COTTRELL
LIMESTONE SCRUBBING
UNITED ENGINEERS
MAGNESIUM OXIDE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
DAVY POWERGAS
WELLMAN LORD
DAVY POWERGAS
WELLMAN LORD
NOT SELECTED
NOT SELECTED
NOT SELECTTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
                                                                              COAL    0-5-  1.0 PERCENT SULFUR    O/  0
                                                                              COAL    0.5- o.s PERCENT SULFUR   6/79
                                                                              COAL 2.5 PERCENT SULFUR
                                                                              COAL 1.0 PERCENT SULFUR
                                                                              COAL 1.0 PERCENT SULFUR
                                                                              COAL 0.8 PERCENT SULFUR
                                                                              COAL 0.8 PERCENT SULFUR
                                                                              COAL 1.3 PERCENT SULFUR
                                                                                      10/78
                                                                              COAL  0.5- 0.6 PERCENT SULFUR    6/76
                                                                                     12/76


                                                                                     12/79


                                                                                      5/79


                                                                                      5/61





                                                                                      1/78
                                                                              COAL   3.5- "».o PERCENT SULFUR   9/76
                                                                              COAL 2.8-3.2 PERCENT SULFUR
                                                                                     12/77
                                              LIME/LIMESTONE
                                                                              LIGNITE - 0.63 PERCENT SULFUR   11/79
                                                        172
                                                                                                PEDCo-ENVIRONMENTAL

-------
                   TABLE 13
            SUMMARY OF PLANNED FGD SYSTEMS AS OF 05/76
       UTILITY COMPANY
        POWER STATION
UNITED POWER ASSOCIATION
COAL CREEK NO. 1
 NEW OR   SIZE OF F6D  VENDOR/PROCESS
RETROFIT   UNIT 
-------
                   TABLE 13
            SUMMARY OF PLANNED F60 SYSTEMS AS OF OS/76
       UTILITY COMPANY
        POWEH STATION
 NEW OR   SIZE OF F6D  VENDOR/PROCESS
RETROFIT   UNIT 
-------
                   TABLE IS
            SUMMARY OF PLANNED FGD SYSTEMS AS OF OS/76
       UTILITY COMPANY
        POUCH STATION
 NEW OR .  SIZE OF F60  VENDOR/PROCESS
RETROFIT   UNIT (MU)
 FUEL CHARACTERISTICS
MO/YR
PUBLIC SERVICE INDIANA
GIBSON NO. 3

PUBLIC SERVICE INDIANA
GIBSON NO. H
             650      NOT SELECTED
                      NOT SELECTED

             650      NOT SELECTED
                      NOT SELECTED
COAL 3.3 PERCENT SULFUR
COAL 3.3 PERCENT SULFUR
 0/76
 0/79
                                                              175
                                                                       PEDCo-ENVIRONMENTAL

-------
                        Table 14
SUMMARY LIST OF F6D SYSTEMS IN THE EARLY PLANNING STAGES
                            177

-------
                                          TABLE 1H
               SUMMARY  LIST or FGO SYSTEMS  IN THE EARLY PLANNING STAGES
  FGO STATUS REPORT  05/76

  I.D. NUMBER AND COMPANY NAME
   UNIT NAME
                          LOCATION
                             START UP DATE   STATUS
                                                                                                                          REG
                                                                                                                          CLASS
    1 DAYTON POWER AND LIGHT CO.
    2 DAYTON POWER AND LIGHT CO.
    3 GENERAL PUBLIC UTILITIES
    
-------
                     Table 15
STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES
                        181

-------
 COMPANY

 POWER STATION
                                             TABLE 15
                        STATUS OF F6D SYSTEMS IN THE EARLY PLANNING STAGES DURING
                                             05/76
                   CURRENT MONTH
1.0. NUMBER    1
DAYTON POWER AND LIGHT CO.
KILLEN NO 1
  600  MW - NEW
COAL
NOT SELECTED
LIMESTONE'SCRUBBING
STARTUP   1/83
SITE PREPARATION IS UNDERWAY.  COMPANY IS INVESTIGATING LONG TERM SUPPLY
OF LOW SULFUR COAL FOR COMPLIANCE WITH REGULATIONS WITHOUT INSTALLING FGD
SYSTEM. DECISION ON THIS MATTER IS DUE MID 1976. SPACE HAS BEEN RESERVED
IN THE PLANT LAYOUT FOR FGD SYSTEM IF NEEDED. KILLEN NO.l NOW SCHEDULED
FOR STARTUP AFTER KILLEN NO.2.
I.D. NUMBER    2
DAYTON POWER AND LIGHT CO.
KILLEN NO 2
  600  MW • NEW
COAL
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP   1/61
SITE PREPARATION IS UNDERWAY.  COMPANY IS INVESTIGATING LONG TERM SUPPLY
OF LOW SULFUR COAL FOR COMPLIANCE WITH REGULATIONS WITHOUT INSTALLING FGD
SYSTEM. DECISION ON THIS MATTER IS DUE MID 1976. SPACE HAS BEEN RESERVED
IN THE PLANT LAYOUT FOR FGO SYSTEM IF NEEDED.
I.D. NUMBER    3
GENERAL PUBLIC UTILITIES
COHO NO.l
  800  Mb - NEW
COAL
NOT SELECTED
NOT SfLECTED
STARTUP   5/87
STARTUP DATE CHANGED TO 5/87 FOR BOTH BOILER AND FGD SYSTEM.  LIME, LIME-
STONE SCRUBBING* AND COAL DESULFURIZATION ARE THE PRIMARY PROCESSES BEING
GQNS10ERED.  NO DECISION HAS BEEN MADE YET.
I.D. NUMBER    4
GENERAL PUBLIC UTILITIES
SEWARO NO.7
  800  Mb - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   5/81*
STARTUP DATE CHANGED TO 5/6«» FOR BOTH BOILER AND FGD SYSTEM.  LIME.
LIMESTONE SCRUBBING, AND COAL DESULFURIZATION ARE THE PRIMARY PROCESSES
BEING CONSIDERED.  NO DECISION HAS BEEN MADE YET.                     .,,
 I.D. NUMBER    5
 GULF POWER CO.
 CRIST NO. H AND .NO. 5
  150  MW • RETROFIT

