EPA-R2-73 135
JANUARY 1973            Environmental Protection Technology Series
Investigation  of Use
of Gel  Material
for Mine Sealing
                       % PROl^
                                 Office of Research and Monitoring
                                 U.S. Environmental Protection Agency
                                 Washington. DC  20460

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            RESEARCH REPORTING SERIES
Research reports of the  Office  of  Research  and
Monitoring,  Environmental Protection Agency, have
been grouped into five series.  These  five  broad
categories  were established to facilitate further
development  and  application   of   environmental
technology.   Elimination  of traditional grouping
was  consciously  planned  to  foster   technology
transfer   and  a  maximum  interface  in  related
fields.  The five series are:

   1.  Environmental Health Effects Research
   2.  Environmental Protection Technology
   3.  Ecological Research
   4.  Environmental Monitoring
   5.  Socioeconomic Environmental Studies

This report has been assigned to the ENVIRONMENTAL
PROTECTION   TECHNOLOGY   series.    This   series
describes   research   performed  to  develop  and
demonstrate   instrumentation,    equipment    and
methodology  to  repair  or  prevent environmental
degradation from point and  non-point  sources  of
pollution.  This work provides the new or improved
technology  required for the control and treatment
of pollution sources to meet environmental quality
standards.

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                                                         EPA-R2-73-135
                                                         January 1973
                 INVESTIGATION OF  USE OF GEL

                  MATERIAL FOR MINE SEALING
                             By

                      Neville  K.  Chung


                      Project  14010 EKW


                       Project Officer

                       Ronald  D.  Hill
        Mine  Drainage Pollution  Control Activities
               Environmental Protection Agency
          National Environmental Research Center
                   Cincinnati, Ohio 45268


                        Prepared  for

              OFFICE OF RESEARCH  AND MONITORING
            U.S. ENVIRONMENTAL PROTECTION AGENCY
                   WASHINGTON, D.C. 20460
For sale by the Superintendent ol Documents, U.S. Government Printing Office, Washington, D.C. 20402 - Price J1.25

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            EPA Review Notice
This report has been reviewed by the Environ-
mental Protection Agency and approved for
publication.  Approval does not signify that
the contents necessarily reflect the views
and policies of the Environmental Protection
Agency, nor does mention of trade names or
commercial products constitute endorsement
or recommendation for use.
                    11

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                     ABSTRACT
Laboratory testing of commercially available chemical
grouts was conducted to evaluate their potential use,
in conjunction with a cheap filler, for remote sealing
of mine voids.  By close control of the setting time and
proper distribution of the grout slurry it was believed
that a mine seal could be placed through a borehole from
the surface without the benefit of retaining bulkheads.

A slurry mix consisting of an acrylamide grout with
flyash or mine refuse as a filler was found to produce a
strong controllable gel which resisted chemical attack
in the laboratory over an eleven week exposure period.

An attempt to demonstrate a novel technique for applica-
tion of the selected grout slurry in a mine entry with
high flow was not successful.  The results suggest that
the technique may be applicable in dry or low flow
situations.  However, the estimated cost of a mine seal
using the gel material is presently not competitive with
existing methods.

Groundwater monitor wells were drilled for the purpose
of determining the effect of mine sealing on groundwater
conditions.  Data reflecting pre-seal conditions was
compiled, but because the sealing of the mine was not
completed the monitoring program has been postponed.

This report was submitted in fulfillment of Project
Number CR-100 Contract 14010 EKW, under the joint
sponsorship of the U. S. Environmental Protection Agency
and the Commonwealth of Pennsylvania, by Dravo Corporation,
Pittsburgh, Pennsylvania 15222.
                         111

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                     CONTENTS


Section                                          Page

  I       CONCLUSIONS                              1

  II      RECOMMENDATIONS                          3

  III     INTRODUCTION                             5

            Previous Investigations                5

            Purpose and Scope of Present Study     6

  IV      DEVELOPMENT OF SEAL MATERIAL             9

            Chemical Grouts Tested                12

            Fillers Tested                        13

            Testing Procedures                    13

            Evaluation of Grout Slurries          14

            Selected Grout Mix                    23

  V       LOCATION AND DESCRIPTION OF TEST SITE   25

            Mine Location and Description         25

            Acid Drainage Characteristics         28

  VI      GROUNDWATER MONITORING STATIONS         35

            Location and Description of
            Monitor Wells                         35

            Sampling Program                      38

  VII     MINE SEALING OPERATIONS                 51

            Double Bulkhead Seals                 51

            Sealing of Air Vent                   54

            Construction of Safety Bulkhead       54

            Injection Nozzle Tests                57

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               CONTENTS (Continued)






Section                                          Page



  VII     MINE SEALING OPERATIONS



            Injection of Gel Material             57



  VIII    ACKNOWLEDGEMENTS                        67
                        VI

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                     FIGURES


                                                 PAGE

1    Arrangement of Proposed Mine Seal            10

2    Injection Procedure for Grout Seal           11

3    Preparation of Test Cubes                    15

4    Unconfined Compressive Strength Test         15

5    Test Cube Storage Controlled Humidity Vault  16

6    Elasticity of Flyash-AM9 Gel                 19

7    Deformation and Failure of Test Cylinder     20

8    Compressive Strength and Volume Changes of
     Flyash-AM9 Gel Immersed in Acid Solution     21

9    Compressive Strength and Volume Changes of
     Mine Refuse-Flyash-AM9 Gel Immersed in
     Acid Solution                                22

10   General Location Map                         26

11   Mine Portal Area                             27

12   Acid Drainage Flow Variation                 29

13   Statistical Variation of Mine Drainage Flow  30

14   Iron, Acid and Sulfate Concentrations in
     Mine Acid Flow                               31

15   Iron, Acidity and Sulfate Loading to Stream  32

16   Location of Wells and Surface Sampling
     Stations                                     36

17   Typical Groundwater Monitor Well             37

18   Double Bulkhead Seals                        53

19   Pressure Gauge-Relief Pipe Installed in
     Place of Old Air Vent                        55
                        Vll

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                FIGURES (continued)


                                                 PAGE

20   Protection of Excavated Mine Entry           56

21   Concrete Bulkhead Details                    58

22   View of Concrete Safety Bulkhead             59

23   Bench-Scale Test of Gel Material             60

24   Angle of Repose Achieved in Lab Test         60

25   Yard Tests of Injection Nozzle                61

26   Slurry Batcher and Weigh Bin                 63

27   Slurry Injection Pipe and Pumping Equipment  64

28   View of Mine Entry through Observation
     Window in Bulkhead                           65
                       Vlll

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                      TABLES


No.

1    Precipitation in Vicinity of Keystone
     State Park                                   33

2    Drilling Logs of Monitor Wells               39

3    Drilling Logs of Existing Park Wells         40

4    Results of Analyses - Sampling Station MD    41

5    Results of Analyses - Sampling Station CR    42

6    Results of Analyses - Sampling Station SP    43

7    Results of Analyses - Sampling Station C-l   44

8    Results of Analyses - Sampling Station C-2   45

9    Results of Analyses - Sampling Station B-l   46

10   Results of Analyses - Sampling Station B-2   47

11   Results of Analyses - Sampling Station B-3   48
                         IX

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                    SECTION I

                  CONCLUSIONS

1.  A slurry consisting of an acrylamide grout with
flyash or neutralized mine refuse as a filler can produce
a stiff gel which may be useful in remote sealing of mine
voids.  The setting time is controllable, and the gel
material is strong, resilient and resistant to attack
by mine acid.

2.  The cost of the materials and placement are at
present higher than that for a concrete seal.  Reductions
are possible through use of a modified mix, possibly with
cement as an admixture, and refinement of injection
procedures.

3.  Dilution and erosion of the gel material prevents
successful formation of a gel seal in high flow mines.
Application of the material and technique to dry or low
flow situations has not been tested.

4.  A concrete seal can be placed between ungrouted
stone bulkheads but settling of the concrete may occur
due to movement of the unconsolidated aggregate,
resulting in increased grout requirement in the subse-
quent pressure grouting operation.
                        -  1  -

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                    SECTION II

                 RECOMMENDATIONS

1.  It is recommended that a groundwater monitoring
program be included in plans for completion of mine
drainage abatement work at the Salem No. 2 Mine at
Keystone State Park, since information is lacking at the
present time regarding the effect of mine sealing on
groundwater conditions, and monitor wells have already
been drilled at the Keystone site.

2.  The location of the mine portal area on State property
which is not developed presently for recreational use,
and the existence of a reinforced concrete safety bulkhead
with view ports and sample valve, make the site ideal for
further test work.  It is recommended that this asset be
explored prior to making a final decision on sealing.
If no testing is foreseen, closing of the drain valve
and sample valve in the bulkhead will make it a concrete
seal.

3.  It is recommended that grout stabilization of the
stone bulkheads be retained as normal procedure in
construction of double bulkhead seals.
                        -  3 -

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                   SECTION III

                   INTRODUCTION

Acid mine drainage is formed by the oxidation of iron
disulfides, usually pyrites, found in association with
coal, when the pyrites are exposed to air and water.
The result is a dilute solution of sulfuric acid and iron
sulfate.  Though there are available treatment techniques,
such as neutralization with lime to adjust pH and precip-
itate iron, it is generally agreed that measures aimed
at preventing the formation of acid drainage hold the
most promise for curbing this source of pollution, par-
ticularly from inactive mines.

There are presently over 3000 miles of streams in
Pennsylvania affected by mine drainage, most of it
originating from abandoned deep mines.  Estimates for
abatement have been set at two billion dollars, and the
major portion of this cost is for source control.  New
techniques are constantly being sought, largely through
research'and development programs sponsored by the U. S.
Environmental Protection Agency and various State
agencies.

Previous Investigations
Techniques which have been investigated for the prevention
of mine acid formation are based on excluding oxygen from
the pyritic surfaces.  This is usually accomplished by
sealing the mine openings to prevent entry of air and to
cause the mine cavity to fill with water.

Seal construction methods tested have included:

a)  placement of an aggregate mass followed by injection
of grout into the aggregate.

b)  placement of a permeable limestone plug for in situ
neutralization and sealing by precipitates.

c)  injection of quicksetting cement grout into expendable
cloth retainers.

d)  formation of forward and rear retaining bulkheads
with a quick-setting slurry followed by injection of a
cement intermediate plug.

e)  placement of forward and rear retaining bulkheads of
aggregate through vertical boreholes, followed by

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stabilization of the bulkheads by injection of grout and
injection of a concrete plug between the bulkheads.

The last method, using two bulkheads of stone with a
concrete plug between them, was recently employed in
sealing over 100 mine openings in Butler County,
Pennsylvania.

Purpose and Scope of Present Study
The work reported herein was undertaken to develop a new
mine sealing technique using a chemical grout with a
filler material as the sealant.  A chemical grout is a
mixture of chemicals which will produce a stiff gel from
a dilute aqueous solution when properly catalyzed.  The
setting time is predictable and controllable, and the
gel material is essentially impermeable.  It was theorized
that a chemical grout with a cheap filler such as flyash
could produce a strong, chemically resistant, impermeable
material suitable for a mine seal, and that by proper
distribution of the grout slurry and control of the gel
time the seal could be built up without the benefit of
retaining bulkheads.

Three major phases of activity were proposed:

1)  Laboratory testing of commercially available grouts
and filler materials to evaluate and select one or more
formulations suitable for the proposed remote mine seal
construction.

2)  Demonstration of a technique for application of the
gel material by sealing three entries of an abandoned
deep mine located in Derry Township, Westmoreland County,
Pennsylvania.

3)  Post-construction surveillance to study the effective-
ness of the seals, and to determine changes in ground-
water quantity or quality resulting from placement of the
seals.

As the work progressed, information developed in each
phase suggested or dictated changes to the original
scope of work in succeeding phases.  Two major changes
were made:

1)  Double bulkhead type concrete seals, with ungrouted
stone bulkheads, were placed in two of the three mine
entries, and only one chemical grout seal attempted.
                        -  6  -

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2)  The post-construction groundwater monitoring program
was postponed.

Although the surveillance program was not performed, a
set of groundwater monitor wells were completed in order
that background information regarding groundwater level
and quality could be developed prior to placement of any
mine seal. . This information, plus data on the flow and
quality of acid drainage from the mine, and stratigraphic
information developed from drilling of the monitor wells,
are included in this report to provide a reference point
for future work if performed at this site.  The need for
information regarding the effect of mine sealing on
groundwater still exists, and it is assumed that this
aspect will be investigated when the sealing of the mine
is completed by injection of grout curtains.
                        - 7 -

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                    SECTION IV

           DEVELOPMENT OF SEAL MATERIAL

Test Objectives
As proposed, the experimental mine seal was to be built
by injection of a gel material with controllable setting
time into the mine cavity through a vertical borehole
from the surface.  The material would be self-supporting,
eliminating the need for retaining bulkheads.  Following
placement of the seal, flyash would be pumped into the
mine side of the seal.  The purpose of this backstop was
twofold.  It was felt that if any leakage occurred flyash
would be carried in suspension into the seal and plug the
leak.  Secondly any leakage that escaped the seal would
be neutralized by the flyash.  A sketch of the proposed
seal is shown on Figure 1.  The safety bulkhead shown is
for protection during development and testing of the seal.