 NOT SELECTED
 NOT SELECTED
 STARTUP   0/76
EACH UNIT IS 75 NW.
1976.
                                                           IF SCRUBBERS ARE SELECTED THEY WILL BE REQUIRED IN
                                                               183
                                                                      PEDCo-ENVIRONMENTAL

-------
  COMPANY

  POWER  STATION
                     TABLE 15
STATUS OF FGO SYSTEMS IN THE EARLY PLANNING STAGES DURING  05/76

                                 CURRENT MONTH
 1.0.  NUMBER     6
 GULF  POWER CO.
 CRIST NO. 6  AND NO.  7
   620  MW -  RETROFIT

 NOT SELECTED
 NOT SELECTED
 STARTUP  0/60
              UNIT 6 IS 320 MW.   UNIT  7 IS 500  MW.
 I.D.  NUMBER     7
 GULF  POWER CO.
 LANSING  SMITH NO.  1  AND  NO.
   305 MW - RETROFIT
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/80
              UNIT NO.  1  IS  125  MW.   UNIT  NO.  2  IS  180 MW.   IF  SCRUBBERS ARE  SELECTED*
              THEY WILL BE REQUIRED  IN  1979  AND  1980 ON THE  RESPECTIVE UNITS.
 I.D. NUMBER    8
 KENTUCKY UTILITIES
 GHENT
  510  MW - NEW
 COAL   3-R PERCENT SULFUR
 NOT SELECTED
 LIME SCRUBBING
 STARTUP   1/77
              IN  THE  EARLY PLANNING  STAGE. COMPANY ALSO HAS AN EXISTING 510 MW UNIT
              AND UNDECIDED ON WHICH UNIT TO  INSTALL THE F6D SYSTEM.
I.D. NUMBER    9
POTOMAC ELECTRIC & POWER
CHALK POINT NO. i>
  630  MW - NEW
OIL
NOT SELECTED
NOT SELECTED
STARTUP   6/76
             AWAITING PERFORMANCE RESULTS FROM MGO UNIT ON DICKERSON NO. 3 (MONTGOMERY
             COUNTY).  UNIT WILL HAVE PEABODY-LURGI 2-STAGE VENTURI SCRUBBERS FOR PAR*
             TICULATE CONTROL.  COMPANY MAY ELECT NOT TO INSTALL FGO SYSTEM IF USE OF
             LOW SULFUR OIL IS CONTINUED.  BOILER START-UP SCHEDULED FOR LATE 1976.
I.D. NUMBER   10
POTOMAC ELECTRIC ft POWER
DICKERSON NO •»
  600  MM - NEW
COAL   2.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   5/62
             THERE ARE NO FIRM PLANS FOR INSTALLATION OF FGD SYSTEM.
             BOILER IS PLANNED FOR 1982.
STARTUP DATE OF
                                                              184
                                                                                                           PEDCo- ENVIRONMENTAL

-------
  COMPANY

  POWER STATION
                     TABLE 15
STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES DURING  05/76

                                 CURRENT MONTH,
 1.0.  NUMBER   11
 POTOMAC ELECTRIC ft POWER
 MORGANTOWN NO.l
   588  MU  - RETROFIT
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   6/79
              THEME ARE NO FIRM PLANS FOR INSTALLATION OF FGD SYSTEM.
              COMPANY PLANS TO EVALUATE ALL COMMERCIALLY AVAILABLE S02 CONTROL METHODS
              INCLUDING COAL GASIFICATION AND USE OF LOW SULFUR COAL.   COMPANY IS ALSO
              AWAITING RESULTS OF MGO SYSTEM OPERATION AT THE OICKERSON PLANT. DECISION
              EXPECTED WITHIN A YEAR.
 I.D.  NUMBER    12
 POTOMAC  ELECTRIC ft POWER
 MORGANTOWN NO.2
   556 MW -  RETROFIT
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   6/79
              THERE ARE NO FIRM PLANS  FOR  INSTALLATION OF FGD SYSTEM.
              COMPANY  PLANS TO EVALUATE  ALL  COMMERCIALLY  AVAILABLE S02 CONTROL  METHODS
              INCLUDING COAL GASIFICATION  AND USE  OF  LOW  SULFUR  COAL.   COMPANY  IS  ALSO
              AWAITING RESULTS OF  MGO  SYSTEM OPERATION AT THE DICKERSON PLANT.  DECISION
              EXPECTED WITHIN A YEAR.
 I.D.  NUMBER    13
 POWER AUTHORITY OF  NEW  YORK
 ARTHUR KILL
   700  MW  • NEW
 COAL  - 3S  SULFUR  -  REFUSE
 NOT SELECTED
 NOT SELECTED
 STARTUP    9/82
              THE  UTILITY  IS  CONSIDERING  BOTH  REGENERABLE  AND  LIMESTONE  SCRUBBING
              PROCESSES. FGD  TECHNOLOGY IS  BEING  CONSIDERED  FOR  A  FOSSIL FUEL  BURNING
              UNIT WHICH WILL EMPLOY  COAL AS THE  PRIMARY FUEL. REFUSE  AND OIL  WILL BE
              PROVIDED  FOR  SUPPLEMENTAL FUEL SUPPLIES.  THE PREFERRED INSTALLATION SITE
              IS THE  ARTHUR KILL FACILITY LOCATED ON STATEN  ISLAND. THE  PROJECT DESIGN
              ENGINEERS ARE SARGENT AND LUNDY.
I.D. NUMBER   14
SALT RIVER PROJECT
NAVAJO NO 1
  750  MW - RETROFIT
COAL   0.45 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
             THE UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
             DESULFURIZATION PROCESSES. A DEFINITIVE DECISION WILL BE MADE PENDING
             COMPLETION OF THE SRP/EPA STUDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
             SPECIFIED.
I.D. NUMBER   15
SALT RIVER PROJECT
NAVAJO NO 2
  700  MW - RETROFIT
COAL   0.45 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
             THE UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
             DESULFURIZATION PROCESSES. A DEFINITIVE DECISION WILL BE MADE PENDING
             COMPLETION OF THE SRP/EPA STUDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
             SPECIFIED.
                                                               185
                                                                                     PEDCo-ENVIRONMtrtTAl

-------
  COMPANY

  POWER STATION
                     TABLE 15
STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES DURING  05/76