Test work to develop a material suitable for the proposed
mine seal included evaluation of five different chemical
grouts with various combinations of flyash, mine refuse,
sand and gravel as fillers.  Characteristics of prime
importance were a short, controllable setting time,
resistance to chemical attack by mine acid, and sufficient
strength to withstand expected forces.

To avoid formation of a point seal at the injection hole
which would prevent completion of the seal across the
entire width of the mine roof, it was felt that it would
be necessary to direct the grout slurry stream outward
away from the injection hole, and slightly upwards, in
order to build the seal up from the outer extremities
in a concave shape, as shown on Figure 2.  A short gel
time of less than one minute would be required while
building up the seal in order to give an economical angle
of repose and prevent excessive running of the material
along the mine floor.  On the other hand during the final
stages a longer gel time would be required to ensure
dispersion and penetration of the grout into the remaining
crevices.  For maximum flexibility it was decided that the
material should have a highly controllable gel time from
greater than five minutes to a few seconds.

The mine floor at the test site slopes upward from an
elevation of 1016 feet at the entry to a maximum elevation
of approximately 1100 feet.  The maximum hydraulic head
that could develop on a seal therefore is approximately
84 feet, equivalent to 36 psi.  The maximum pressure which
                       - 9 -

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                                                         PLAN
                                                                                             FLYASH INJECTION HOLE
o
 I
                                             SEAL INJECTION HOLE
                                                        ELEVATION
                                        FIGURE  1,    ARRANGEMENT OF  PROPOSED MINE SEAL

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                 INJECTION NOZZLE
                                                               y/^f\
      ELEVATION
     'A1



SECTION
FIGURE  2,    INJECTION  PROCEDURE  FOR GROUT  SEAL

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could be exerted by the overburden of about 30 feet was
estimated at 35 psi, essentially equivalent to the
maximum hydraulic head.  Using a design safety factor of
3, which includes allowances for differences in filler
materials and between laboratory techniques and field
procedures, a compressive strength of 110 psi was selected
as the desired strength of a seal material.

Chemical Grouts Tested
Five commercially available chemical grouts were tested:

     Trade Name                   Type

     Terranier-C                  Phenolic polymer

     AM-9                         Vinyl polymer

     Cyanaloc-62                  Methylol bridge polymer

     Terra Firma                  Chrome lignin

     Geoseal                      Phenolic polymer

Terranier-C is a three-component system consisting of a
principal reactant, a catalyst and a secondary reactant
or crosslinking agent.  The principal reactant is a
phenolic powder which is dissolved in water to make one
solution.  A second solution is prepared containing the
catalyst, sodium dichromate, and a formaldehyde cross-
linking agent.  A polymerization-crosslinking reaction
occurs when the two solutions are mixed.

AM-9 Chemical Grout is a four-component system consisting
of a reactant, catalyst, inhibitor and initiator.  The
reactant is a mixture of two organic monomers, acrylamide
and N,N*-methylenebisacrylamide.  It is a granular material
which is mixed with water to make a solution of desired
strength.  The catalyst is B-dimethylaminopropionitrile
(DMAPN) an alkaline liquid.  The inhibitor potassium
ferricyanide, is added in very small quantities to control
the reaction.

The reaction is triggered by the initiator, ammonium
persulfate, which is a very strong oxidizing agent.  Two
solutions are prepared, one containing AM-9, DMAPN and
potassium ferricyanide, and the other ammonium persulfate.
Gelation occurs by a polymerization-crosslinking reaction
when the two solutions are mixed.
                       - 12  -

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 Cyanaloc-62  consists  of two  components,  a  reactant and a
 catalyst.  The  reactant is a viscous  liquid monomer which
 is  diluted to desired strength  with water.  Polymerization
 occurs  when  a solution of sodium  bisulfate, the  catalyst
 is  mixed with the  reactant.

 Terra Firma  consists  of a lignosulfonate reactant which
 is  catalyzed by sodium dichromate to  form  a chrome lignin
 gel.  Both materials  dissolve readily in water to make
 solutions of desired  consistency  for  application.

 Geoseal is a two-component system consisting of  a phenolic
 reactant and sodium hydroxide catalyst.  The reactant is
 a powder which  is  not dissolved in water,  but added
 directly to  a solution of the catalyst.  Polymerization
 occurs when  the two are mixed in  certain proportions
 which give a pH of between 9.5  and 10.2.

 Fillers Tested
 Flyash was the  first  material considered for testing as
 a filler.  It is cheap and readily available, and was also
 proposed as  a backstop behind the seal because of its
 particle size and  alkalinity.   For the laboratory testing
 800 Ib of flyash was  obtained from Duquesne Light
 Company's Elrama,  Pa.  station.  This  sample of ash had a
 particle density of 2.11 gm/cc  and a  bulk  density of
 1.05 gm/cc,  indicating approximately  50% voids.

Mine refuse  from the  mine site  was investigated  as a
possible filler material since  if successful this would
 also solve,  at  least  partially, the problem of disposal
 of  this unsightly  acid producing  waste material.   The
 loosely compacted, claylike material  was found to have a
particle density of 2.35 gm/cc  and a  bulk  density of
 1.53 gm/cc,  indicating  34% voids.  The material  is acidic
with a pH of approximately 3.0.

Shot gravel  and Ohio  River highway grade sand were tested
briefly and  found  to  offer no advantages over flyash or
mine refuse  as  fillers  for the  proposed seal material.

Testing Procedures
Preliminary  tests were  run with each material to  determine
its particular  characteristics  and suitability as a
potential mine  sealant.  Mix  proportions, strength, gel
time control, and  compatibility with  the fillers  were
evaluated.   Once these  tests were  completed, practicable
grout formulations were selected  for  further testing  of
physical properties and stability.
                      - 13 -

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Test cubes were prepared by mixing selected proportions
of grout, water, filler and whenever necessary inhibitor
or crosslinking agent, for thirty minutes to insure
homogeneity, adding the catalyst or activator, and
pouring the slurry into ASTM standard 2-inch cube molds
shown on Figure 3.  After solidification the cubes were
placed in a storage vault with humidity, controlled at
100% to prevent dehydration.  Two or three cubes were
tested for compressive strength daily for one week.
(Figure 4.)  After the first week cubes were tested once
per week for ten weeks.  Figure 5 shows the controlled-
humidity storage vault.

Resistance to chemical attack from acid mine drainage
was tested by submerging cubes in an acid solution
prepared in the laboratory to simulate the most severe
condition anticipated.  This solution contained 200 ppm
iron, 400 ppm sulfate, and had a pH of 2.0.   Size,
compressive strength, and weight of test cubes were
checked weekly for ten weeks.  The test solution was
examined for discoloration and sediment, and changed
weekly or whenever the pH value reached 3.5.