                                 CURRENT MONTH
 I.D.  NUMBER   16
 SALT  RIVER PROJECT
 NAVAJO NO 3
   750  MW - RETROFIT
 COAL    0.45 PERCENT  SULFUR
 NOT SELECTED
 LIME/LIMESTONE SCRUBBING
 STARTUP   O/ 0
              THL UTILITY IS PRESENTLY INVESTIGATING THE USE  OF LOW SULFUR  COAL  AND
              DESULFURIZATION PROCESSES.  A DEFINITIVE DECISION WILL BE  MADE PENDING
              COMPLETION OF THE SRP/EPA STUDY.  NO SPECIFIC  STARTUP  DATE HAS VET  BEEN
              SPECIFIED.
 1.0.  NUMBER    17
 SPRINGFIELD  WATER  LIGHT   POWER
 DALLMAN  NO 3
   190 MM •  NEW
 COAL   3.0-  H.3 PERCENT  SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   6/79
              FGU SYSTEM IS UNDER  CONSIDERATION  WITH  BOTH  REGENERABLE  AND LIMESTONE
              SCKUBBING BEING  CONSIDERED.   BECAUSE  OF SPACE  LIMITATIONS  A REGENERABLE
              SYSTEM IS THE LIKELY CHOICE.   THE  COMPANY  IS ALSO  CONSIDERING COMPLIANCE
              THROUGH BURNING  OF LOW  SULFUR WESTERN COAL.
 I.D.  NUMBER    16
 TEXAS POWER AND LIGHT CO.
 TWIN  OAKS NO.  1
  750 MM - NEW
 LIGNITE
 NOT SFLECTED
 NOT SELECTED
 STARTUP   B/60
              THIS  UNIT  WILL  BE  JOINTLY OWNED BY TPSL AND ALCOA.
              NOT BEEN MADE WHETHER  TO INSTALL FGD FACILITIES.
A FIRM DECISION HAS
I.D. NUMBER   19
TEXAS POWER AND LIGHT CO.
TWIN OAKS NO. 2
  750  MW • NEW
LIGNITE
NOT SELECTED
NOT SELECTED
STARTUP   9/61
             THIS UNIT WILL BE JOINTLY OWNED BY TPSL AND ALCOA.
             NOT BEEN MADE WHETHER TO INSTALL FGD FACILITIES.
A FIRM DECISION HAS
I.D. NUMBER   20
VIRGINIA ELECTRIC AND POWER CO
MT. STORM
 11«»7  MW - RETROFIT
COAL
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
             THE UTILITY IS PRESENTLY CONSIDERENG BOTH OESULFURIZATION AND THE USE OF
             LOW SULFUR COAL. A DESULFURIZATION SYSTEM WOULD TREAT 69 PERCENT OF THE
             FLUE GAS FROM THREE BOILERS. CONSTRUCTION AND STARTUP DATES ARE CON-
             SIDERED INDEFINITE AT THIS TIME.
                                                                186
                                                                                                             PEDCo- ENVIRONMENTAL

-------
                                Table 16
FGD SYSTEM OPERATIONS THAT HAVE BEEN TERMINATED OR SHUT DOWN INDEFINITELY
                                     187

-------
                   Table 16
TERMINATED OPERATIONAL FGD SYSTEMS
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCY.
  PARTICULATES

  S02
   1
 BOSTON EDISON
 MYSTIC NO  6
 EVEFSTT MASSACHUSETTS
  150 MW
 OIL    2.5 PERCENT SULFUR
 CHEMICO
 MAGNESIUM  OXIDE SCRUBBING
 RETROFIT
  <»/72
 OPERATIONAL

 50 PERCENT

 90 PERCENT
 WATER MAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S32/KW CAPITAL * CALCINATION

 AVERAGE FGD SYSTEM AVAILABILITY FACTORS - APRIL 72 TO MAY 73.  17*.
 JUNE 73 TO DEC. 73. H8X.  JAN. 7H TO JUNE 7H. 60S.  JUNE 74.  80*.
 THE FGD SYSTEM HAS BEEN SHUT DOWN INDEFINITELY SINCE JUNE 7«*.
                                                                                                 PEDCO-ENVIRONMENTAL
                                                           189

-------
                                                           BACKGROUND  INFORMATION
                                                                    ON
                                                    THE MYSTIC  POWER STATION, UNIT NO. 6

THE MAGNESIUM OXIDE FGD SYSTEM «T BOSTON EDISON CONSISTS OF A CHEMICO  SINGLE-STAGE VENTURI SCRUBBER.  THE SCRUBBER UNIT IS CONSTRUCTED OF CARBON
STEEL WITH A SPRAY-APPLIED POLYESTER LINING.  THE SCRUBBER TREATS  440,000 ACFM OF 300°F FLUE GAS CONTAINING SOg AT A CONCENTRATION OF 1410 PPM.  S02
REMOVAL EFFICIENCY IS REPORTED TO BE 90 PERCENT.
     THE MgO PROCESS IS A REGENERABLE PROCESS.  THE SCRUBBER CAPTURES  S02 BY  FORMATION OF MAGNESIUM SULFITE.  THIS PRODUCT SLURRY IS THEN FILTERED AND
DRIED.  THE DRY MATERIAL IS CALCINED AT HIGH TEMPERATURES TO DRIVE OFF THE  S02 AND REGENERATE MgO.  THE S02 STREAM IS PROCESSED IN A SULFURIC ACID
PLANT TO MAKE 98 PERCENT GRADE OF SULFURIC ACID.
PROBLEMS AND SOLUTIONS
     FROM THE INITIAL START-UP IN APRIL 1972 UNTIL MAY 1973 THE SCRUBBER OPERATED  INTERMITTENTLY BECAUSE OF MECHANICAL DIFFICULTIES.  THE MAJOR PROBLEM.
ENTAILING DESIGN AND OPERATION OF MgSOj CRYS'jAL DRYER, APPARENTLY  HAS  BEEN  RESOLVED  BY REDESIGN AND FUEL CHANGE.  PROBLEMS WITH THE STACK AND PUMP
OCCURRED DURING USE OF REGENERATED MgO.  OVERHEATING OF THE SLURRY DURING ACTIVATION OF THE STEAM FREEZE PROTECTION SYSTEM CAUSED FORMATION OF SCALE
IN THE MgO SLURRY PIPING.  IN 1974,. SYSTEM OPERATION WAS LIMITED BY BOILER  AVAILABILITY.  SINCE FEBRUARY 1974 AVAILABILITY OF THE BOILER HAS BEEN
INCREASED.  THE SYSTEM HAS BEEN SHUT DOWN INDEFINITELY SINCE JUNE  1974,  WHEN  EPA FUNDS FOR THE CALCINING PORTION OF THIS OPERATION WERE EXHAUSTED.
     AVAILABILITY FACTORS AND COMMENTS CONCERNING THE OPERATION OF THIS  SYSTEM SINCE STARTUP ARE PRESENTED IN THE FOLLOWING TABLE.
                                                                                                                             PEDCo- ENVIRONMENTAL