Evaluation of Grout Slurries
The preliminary tests which were conducted with each
material eliminated some of the materials and certain
combinations of materials from further, long-term testing.
Shot gravel and highway grade sand were tested as fillers
for added mass in combination with flyash and mine refuse.
They were found to yield lower compressive strength than
either flyash or mine refuse alone, and were therefore
eliminated from further consideration as fillers.

Tests with Terra Firma indicated that the gel time could
be effectively controlled only by varying the water
content, which affected the strength of the resultant gel.
Catalyst concentration was dependent on monomer concentra-
tion, which resulted in shorter gel times with increasing
concentrations of the chemical grout.  This system was
also found to be incompatible with flyash due to the
alkalinity which results in precipitation of trivalent
chromium from the dichromate catalyst.

Geoseal is catalyzed by sodium hydroxide at a pH between
9.5 and 10.2.  The caustic not only initiates the reaction
but is also necessary to dissolve the reactant to a true
solution.  Polymerization therefore begins as soon as the
reactant is dissolved in the catalyst solution.  This
necessitates a batch, or one-shot, system of application
                      - 14 -

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FIGURE 3,   PREPARATION OF TEST CUBES
FIGURE
                    M &           IL
       UNCONFINED COMPRESSIVE STRENGTH  TEST
              -  15

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FIGURE 5,   TEST CUBE STORAGE IN CONTROLLED-
            HUMIDITY VAUL1
                - 16 -

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which severely limits control of gel time and precludes
use of a very short gel time.  A two-shot system was
devised by preparing the grout solution with less sodium
hydroxide than is necessary for gelation, and feeding the
remainder of the required caustic in a separate stream.
In theory this seemed feasible, but it could not be made
to work.  The material increased in viscosity but would
not gel.  An increased amount of caustic caused a gel
which was attacked by moisture indicating only a partial
reaction.

The addition of either flyash or mine refuse to a solution
of Terranier-C was found to start gelation immediately,
apparently due to a catalytic effect of polyvalent cations
in the fillers.  It was discovered that a more stable
mixture, usable for 30 to 40 minutes, could be prepared
by adding dry Terranier-C to a flyash slurry or neutral-
ized mine refuse slurry.  Test cubes made in this manner
were found to be hard and brittle with compressive strength
of 70 to 115 psi.  When the cubes were immersed in a
synthetic mine acid solution, the solution turned a dark
reddish-brown color characteristic of the polymer within
one day.

Leaching of color continued for about seven weeks, during
which time the cubes shrank approximately 51 in volume,
but no corresponding loss of strength was detected.  This
loss of  color and shrinkage may indicate a condition
which could eventually lead to failure; however the
immediate problem with use of Terranier-C slurry as a
mine sealant was the initiation of setting by  the fillers.

Cyanaloc-62 is acid catalyzed and therefore will not form
a gel with alkaline flyash.  With mine refuse  as a filler
gelling  is initiated but proceeds very slowly, over a
period of hours.  Test cubes made with a grout mix
consisting of 25 pounds mine refuse  to 1 gallon of one-to-
one by volume Cyanaloc-62 solution had compressive strength
of 560 psi.  However, after five weeks immersion in an acid
solution the cubes began to  show signs of deterioration.
The surface developed a slimy  appearance, and  an 8% weight
loss was measured.  A sudden,  severe loss of strength
occurred during  the eighth week.  At the end of the ten
week test period the strength  loss was 421 due to  attack
by the  acid.  Test cubes stored at  1001  humidity showed
no similar loss  of strength.
 Testing of AM-9 chemical grout was narrowed down  to
 and 15% solutions after preliminary tests.   The exothermic
                         - 17  -

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polymerization reaction released enough heat to cause
cracking of cubes made with a 30% solution, and a 5%
solution produced a very weak gel.  The 20% solution was
eliminated from further testing after three weeks because
indications were that satisfactory strength would be
obtained with a 15% solution.

Both flyash, and mine refuse neutralized with lime or
flyash, were found to be compatible with AM-9.  Test cubes
were made using 10% and 15% AM-9 solutions with the follow-
ing amounts of filler per gallon:

a)  15 Ib flyash

b)  20 Ib mine refuse, 22 gm CaO

c)  7 Ib flyash, 14 Ib mine refuse

All the components of the AM-9 system were easily handled
and readily dissolved to true solutions with viscosities
similar to water.  Mine refuse alone was found to be
unsuitable as a filler because of its acidity, but neutral-
ization to a pH greater than 7 with either lime or flyash
made it an acceptable filler.

Gel time of AM-9 grout mixes was found to be highly
controllable by varying the amounts of catalyst DMAPN,
ammonium persulfate and potassium ferricyanide which
together comprise the catalyst system.

Grout mixes made with AM-9 were found to produce a material
which had a certain degree of elasticity.  Figure 6 is a
plot of observed deformations of cubes made with 10%, 15%
and 20% AM-9 solutions and flyash versus applied compres-
sive stress.  Elasticity of a test cylinder is illustrated
on Figure 7 which shows extreme deformation at failure.
It is believed that this property would be advantageous
in formation of a tight seal, after leakage is stopped by
pressure grouting or by flyash carried in suspension from
the backstop.

Compressive strength and size of test cubes immersed in
an acid solution simulating mine drainage were measured
weekly over an eleven week period.  Figures 8 and 9 show
the compressive strengths and volume changes observed for
test cubes made using AM-9 with flyash alone and a combina-
tion of mine refuse and flyash as fillers.  From the graphs
it would appear that the chemical stability of the cubes
made with a combination of flyash and mine refuse as filler
                       - 18 -

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  160
                           FAILURE
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  CUBE HEIGHT (INCHES)
     2.O    1.9
                                                     1.2
          FIGURE 6,    ELASTICITY OF FLYASH-AM9 GEL
                        - 19 -

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FIGURE 7.    DEFORMATION AND FAILURE OF
            TEST CYLINDER
                -  20  -

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                              TIME (WEEKS)
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        FIGURE 8,
4567


   TIME (WEEKS)
                                                8
                                                        IO    II
                  COMPRESS IVE STRENGTH & VOLUME CHANGES OF

                  FLYASH-AM9 GEL  IMMERSED IN ACID SOLUTION
           12
                             -  21  -

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   TIME (WEEKS)
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                            TIME (WEEKS)

   FIGURE 9,    OPPRESSIVE  STRENGTH & VOLUME CHANGES FOR MINE

               REFUSE-FLYASH-AM9  GEL IMMERSED  IN  ACID SOLUTION
                            - 22  -

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 is better  than  that  of  the  cubes made  with  flyash  alone
 as the  filler.   However it  is  believed that the observed
 variations  in the  strength  and size  of the  cubes made
 with  flyash alone  were  due  to  neutralization of flyash
 particles  by acid  at the surface of  the  cubes rather than
 to reaction with the chemical  grout  material itself, and
 a stable condition would be reached.   When  gels were
 formed  at  a lower  pH by neutralizing the flyash with mine
 refuse  (or  vice  versa)  the  observed  strength and size were
 uniform.