                                                                         190

-------
                                                          FGD SYSTEM AVAILABILITY
                                                             MYSTIC UNIT NO. 6

Month               Availability (1)                                                 Comments
Apr< 72                  17                      The module operated Intermittently because of mechanical  difficulties.  A major problem concerned
   to                                            design and operation of the magnesium sulflte crystals dryer.
May 73
Jun. 73                  68
Jul. 73                  61
Aug> 73                                          The boiler was down for the annual overhaul.  System availability decreased'during  the last quarter
Sep  73                  38                      of the year because of heavy erosion/corrosion 1n the liquor redrculatlon  pumps  and centrifuge.
Oct. 73                  60
Nov. 73                  26
Dec. 73                  13
Jan  74                  28                       System availability was limited by boiler-related problems that caused frequent  shutdowns  In
Pet>. 74                  25                       January  and February.
Mar. 74                  87
Apr. 74                  81
(ky 74                   57                       57 percent availability was due to 2 weeks outage of the acid plant rather  than  to  FGD system
Jun  74                  80                       failure.  Demonstration program was completed and FGD system was shut down.  EPA funding of MgSOj
                                                  calcination  has  expired.   There are no definite plans for restarting of this unit.
Average Availability  (January to June, 1974) - 59.7 Percent.
                                                                        191                                                     PEDCo-ENVIRONMENTAL

-------
                             Table  16
  TERMINATED  OPERATIONAL  FGD SYSTEMS
IDENTIFICATION NO.

UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCYt
 PARTICULATES


 S02
                      DAIRYLAND POWER  COOP

                      ALMA STATION
                      ALMA WISCONSIN

                        60 MW
                      COAL   3.0- 3.5  PERCENT SULFUR

                      FOSTER WHEELER
                      LIME INJECTION

                      RETROFIT

                       6/71

                      OPERATIONAL
                      25 PERCENT
WATER HAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
 "
                      THIS EXPERIMENTAL WET LIME FURNACE INJLCTION SYSTEM HAS BEEN OPEKATIONAL
                      SINCE 1971 FOR PERIODS UP TO 30 DAYS.  IN AUGUST 1971 THE UNIT WAS TESTED
                      FOR TWO DAYS USING WESTERN LOW SULFUR COAL.  THE TEST SHOWED ABOUT SOX
                      S02 REMOVAL EFFICIENCY, BUT PRECIPITATOR PERFORMANCE WAS ADVERSELY
                      AFFECTED.  THE FGD PROJECT HAS BEEN SHUT DOWN INDEFINITELY SINCE
                      AUGUST 197* t AND THERE ARE NO PLANS FOR FUTURE OPERATION.
                                                                                                       PEDCo- ENVIRONMENTAL,
                                                          192

-------
                     Table 16
TERMINATED OPERATIONAL FGO SYSTEMS
  IDENTIFICATION NO.

  UTILITY  NAME

  UNIT  NAME

  UNIT  LOCATION

  UNIT  RATING
 ILLINOIS POWER

 WOOD RIVER NO H

 EAST ALTON ILLINOIS

  no nw
  FUEL  CHARACTERISTICS   COAL    2.9-  3.2 PERCENT  SULFUR
  FGD  VENDOR
  PROCESS
  NEW  OR RETROFIT
  START UP  DATE
  FGO  STATUS
  EFFICIENCY.
   PARTICULATES
 MONSANTO ENVIRO CHEM SYSTEMS

 CATALYTIC OXIDATION

 RETROFIT

 10/72

 OPERATIONAL
   S02
 85 PERCENT
  WATER  MAKE UP
  SLUDGE  DISPOSAL
 UNIT COST
S7S/Kh CAPITAL*** MILLS/KWH OP
 OPERATIONAL
  EXPERIENCE
 THE FGO SYSTEM HAS HAD CONSIDERABLE AMOUNT OF PROBLEMS SINCE STARTUP IN
 1972.  TOTAL OPERATION WAS «f«m HOURS IN 1972. 158 HOURS IN 1973»  AND 55
 HOURS IN 1974. HEAT EXCHANGER LEAKS HAVE BEEN ENCOUNTERED. AND AN
 EVALUATION IS NOW BEING MADE TO DETERMINE WHETHER TO REPLACE THE  HEAT
 EXCHANGER OR TO REPAIR IT. THE SYSTEM IS SHUT DOWN INDEFINITELY AT
 PRESENT.
                                                             193
                                                                                                         PEDCO-ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION
                                                               ON
                                                        WOOD RIVER NO. 4


     THE WOOD RIVER NO.  4 BOILER IS LOCATED NEAR EAST ALTON, ILLINOIS, NORTH OF ST. LOUIS.  THE BOILER HAS A RATED CAPACITY OF 110 MW.   IT IS RETRO-
FITTED WITH A CATALYTIC  OXIDATION FGD SYSTEM DESIGNED BY MONSANTO ENVIRO-CHEM SYSTEMS.  THE SYSTEM TREATS THE FLUE GAS FROM A HIGH EFFICIENCY ELECTRO-

STATIC PRECIPITATOR.
     THE FLUE GAS IS HEATED TO A TEMPERATURE OF 850°F AND  IS PASSED THROUGH A VANADIUM. PENTOXIDE FIXED-BED CATALYTIC CONVERTER, WHERE S02 IS OXIDIZED TO
SO .  THE GAS THEN FLOWS THROUGH AN ACID ABSORPTION TOWER,  WHERE THE SULFUR TRIOXIDE  IN THE GAS IS CONVERTED TO SULFURIC ACID.  AN ACID MIST ELIMINATOR
ENSURES REMOVAL OF ENTRAINED ACID MIST FROM THE GAS STREAM.  THE CLEANED GAS IS DISCHARGED TO THE STACK AND THE PRODUCT ACID IS COOLED AND STORED IN