 It should  be noted that strength determinations are made
 by destructive testing  and  that therefore each determina-
 tion  is_made on  a  different cube prepared from the same
 grout mix.   As a result some variation of observed strength
 can be  expected  from cube to cube, regardless of the
 curing  time  or exposure conditions.

 Selected Grout Mix
 Of the  five  chemical  grouts tested only  AM-9 was found to
 meet  all the essential  requirements  of adequate strength,
 good  gel time control and resistance to  mine acid.  The
 compressive  strength  tests  indicated that a 15% AM-9
 solution would be  required,  whether  flyash  or mine refuse
 was used as  the  filler.  On the basis  of  a  seal 12 feet
 wide by 28  feet  long, the cost  of grouting  chemicals alone
 was estimated at $9,000  per seal.  This  was  considerably
 higher  than  original  estimates, which  had been based on
 use of  a cheaper grout  material, and it  appeared that even
 if the material  could be cheaply applied  the overall cost
 would exceed that  of  alternate  sealing techniques.

 It was  agreed in a joint meeting with  the project sponsors
 to proceed with  only  one experimental  grout  seal, and seal
 the other two mine entries  with double bulkhead type
 concrete seals.   Though  the  cost of  the  gel  seal was
 expected to be uneconomical, it was  felt  that testing of
 the injection technique  was  still desirable  since if
 successful, further  research could be  directed to reducing
 the cost of both the materials  and the procedure.

A grout slurry of  15  Ib  flyash  to one  gallon of 15% AM-9
 solution was selected for the  test.  Flyash  offered
 certain inherent advantages  over mine  refuse as a filler
 for the proposed seal.   Screening and  neutralization were
 not required, as with mine  refuse.   Also, since one aspect
 of the proposed  sealing  operation consisted  of pumping
 flyash  into the mine  side of the grout seal, the use of
 flyash  as the filler would  further simplify  materials
                      - 23 -

-------
handling.  The main reason for considering mine refuse
lay in the disposal aspect.  However, in view of the
variable nature and quantity of this material from mine
to mine, any success with use of the material at this
mine would not necessarily be repeatable at another site
                       -  24 -

-------
                    SECTION V

             LOCATION AND DESCRIPTION

                   OF TEST SITE

Mine Location and Description
The site selected for demonstration of the experimental
sealing material and technique is an abandoned deep mine
located in Derry Township, Westmoreland County, Pennsyl-
vania.  Most of the mine, including the portal area, is
located within the Commonwealth of Pennsylvania's
Keystone State Park, approximately 35 miles east of
Pittsburgh.  The location is shown on Figure 10.

The mine, which was known as the Salem No. 2 Mine, covers
approximately 300 acres, sloping upward at an approximate
grade of 31 from an elevation of 1016 feet at the entrance
to approximately 1100 feet at the highest point.  There
were three openings located a short distance below the
spillway of Keystone Lake.  The west opening was the main
portal, while the middle opening served as a fanway.  The
third opening to the east was made by blowing a hole
through the mine roof by an explosive charge set within
the mine.  The mine portal area is shown on Figure 11.

The main entry extends approximately half a mile in a
southerly direction beneath a wooded hill.  Side entries
run east and southwest from the main entry.  Beneath the
crest of the hill the mine lies some 200 feet below the
ground surface.  Other than the portal area the thinnest
cover occurs in the southernmost extremities where the
mine is 40 to 60 feet below the ground surface.

A 12" air vent, located approximately 200 feet up from
the main entrance as shown on Figure 11 was the only
other opening found into the mine.  No instance of
subsidence was known to a former miner who worked in the
mine for 20 years, and no evidence of holes or slumps
were found during field inspections of the mined area.

All three entries were blocked with rubble, and acid
drainage appeared to be coming only from the middle entry
in front of which the water was pooled.  The overflow
drained into the small creek below the Lake.  This creek
enters the Loyalhanna Creek, a tributary of the Allegheny
River, approximately 1-1/2 miles downstream.
                       - 25 -

-------
                      NEW YORK
                    PENNSYLVANIA
               KEYSTONE STATE  PARK

        GREENSBURG
                                -^MARYLAND
                                        >
                                        N
                         VIRGINIA
                                25     5O
FIGURE 10,   GENERAL LOCATION MAP
          - 26  -

-------
                       o
                 FAN WAY
                    OUTCROP

                         SECONDARY PORTAL
                                 EXISTING
                                  FOUNDATIONS
                                               200
                               SCALE  FEET
FIGURE 11,    MINE PORTAL AREA
          -  27 -

-------
Acid Drainage Characteristics^
The acid drainage from the mine was measured and sampled
over a two-year period prior to the start of remedial
activity, from October 1967 to August 1969.  The flow
generally ranged from 20,000 gallons per day (13.9 gpm)
to 160,000 gallons per day (111 gpm), with the lowest
flows occurring in late summer and fall, and the highest
flows occurring usually during the first three months
of the year.  Figure 12 shows the flow variation over
the two-year sampling period.  Flow rates plotted are
single measurements or averages of two to four measure-
ments taken during a given month.  Occasional peak flows
up to 850,000 gallons per day (590 gpm) were reported;
however ninety percent of the time the flow was less than
160,000 gallons per day, and half the time less than
60,000 gallons per day, as shown by the statistical
analysis of all recorded flow measurements, Figure 13.

Concentrations of iron, acidity and sulfate in the mine
drainage over the sampling period are shown on Figure 14,
and the corresponding loadings in pounds per day are
shown on Figure 15.  Again the values plotted are either
single determinations or averages of two to four samples
taken during a given month.  The total pollution load due
to the mine drainage is related primarily to the flow
quantity and only secondarily to contaminant concentra-
tions.  Peak loads generally coincided with high flow
periods.

Inasmuch as the mine drainage flow, and consequently the
pollution load, may be a function of the wetness or dry-
ness of any given period, an evaluation of abatement
measures should take into consideration the amount of
precipitation in the area over the study period.  The
terrain above the mine is conducive to fairly rapid
surface runoff on all sides of the rounded hilltop.
However infiltration that does occur will find its way
into the mine cavity which, by virtue of its areal
extent and the relatively unimpeded routes it provides,
should be the principal flow control for subsurface
water.  Precipitation data for the Keystone State Park
area for the years 1967, 1968 and 1969 is given on Table 1.
                      - 28 -

-------
t-o
VQ
        600,000
        500,000
        IOO.OOO
                0   NDJFMAMJJASONDJFMAMJJA
                   1967
1968
                                                                                     1969
                                 FIGURE 12,    ACID DRAINAGE  FLOW VARIATION

-------
w
o
            500,000

            400,000


            300.00O



           200,000 •
 100,000
  90,000
  80,000
^ 70,000

& 60.0OO

* 50,000

"• 40,000
            30,000  •
             20,000
             10,000
                                   	1      I    »	1—I	1	1	*—
                                           10     2O  30  40  50 60  70  80
                                   PERCENTAGF OF TIME EQUAL TO OR LESS THAN
                                                                                         90   95
98  99
                              FIGURE  13,   STATISTICAL VARIATION OF MINE DRAINAGE  FLOW

-------
        3000
      -2000
       j IOOO
              0  N
           	1967
D   J
FMAMJJASONDlJFMAMJJA

   	     1968	^	"969	
        1000
       Q_
       CL
         800-
         600-
       g
       o 400
i         200
              ONDIJFMAMJJASOND
           —	1967	4—
                      1968
                                                  JFMAMJJA
                                                                                 1969
         4OO
       Z
       a 300
         200
          IOO
              ONDIJ    FMAMJ   JASONO
                1967 	4.
                      1968
                                                  J   FMAMJJA
                                                                                 1969
                 FIGURE  W,     IRON,  ACID  &  SULFATE  CONCENTRATIONS  IN  MINE ACID FLOW

-------
              TO 3347
ts>

I
 1600
 1400
o
x.
c/>
CD
s
£ 800

fi
_/

 600
H
Q
IAOO
  200
                                                                                  \
                                                                                    \
       ON   D '  J   F   MA   M   J
                                                   A   S   0   N   D
         (967	«L-
                                          1968
F   M   A   M   J   0   A
       1969
               FIGURE 15,    IRON,  ACIDITY & SULFATE  IN  MINE ACID FLOW

-------
                              TABLE I




                   PRECIPITATION IN VICINITY OF




                        KEYSTONE STATE PARK




 (Average of Measurements at Blairsville, Vandergrift  & Derry)




                      Inches of Precipitation
1967
Jan.
Feb.
March
April
May
June
July
Aug.
Sept.
Oct.
Nov.
Dec.
ANNUAL

1.28
2.82
6.59
4.55
4.21
1.69
5.02
3.88
3.50
3.02
2.82
2.46
41.84
1968
Jan.
Feb.
March
April
May
June
July
Aug.
Sept.
Oct.
Nov.
Dec.


2.47
1.25
3.39
2.05
6.88
1.61
4.15
4.69
2.80
1.93
3.85
3.80
38.87
1969
Jan.
Feb.
March
April
May
June
July
Aug.
Sept.
Oct.
Nov.
Dec.


2.70*
1.03*
1.45*
4.54*
2.57*
3.64*
6.01
2.16
2.15
2.81
3.12
4.93
37.11
*  No data from Derry.  Donegal data used.
                              -  33  -

-------
                    SECTION VI

         GROUNDWATER MONITORING STATIONS

Location and Description of Monitor Wells
In order to provide the means of evaluating the impact
of the sealing of the mine on groundwater in the area, a
set of groundwater monitor wells were drilled in the
locations shown on Figure 16.

Well A-2, located on top of the hill above the mine, was
drilled to a depth of 200 feet, or to approximately 15
feet of the top of the mine, in order to evaluate the
dewatering effects on the strata comprising the hill
above the mine by the mined area.  Two wells were origi-
nally proposed, one on each of the two rounded hilltops;
however Well A-l was later eliminated.

Wells B-l, B-2 and B-3 were drilled for the purpose of
monitoring the groundwater in the immediate surrounding
area in order to determine its response to the inundation
of the mined area.  Drilling depths were 230 feet, 225
feet and 200 feet respectively.

Wells C-l and C-2 near to Keystone Lake and Creek, were
drilled to 100 feet below their bottom elevations in order
to give warning of possible deep flow lines and inputs of
mine drainage polluted groundwater through the bottom
of the lake or stream as a response to vertical pressure
buildup as the mine fills.  Depth of C-l is 156 feet, and
the depth of C-2, 110 feet.

All of the monitor wells are 6 inches diameter with 6-1/4"
I.D. casing extending from 1 foot above grade to below
bedrock.   A screwed cap is provided on each well to
prevent entry of foreign matter.  Ten feet high markers,
consisting of 6 inch diameter plates mounted on 1-1/2"
diameter pipe, were erected at each monitor well to
facilitate location and identification.  A typical monitor
well is shown on Figure 17.

Water was encountered during drilling of all the wells
except well A-2 located on the crest of the hill.  In
general the wells at higher elevations such as B-l and
B-2 yielded small quantities of water.  At wells C-l and
C-2 which are at a low elevation and lie close to the
lake and stream, water was encountered at two separate
elevations.
                       -  35  -

-------
< '
 •
                                                                                EXISTING WATER WELLS
                    //  '   '/ ' '  x
               V A  !  M x
                ^f     / o
                        / ;-'
                                                                                NEW MONITOR WELLS AND


                                                                                SAMPLING STATIONS
                    /



                   FIGURE 16,    LOCATION OF  WELLS AND  SURFACE SAMPLING STATIONS

-------
              MARKER



c

+1
o


1
\ \ ^ <-\
V

>









-<:
y







I^^-G-DIA.
j 	 ROUND ROD WELDED TO CAP
/-I>2"DIA.
^ J
i 	 1_, ^_ or.DPurpn PAD






-

<
*
<



;


^c — tc — u — c




r^"
U-^H
--O


1 §
1
! _^J

«
(5 ^
^
S r
S

^ ;
'o
1
,
., •
1 „
' ^^— &/4 I.D. CASING
/^— ROCK
•


6_^- — 6"DIA.HOLE



FIGURE 17,   TYPICAL GROUNDWATER MONITOR WELL
                  37

-------
The drilling logs of the monitor wells are tabulated on
Table 2, and logs of water wells previously drilled in the
park on Table 3, as an aid to defining the stratigraphy of
the area for future interpretation of groundwater changes
resulting from water buildup in the mine.  The locations
of the existing water wells are shown on Figure 16.  Well
No. 4 was not completed.

Sampling Program
In addition to the groundwater monitoring wells, surface
sampling stations SP and CR were established upstream and
downstream of the point where the mine drainage entered
the creek and at the mine opening itself, designated
station MD.  Location of these sampling points are shown
on Figure 16.