TANKS.
PROBLEMS AND SOLUTIONS
     SINCE COMPLETION OF THE SYSTEM IN JULY 1972, A SERIES OF MECHANICAL DIFFICULTIES HAS OCCURRED AND MODIFICATIONS HAVE BEEN EFFECTED.  DURING JULY
1973, AN ACCEPTANCE TEST WAS CONDUCTED TO ESTABLISH THE SPECIFIED 85 PERCENT SULFUR DIOXIDE REMOVAL, WHILE PRODUCING AN ACID PRODUCT OF RQUIRED CON-

CENTRATION OF 77.7 PERCENT.  BOTH OF THESE SPECIFICATIONS  WERE  MET.
     LONG TERM OPERATION OF THE SYSTEM HAS BEEN DELAYED BECAUSE OF  DELAYED DELIVERY OF EQUIPMENT FOR A PLANNED SYSTEM MODIFICATION TO CONVERT THE
REHEATER BURNERS FROM NATURAL GAS TO FUEL OIL.  SEVERAL MAJOR  PROBLEMS INCLUDE  FROZEN DAMPERS ON REHEAT BURNERS, CRACKS IN THE TEFLON LINER ON THE ACID
PUMP'S DISCHARGE HEADER, CRACKS IN THE REHEAT DUCTING,  FALL OF  REFRACTORY  BRICKS  FROM THE REHEATER BURNER DOME, AND NEED FOR REINFORCEMENT OF THE
STRUCTURE SUPPORTING THE HIGH TEMPERATURE FLUE GAS DUCT TO THE  CATALYTIC CONVERTER.   MOST OF THESE PROBLEMS HAVE BEEN CORRECTED.  ILLINOIS POWER AND EPA
ARE NOW DETERMINING HOW TO CORRECT LEAKING ACID COOLERS.  PATCHING  ATTEMPTS HAVE  BEEN UNSUCCESSFUL.  REPAIR OR REPLACEMENT OF THE COOLERS IS EXPECTED

TO TAKE SEVERAL MONTHS.
                                                                       194
                                                                                                                         PEDCo-ENVIRONMENTAL

-------
             OPERATING LOG


       CATALYTIC OXIDATION SYSTEM
     •

  WOOD RIVER NO. 4 - ILLINOIS POWER CO.
System operating
Date
9-4-72
9-5-72
9-6-72
9-7-72
9-10-72
9-11-72
9-12-72
9-13-72
9-14-72
9-15-72
9-16-72
9-17-72
9-18-72
9-19-72
9-24-72
10-6-72
10-7-72
hours
12
24
24
2
6
2
16
24
24
24
24
24
24
3
17
12
24
Date
10-8-72
10-9-72
10-10-72
10-12-72
10-13-72
10-14-72
10-30-72
10-31-72
7-21-73
7-22-73
7-23-73
7-24-73
7-25-73
7-26-73
7-17-73
7-28-73
7-29-73
hours
24
24
18
16
20
16
24
16
18
24
18
24
14
13
19
19
9
   TOTAL
602 HOURS
               195
                                                                    PEDCo-ENVIRONMENTAL

-------
                  Table 16
  TERMINATED OPERATIONAL FGD SYSTEMS
IDENTIFICATION NO.

UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
 POTOMAC ELECTRIC & POWER

 DICKERSON NO 3

 OICKERSON MARYLAND

   95 MW
FUEL CHARACTERISTICS  COAL   2.0 PERCENT SULFUR
FGO VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY!
 PARTICULATES
 CHEMICO

 MAGNESIUM OXIDE SCRUBBING

 RETROFIT

  9/73

 OPERATIONAL
 S02
 90 PERCENT
WATER MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
S70/KW CAPITAL
 REFER TO BACKGROUND INFORMATION SECTION  IN  TABLE 16 OF  THIS REPORT. THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE  SEPTEMBER 1973.  THE UNIT HAS BEEN
 TERMINATED AS AN S02 SCRUBBER.  HOWEVER.IT WILL CONTINUE TO OPERATE AS A
 PARTICULATE SCRUBBER.
                                                                                                         PEDUo-tnvmONMENTAL
                                                         196

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                               OICKERSON  NO.  3

    .THE DICKERSON STATION OF POTOMAC ELECTRIC POWER CO.  (PEPCO)  IS LOCATED ON  THE  POTOMAC RIVER NEAR DICKERSON, MARYLAND, ABOUT 30 MILES NORTHWEST OF
WASHINGTON. D.C.  THE STATION HAS THREE ELECTRIC GENERATORS.  EACH RATED AT 190  MW.  UNIT  NO. 3  IS A DRY BOTTOM COAL-FIRED BOILER DESIGNED BY COMBUSTION
ENGINEERING AND INSTALLED IN 1962.  THE COAL NOW BURNED HAS AN AVERAGE GROSS  HEATING VALUE OF 11.700 BTU/LB AND AVERAGE ASH AND SULFUR CONTENTS OF
14 AND 2 PERCENT. RESPECTIVELY.  THE BOILER IS FITTED WITH AN ELECTROSTATIC PRECIPITATOR  DESIGNED AND INSTALLED BY RESEARCH-COTTRELL IN 1962.  THE FGD
SYSTEM EMPLOYS THE CHEMICO-BASIC MAGNESIUM OXIDE SCRUBBING PROCESS.   THE  RETROFIT -SYSTEM  HANDLES APPROXIMATELY 50 PERCENT OF THE EXHAUST GAS FROM THE
NO. 3 UNIT.
     THE FGD SYSTEM CONSISTS OF A SINGLE. TWO-STAGE SCRUBBER/ABSORBER, WHICH  INCORPORATES AN ADJUSTABLE-THROAT VENTURI SCRUBBER FOR PARTICULATE
REMOVAL AND A SECOND STAGE ABSORBER WITH A FIXED VENTURI  TO REMOVE SULFUR DIOXIDE.  THE LIQUOR  STREAMS FOR BOTH STAGES ARE SEPARATE AND OPERATE IN A
CLOSED LOOP MODE.  UNTIL MID-1975 THE MAGNESIUM SULFITE GENERATED WAS TRANSFERRED TO AN EPA FINANCED FACILITY AT THE ESSEX CHEMICAL COMPANY SULFURIC
ACID MANUFACTURING PLANT IN RUMFORD. RHODE ISLAND,  WHERE  MAGNESIUM OXIDE  WAS  REGENERATED  AND S02 FROM THE REGENERATION PROCESS WAS CONVERTED TO SULFURIC
ACID.  THE RUMFORD FACILITY HAS SINCE BEEN CLOSED DOWN.
     CONSTRUCTION WAS COMPLETED IN AUGUST AND THE SYSTEM  STARTED  UP IN SEPTEMBER 1973.  IN INTERMITTENT OPERATIONS FOR SHAKEDOWN THROUGH JANUARY 1974,
THE LONGEST CONTINUOUS RUN WAS 271 HOURS.  THE SYSTEM WAS RESTARTED FROM  JULY THROUGH DECEMBER  1974, AND AGAIN ON AUGUST 11. 1975, FOR APPROXIMATELY
87 HOURS.
     FGD UNIT OUTAGES WERE CAUSED PRIMARILY BY PIPE AND PUMP  CORROSION AND MAJOR TURBINE  OVERHAUL OF THE BOILER.  PARTICULATE AND S02 REMOVAL EFFICIENCY
GUARANTEES WERE CORROBORATED DURING OPERATIONAL PHASES.
     THE REMAINING SUPPLY OF MAGNESIUM OXIDE, ABOUT 100 TONS  (10  DAYS). HAS BEEN DEPLETED. AND  THE DICKERSON UNIT HAS BEEN TERMINATED AS AN FGD SYSTEM.
                                                                                                                           PEDCo-ENVIRONMtNiAL
                                                                   197