Since the surveillance program has been postponed, there
is of course no data reflecting a change in the hydro-
geological environment due to mine water impoundment.
However, samples were taken from the monitor wells and
surface sampling stations on a more-or-less weekly
schedule over a two-month period prior to the scheduled
sealing, in order to establish background data on water
quality and level.  These samples were analyzed for pH,
total iron, sulfate, acidity and total solids.  On each
sampling tour the water level in the monitor well was
measured.

The data from the "pre-sealing" sampling program is
presented on Tables 4 through 11.  At stations C-l and C-2
samples were taken from two depths approximately coincident
with the levels at which water was encountered during
drilling.  Monitor well A-2 was dry throughout the sampling
period.

Some observations concerning the analytical data can be
made.   Iron concentrations were generally higher in the
samples taken at the higher level in wells C-l and C-2
indicating possible influence of mine drainage.  Total
solids  concentrations in the samples taken January 20
at Sta. C-2 showed a sudden three-fold increase, but
there was no corresponding increase in acidity, iron or
sulfate concentration.  On the contrary  there was a
reduction in acidity.   It is believed that this sudden
change  in groundwater quality was due to contamination
by a cement-flyash grout mixture that was pumped into the
west entry the preceding week.  This reinforces the
evidence of contamination of well C-l by water from the
mined area.
                       -  38  -

-------
          TABLE 2




DRILLING LOGS OF MONITOR WELLS
Well A- 2
Strata
D«pth

0-4
4-21
21-33
33-49
49-56
56-67
67-83
83-92
92-94
94-94)4
94K>107
107-123
123-145
145-146
146-148
148-151
151-200




Descrip-
tion

Clay
Sand Rock
Shale
Sand Rock
Shale
Sand Rock
Shale
Sand Rock
Shale
Coal
Fire Clay
Sandy Shale
Sand Rock
Shale
Coal
Sandy Shale
Solid Rock




Well B-l
Strata
Depth

0-10
10-14
14-35
35-37
37-55
55-81
81-124K2
124)4-125
125-127
127-134
134-141
141-156
156-168
168-169'/2
169H-206
206-215
215-217
217-222
222-230

Descrip-
tion

Sand
Clay
Shale
Sand Rock
Shale
Sand Rock
Shale
Coal
Fire Cloy
Shale
Sand Rock
Sandy Shole
Sand Rock
Coal
Sand Rock
Sandy Shale
Sand Rock
Sandy Shale
Sand Rock

Water at 125'
Well B-2
Strata
Depth

0-18
18-61
61-63
63-66
66-77
77-120
120-123
123-126
126-146
146-159
159-183
183-186
186-190
190-192
192-213
213-218
218-224
224-225


Descrip-
tion

Clay
Shale
Coal
Fire Clay
Sandy Shale
Sand Rock
Coal
Fire Clay
Sand Rock
Shale
Sand Rock
Shale
Coal
Fire Clay
Sand Rock
Shale
Coal
Fire Clay


Water at 176'
Well B-3
Strata
Depth

0-1
1-16
16-21
21-26
26-28
28-39
39-43
43-46
46-52
52-79
79-98
98-102
102-104
104-106
106-110
110-111
111-126
126-135
135-140
140-200
Descrip-
tion

Topsoil
Clay
Shale
Solid Rock
Shale
Solid Rock
Coal
Fire Clay
Solid Rock
Shale
Solid Rock
Shale
Coal
Clay
Solid Rock
Coal
Solid Rock
Shale
Coal
Shale
Water at 49 '
Well C-l
Strata
Depth

0-9
9-45
45-49
49-55
55-62
62-72
72-85
85-90
90-91
91-100
100-123
123-134
134-137
137-151
151-155
155-156




Descrip-
tion
Topsoil
&Clay
Sand Rock
Coal
Shale
Sand Rock
Shale
Sand Rock
Sandy Shale
Coal
Shale
Sand Rock
Shale
Sandy Shale
Shale
Coal
Shale




Water at 49', 140'
Well C-2
Strata
Depth

0-8
8-10
10-28
28-30)4
30)6-34
34-38
38-40
40-45
45-70
70-75
75-84
84-93
93-95
95-104
104-108
108-110




Descrip-
tion
Topsoil
&Clay
Shale
Solid Rock
Coal
Shale
Sand Rock
Shale
Limestone
Shale
Sand Rock
Shale
Sand Rock
Shale
Sandy Shale
Sand Rock
Shale




Water at 28 ', 65 '

-------
                                                               TABLE 3
                                                   DRILLING LOGS OF EXISTING PARK WELLS
Well No. 1
Strata Dt pth
0-18
18-30
30-32
32-70
70-75
75-80
80-85
85-110
110-165
165-170
170-210
210-245
245-270
270-300



Description
Clay
Gray Shale
Coal
Gray Shale
Gray Sand
Coal
Gray Shale
Gray Sand
Gray Shale
Coal
Gray Sand
Gray Shole
Gray Sand
Gray Shale
and Sand


Wafer at 50', 110', 245'

Well No. 2
Strata Depth
0-9
9-11
11-25
25-37
37-50
50-52
52-55
55-60
60-70
70-75
75-80
80-82
82-130
130-135
135-145
145-170

Description
Clay
Dark Shale
Gray Shale
Dark Shale
Gr. Sand Rock
Coal
Gray Shale
Sand Rock
Gray Shale
Sand Rock
Gray Shale
Black Shale
Gray Shale
Sand Rock
Sandstone
Gray Shale

Water at 37', 40', 55',
105', 135', 160'
Well No. 3
Strata Depth
0-10
10-50
50-60
60-65
65-115
115-120
120-125
125-130
130-150
150-155
155-175
175-205
205-210




Description
Cfay
Gray Shale
Gray Sand
Coal
Gray Send
Gray Shale
Gray Sand
Coal
Gray Shale
Coal
Gray Shale
Gray Sand
Gray Shale




Water ol 25', 150', 175'

Well No. 5
Strata Depth
0-20
20-65
65-80
80-85
85-87
87-90
90-100
100-110
110-140
140-150
150-160
160-185
185-190
190-200
200-220
220-295
295-300
Description
Clay
Gray Shale
Gray Sand
Gray Shale
Gray Sand
Coal
Gray Shale
Gray Sand
Gray Shale
Gray Sand
Coal
Gray Shale
Coal
Gray Shale
Gray Sand
Gray Shale
Gray Sand
Wafer af 35', 80', 200'

Well No. 6
Strata Depth
0-15
15-40
40-47
47-48
48-50
50-70
70-90
90-100
100-105
105-110
110-135
135-140
140-150
150-175
175-190


Description
Cloy
Gray Shale
Gray Sand
Coal
Gray Shale
Gray Sand
Gray Shale
Gray Sand
Brown Shale
Coal
Gray Shale
Coal
Gray Shale
Gray Sand
Gray Shale


Water at 30', 45', 65',
100', 115'
o
 I

-------
PH

Iron

Sulfate

Acidity ("hot")