-------
                                                         DICKERSON NO.  3
                                                  FGD SYSTEM OPERATING HISTORY

          _  .  .                                                     Comments
Operating Period                                                     	
Sep  73                  problems during this  period ranged from corrosion leaks In expansion joints to problems  In material
  to                     handling equipment, feeding and slaking of MgO, plugging In the MgO mix tank and suction lines to
Jan. 74                  the MgO make-up pumps.

Jan> 74                   Maintenance and modifications were  performed  on  the  system.  The major system revision made during
   to                      this period was the addition of  a pre-mlx tank In  the MgO system.
Apr. 74

Apr  74                   UnHteo" operation because the utility did not have access  to the EPA calcining  facility at the  Essex
   to                     chemical  Company sulfurlc add plant.  By the end of June  1974, all  the  MgO at  Dlckerson had been used
Ju1<  74                   and a  silo plus three  train cars were full of MgSOj.

 Aug, 74                   During this period  the system generally operated at 75 percent of the design gas flow.
   to
 Dec. 74

 Jan. 75
Problems developed In the  bucket elevator transporting the MgS03 from the dryer to the storage silo.
  Feb>   75                  Unit No. 3 was taken out of service for an 8 to  12 week turbine overhaul.  The scrubber was Inspected,
    to                      maintenance and modifications were made.
  Jul.  75
                                                                                                                 PEDCo-ENVIRONMENTAL

                                                           198

-------
                                              DICKERSON NO. 3 (Continued)
                                             FGD SYSTEM OPERATING HISTORY

Operating Period                                                     Comments
Aug. 75                   The  FGD  system was restarted In August.  Steam was  lost  to  the MgO mix tank, resulting in a very moist
                          product  from the centrifuge.   Caking In the dryer  occurred.  At this point, the utility decided to  test
                          only the first-stage of the scrubbing system, taking  gas ahead- of the preclpltator.  FGD operation at
                          Dlckerson  terminated at this point.
                                                                                                                PEDCo-ENVIRONMENTAL
                                                         199

-------
                   Table  16
  TERMINATED OPERATIONAL  FGD SYSTEMS
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 SOUTHERN CALIFORNIA EDISON

 MOHAVE NO 1A

 LAUGHLIN NEVADA

  170 MW
 FUEL  CHARACTERISTICS  COAL   0.5-  0.8 PERCENT  SULFUR
 FGD  VENDOR

 PROCESS

 NEW  OR RETROFIT

 START UP DATE

 FGD  STATUS

 EFFICIENCY.
 PARTICULATES

 S02

 WATER MAKE UP

 SLUDGE DISPOSAL

UNIT COST
 UNIVERSAL OIL PRODUCTS

 LIMESTONE SCRUBBING

 RETROFIT

 11/74

 OPERATIONAL
OPERATIONAL
 EXPERIENCE
THIS EXPERIMENTAL MODULE STARTED UP OCT. 31, 197* AND OPERATED WITH AN
AVAILABILITY OF 60.tS THROUGH FOUR MONTHS OF TESTING.  TESTS HAVE BEEN
COMPLETED, AND THE F&D SYSTEM WAS SHUT DOWN INDEFINITELY ON JULY 2, 1975.
NEVADA ASSEMBLY bILL NO. 706 HAS PLACED A 2-YEAR MORATORIUM ON THE
ENFORCEMENT OF THE COMPLIANCE SCHEDULE FOR THIS STATION.  FURTHER FGO
ACTIVITIES WILL BE DEPENDENT ON FUTURE LEGISLATION.
                                                 200

-------
               Table 16
TERMINATED OPERATIONAL FGD SYSTEMS
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
FGD VENDOR
PROCESS
NEW OR RETROFIT
START UP  DATE
FGD STATUS
EFFICIENCY,
 PARTICULATES
 so2
WATER MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
                        SOUTHERN CALIFORNIA EDISON
                        MOHAVE NO. 2A
                        LAUGHLIN NEVADA
                        160 MW
                        COAL   0.5- 0.8 PERCENT SULFUR
                        SCE/  STEARNS ROGER
                        LIME  SCRUBBING
                        RETROFIT
                        11/73
                        OPERATIONAL
                                   -«
                          90  PERCENT
                          370 GAL/LB MOLE  SOg REMOVED
                          STABILIZED SLUDGE DISPOSED  IN UNLINED POND
                         TO THE FOUR CORNERS PLANT. OPERATED BY ARIZONA PUBLIC SERVICE. FOR INSTALLATION.
                                                                                                     PEDCo- ENVIRONMENTAL
                                                        201

-------
                                                      BACKGROUND INFORMATION
                                                              ON
                                          THE MOHAVE TEST MODULES PROGRAM:  NOS. 1A AND 2A

     no PROTOTYPE SUL™ D,o,,M ABSORBER HONLES WERE .NSTALLEO  „ ,„ ,T « WHWE 6EHEMIIBS sm,OH . w SOUTH£m
       .  A TO „«. MIED „ 170 „, M
 ALSO RATEO AT ,„ „. MS ,BSTALLEO „ reEAT , SImLM FLU£ as „,„„„ FRW „ m  2  ^ imtM

 «». »ET ™T»«,S CENEMTI)B CAPAC.TV 0, 790 W . EKH WO. . reSTEm, Lffl,.SULFU8 ^ „„„ A „„„„, ^ „
 AND SULFUR CONTENTS OF 10 AND  0.4 PERCENT RESPECTIVELY.                             '
 VERTICAL MODULE
     m VERTICAL HOOUU, A UN..ERSA! 0,L PROOUCTS TURmBT COMTACT «SO«BE« (TCA). w TESTED „ T.O »DES:  FIRST. AS A TCA UK,T  PROH
.. .« TO APRK 30. ,„. „ S.COHO AS A *«. PACKE0 AeSORBE, ,«,. « «» THE «, „ ,„,. UERE REPL4CED 
-------
                          MOHAVE NO. 1A - VERTICAL TEST MODULE

                  OUTAGE  TIME HISTORY:  NOVEMBER 2, 1974 TO JULY 2,  1975
                    Reason                                   Time (hr)
1.   Repair grids and redistribute TCA balls                    710
2.   Clean scale from scrubber  internals                        344
3.   Repair/replace plugged  nozzles                             153
4.   Repair leaks in trap-out tray                              120
5.   Repair/realign PPA packing                                  85
6.   Correct booster fan  trip problems                           72
7.   Conduct inspections  for extended operations                 46
8.   Remove hardhat from  thickener                               46
9.   Total outage time                                        1585

     Total" outage time:  1585 hours
     Total calendar time:  5813 hours
     Total operational time:  4228 hours
     Percent availability:   72.73
                                                                                           PEDCo-ENVIRONMENTAL
                                            203

-------
                          MOHAVE NO. 2A - HORIZONTAL TEST MODULE

                 OUTAGE TIME HISTORY:  JANUARY 16. 1974 TO FEBRUARY  9,  1975
                    Reason                                       Time  (hr)
 1.    Modify and  repair plastic demlster blades                      503
 2.    Correct booster fan balance problems                           317
 3.    Pump repair                                                   256
 4.    Spray nozzle  replacement                                       238
 5.    Modify gas  Inlet flow distribution                             162
 6.    Repair hopper leaks                                            135
 7.    Remove hardhat from thickener                                  82
 8.    Modify slaking water for scale prevention                      45
 9.    Conduct Inspections for extended operations                   	19_
10.    Total outage  time                                             1757

      Total outage  time:  1757 hours
      Total calendar time:  9328 hours
      Total operating time:  7571 hours
      Percent availability:  81.161
                                                                                             PEDCo-ENVIRONMENTAL

                                         204

-------
                  Table 16
  TERMINATED OPERATIONAL FGD SYSTEMS  2/76
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
TENNESSEE VALLEY AUTHORITY

SHAWNEE NO. IOC

PADUCAH KENTUCKY

  10 MW
FUEL CHARACTERISTICS  COAL 2.9 PERCENT .SULFUR
FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY.
  PARTICULATES


  S02


WATER HAKE  UP


SLUDGE  DISPOSAL


UNIT  COST
 OPERATIONAL
  EXPERIENCE
TENNESSEE VALLEY AUTHORITY

LIME/LIMESTONE SCRUBBING

RETROFIT

 H/72

OPERATIONAL
 REFEH TO BACKGROUND INFORMATION SECTION IN TABLE 16 OF THIS KEPOKT.  THIS
 FGD SYSTLM HAS KEEN OPERATIONAL SINCE APRIL.15.72.  THIS MARBLE-BED AB-
 SORBER, MANUFACTURED BY COMBUSTION ENGINEERING CO., WAS DISCONTINUED
 EARLY IN THE TEST PROGRAM BECAUSE OF CONTINUED OPERATING PROBLEMS WITH
 NOZZLE FAILURE AND SUBSEQUENT PLUGGING OF THE MARBLE BED.  THIS SYSTEM
 BECAME OPERATIONAL IN APRIL 1972 AND WAS PERMANENTLY TERMINATED IN
 JULY 1973.
                                                                                                          PEDCo-ENVIRONMENTAL
                                                          205

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                       SHAWNEE NOS.  10A, 10B,  AND IOC

     IN JUNE 1968, THE EPA INITIATED A PROGRAM TO TEST PROTOTYPE WET LIME AND  LIMESTONE  SCRUBBING SYSTEMS FOR REMOVAL OF SULFUR DIOXIDE AND PARTICULATES
FROM FLUE GAS.  THE PROGRAM WAS CARRIED OUT IN A TEST FACILITY INCORPORATED INTO THE  FLUE GAS DUCT WORK OF UNIT NO. 10, A COAL-IFRED BOILER AT THE
TVA SHAWNEE POWER STATION, PADUCAH, KENTUCKY.  TVA IS THE CONSTUCTOR AND FACILITY OPERATOR AND THE BECHTEL CORP. IS THE MAJOR CONTRACTOR AND TEST
DIRECTOR.
     THE TEST FACILITY CONSISTS OF THREE PARALLEL SCRUBBER SYSTEMS OF PROTOTYPE  SIZE  TREATING PART OF THE FLUE GAS FROM THE BOILER.  EACH SCRUBBER    •
TRAIN IS CAPABLE OF TREATING APPROXIMATELY 30,000 ACFM, OR THE EQUIVALENT OF APPROXIMATELY 10 MW OF POWER PLANT GENERATING CAPACITY.
     THREE PARALLEL WET SCRUBBER SYSTEMS WERE SELECTED FOR THE TEST  PROJECT:   1)  A VENTURI WITH A SPRAY TOWER AFTER ABSORBER; 2) A TURBULENT CONTACT
ABSORBER (TCA) AND 3) A MARBLE-BED ABSORBER.  THE VENTURI SYSTEM; MANUFACTURED BY CHEMICAL CONSTRUCTION CO., CONTAINS AN ADJUSTABLE THROAT THAT PERMITS
CONTROL AND VARIATION OF PRESSURE DROP UNDER A WIDE RANGE OF FLOW CONDITIONS.  THE TCA UNIT, MANUFACTURED BY UNIVERSAL OIL PRODUCTS, EMPLOYS A
FLUIDIZED BED OF LOW DENSITY PLASTIC SPHERES THAT ARE FREE TO MOVE BETWEEN RETURNING  GRIDS.  THE MARBLE-BED ABSORBER, SUPPLIED BY COMBUSTION ENGINEERING
CO., USES A PACKING OF 3/4-INCH GLASS MARBLE SPHERES AND A TURBULENT LAYER OF  LIQUID  AND GAS ABOVE THE MARBLE LAYER TO ENHANCE MASS TRANSFER.
     THE TEST FACILITY WAS DESIGNED SO THAT MODIFICATIONS AND VARIATIONS OF SCRUBBER  INTERNALS AND PIPING COULD BE READILY EMPLOYED FOR EACH SCRUBBER
SYSTEM.   EACH SYSTEM CAN TREAT APPROXIMATELY 30,000 ACFM OF FLUE GAS AT  300°F  CONTAINING 1800 TO 4000 PPM OF S02 AND 2 TO 5 GRAINS/SCF OF PARTICULATES.
TESTING OF THE TCA AND THE VENTURI SPRAY TOWER IS IN PROGRESS;  OPERATION OF THE MARBLE-BED ABSORBER UNIT HAS BEEN PERMANENTLY DISCONTINUED.
                                                                                                                        PEDCo-ENVIRONMENTAL
                                                                     206

-------
DEFINITIONS
  207

-------
                                         DEFINITIONS
Boiler Capacity Factor
Boiler Utilization Parameter
Efficiency,
   Particulates
   SO,
FGD Availability Factor
FGD Reliability Factor
FGD Operability Factor
FGD Utilization Factor
FGD Status
   Category 1

   Category 2
   Category 3
(kWh generation in year)/(maximum continuous generating
capacity in kW x 8760 hr/yr).

Hours boiler operated/hours in period, expressed as a
percentage.


Operational - The actual percentage of particulates re-
moved by the FGD system and the particulate control de-
vices from the untreated flue gas.  All others - The
design efficiency (percentage) of particulate removed by
the FGD system and the particulate control devices.

Operational - The actual percentage of S02 removed from
the flue gas.  All others - The design efficiency.

Hours the FGD system was available for operation  (whether
operated or not)/hours in period, expressed as a percentage,

Hours the FGD system operated/hours FGD system was called
upon to operate, expressed as a percentage.

Hours the FGD system was operated/boiler operating hours
in period, expressed as a percentage.

Hours FGD system operated/hours in period, expressed as
a percentage.


Operational - Unit has been or is in service removing S02.

Under Construction - Ground has been broken for installa-
tion of FGD system, but FGD system has not become opera-
tional.

Planned, Contract Awarded - Contract has been signed for
purchase of FGD system but ground has not been broken
for installation.
                                          209

-------
   Category 4



   Category 5



   Category 6


   Category 7


FGD Vendor


Fuel Characteristics



Identification Number


New



Operational Experience
Process
     DEFINITIONS

Planned, Letter of Intent Signed - Letter of intent has
been signed, but legal contract for purchase has not been
awarded.

Planned, Requesting/Evaluating Bids - Bid requests have
been released but no letter of intent or contract has
been issued.

Considering only FGD Systems - An FGD system is proposed
as a means to meet an SO2 regulation.

Considering an FGD system as well as alternative methods
(Tables 14, 15).

Vendor with a signed contract, letter of intent or strong
commitment because of test unit or past purchases.

Type of fuel, average gross heating value in Btu/lb,
average percent ash and average percent sulfur content
for fuel as fired.

Number of unit  in the alphabetical listing in Tables 1,
2, 3 or Tables  14, 15.

FGD unit and boiler were designed at the same time or
space for addition of an FGD unit was reserved when
boiler was constructed.

Operational - Brief summary of FGD system operation
since start-up  and description of current month's per-
formance.  All  others - Comments regarding stage of con-
struction, etc.

Company name if process is patented.  Generic name if
several companies have similar processes.
                                         210

-------
Regulatory Class
Retrofit


Sludge Disposal



Start-up Date



Unit Cost
      DEFINITIONS

 A.    New boiler constructed subject to Federal New Source
      Performance Standards.

 B.    Existing boiler subject to State Standard that is
      more stringent than the Federal New Source Perform-
      ance Standard (NSPS).

 C.    Existing boiler subject to State Standard that is
      equal to or less stringent than NSPS.

 D.    Other.

 E.    Unknown.

 FGD  unit must be added to an existing boiler  not
 specifically  designed to accommodate FGD unit.

 Comments on disposal  method for those units generating
 sludge  including:  lined  or  unlined  ponds, stabilized or
 unstabilized  sludge,  and on- or off-site disposal.

 Operational -  Date  when  S02 removal  began.  All  others -
 Date when  SO2  removal  is scheduled  to begin.  Generally
 this will  be  the start-up date  of the boiler.

 Capital  Cost  in  $/kW  including:  S02  absorption and regen-
 eration  system,  SO2 recovery system,  solids disposal,
 site improvements,  land, roads,  tracks,  substation, engi-
 neering  costs, contractors  fee  and  interest on capital
 during construction.

Annualized Cost  in mills/kWh  including fixed and variable
 costs.   Fixed costs include:  interest on capital, deprecia-
 tion, insurance, taxes,  and  labor costs  including overhead.
Variable costs include:  raw materials, utilities, and
maintenance.
                                        211

-------
Unit Location

Unit Name




Unit Rating



Utility Name



Water Make-Up
     DEFINITIONS

City and State listed in mailing address.

Unit identification as it appears 'in Electrical World -
Direction of Electrical Utilities, McGraw-Hill - Current
Edition - or as indicated by utility representative for
installations in planning stages.

Operational - Maximum continuous gross generation capacity
in MW; Preoperational - maximum continuous design genera-
tion capacity in MW

Name of corporation as it appears in Electrical World -
Directory of Electrical Utilities, McGraw-Hill - Current
Edition - as space permits .
Gallons per minute of make-up water required per MW
capacity.
                                                    of
                                           212

-------