T. Solids
                                                  TABLE 4
                                            RESULTS OF ANALYSES

11-19-71
2.81+
105
1930
535
8l?2

11-30-71
2.62
3^8
1000
603
2811
SAMPLING
12-8-71
2.73
67.0
650
Uo?
1281
STATION MD
12-13-71
2.72
75
650
U25
1561

12-21-71
2.71
57.2
666
teu
1371

1-6-72
2.82
62. U
5M*
369
2025

1-13-72
2.86
56
532
1*60
1179

1-20-72
2.88
56.5
600
U58
1360

1-28-72
2.91
146.2
620
1*85
8691*
            All concentrations in parts per million

-------
                             TABLE 5
                      RESULTS OF ANALYSES




1
to
1



PH
Iron
Sulfate
Acidity

T. Solids

11-19-71
6,27
5.29
23.5
7.38

239

11 -30 -71
7.62
8.3
16
1.6

279
SAMPLING
12-3-71
7.20
5.08
3U.O
3.1

116
STATION CR
12-13-71
7.^7
6.6
51
1.6

189

12-21-71
7.56
3.8
U5
l.U

10U

1-6-72
5-85
2.2
26
11.7

156

1-13-72
6.73
2
3^
6.1

158

1-20-72
7.26
3.5
te
3.6

206

1-28-72
6.83
2.6
33
6.3

141
All concentrations in parts per million

-------
                             TABLE 6
RESULTS OF ANALYSES
pH
Iron
Sulfate
Acidity
T. Solids
11 19-71
7.50
O.Ul
26.5
2.0
98
11-30-71
7.2U
0.8
26
3.3
109
SAMPLING
12-8-71
7-29
2.U6
26.5
3-1
101
STATION SP
32-13-71
7.96
U.3
16
l.l
86
32-21-71
7-93
1.1*
15
1.2
78
1-6-72
7.85
ND
16
1.3
96
1-13-72
7.26
1
17
3.2
lUi
1.20-72
7.9^
ND
16
1.3
99
1.28.72
6.80
1.0
15
10.9
179
All concentrations in parts per million

-------
                                      TABLE  7
RESULTS OF ANALYSES
SAMPLING STATION C-l
11-19-71 11-30-71 12-8-71 12-13-71 12-^1-7:
Water Level (ft)
PH

Iron

Sulfate

Acidity

T. Solias

(u)
(L)
(u)
(L)
(u)
(L)
(u)
(L)
(u)
(L)
101*
7.68
7.63
0.93
1.58
12.0
10.5
7.0
5.75
29U
387
10U3 10146
8.11 8.01
7.87
1.8 12. U
12.1*
15 15.7
12.8
0.6 1.2
U.2
283 385
U07
10U7
8.51
8,53
10.7
8.6
ND
5
U.2
3.8
556
358
10UU
8.U9
8,U2
12.5
8.1
2
U
2.6
2.U
525
373
I 1-6-72
10U3
7.67
7.95
9.0
5^
2
2
7.9
3.8
357
3^6
1-13-72
10U3
7.76
7.57
12
8
5
u
7.U
n.5
381
U35
1-20-72
10UU
8.5U
8.35
9-1
6.9
2
2
5.0
ND
356
328
1-28-72
10UU
7.87
8.31
8.0
5.8
u
U
U.6
5.5
313
312
All concentrations in parts per million

(U)  Sample taken at upper elevation, approximately 1030*
(L)  Sample taken at lower elevation, approximately
 ND  None Detected

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                                      TABLE 8
RESULTS OF ANALYSES
SAMPLING STATION C-2
Water Level (ft)
pH (U)
(L)
Iron (U)
(L)
in Sulfate (U)
(L)
Acidity (U)
(L)
T. Solids (U)
(L)
11-19-71
1011
7.2'i
7.69
3.59
3.^9
29-7
18.5
9-25
3.75
251
U58
11-30-71
1011
7.02
8.26
10. U
6.7
33
11
10.8
O.U
209
193
12-8-71
1010
6.76
7.57
10.3
7-77
31.0
19.2
U.o
7.3
183
302
12 -13 -71
1012
8.50
8.89
12.7
8.8
16
5
1.2
8.0
238
U6U
12-21-71
1010
8.M4
8.80
10.8
7.0
16
5
0.9
7.1
173
269
1-6-72
1012
7.09
7.55
lU.O
8.6
16
6
11.2
10.8
308
369
1-13-72
1032
6-93
7.^7
15
9
lU
8
22.8
11.0
320
352
1-20-72
1013
8.60
8.73
15.8
12.5
5
5
6.2
6.0
983
911
1-28-72
1013
8.55
8.83
10.8
8.5
3
h
3.5
3.8
783
656
All concentrations in parts per million

(U)  Sample taken at upper elevation, approximately 990'
(L)  Sample taken at, lower elevation, approximately 955'
 ND  None Detected

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                                                           TABLEJ)
                                                     RE S ULTS OF ANAL YSE S
CTv
Water Level  (ft)

pH

Iron

Sulfate

Acidity

T. Solids
SAMPLING STATION B-l
12-13-71
1219
8.6**
9-9
13
2.8
651
12-21-71
1217
8.5U
fl.7
16
2ji
6U9
1-6-72
1218
7.78
3.3
15
2.9
1*39
1-13-72
1219
7.53
6
13
l'.3
652
1-20-72
1218
8.55
5.8
11
2.1
J*U3
                                   All  concentrations  in parts ner million

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                                                 TABLE  10
Water Level (ft)




pH




Iron




Sulfate



Acidity



T. Solids
RESULTS OF ANALYSES
SAMPLING STATION B-2
11-30-71
1177
7.19
U.2
2»*
5-1
533
12-8-71
1177
7.15
6.60
2U.2
17.6
U22
12-13-71
1171*
8.08
7.3
7
1.0
UU9
12-21-71
1179
8.05
7.8
7
1.1
i+17
1-6-72
1183
7.50
6.1
7
16.0
555
1-13-72
1188
7.21
5
8
28.9
393
1-20-72
1189
8.10
7.8
7
1.3
UoU
                          All concentrations in parts per million

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                                                        TABLE 11
CO
RESULTS OF ANALYSES
SAMPLING STATION B-3

Water Level (ft)
pH
Iron
Sulfate
Acidity
T. Solids
11-19-71
10U9
6.7^
2.79
11.0
10.75
260
11-30-71
1055
7.93
ND
15
0.8
350
12-8-71
1056
6.33
6.1*9
2U.7
lU.9
519
12-13-71
1055
8.27
11.3
6
0.6
503
12-21-71
1057
8.10
12.5
5
1.6
U99
1-6-72
1059
6.50
U.9
13
18.1
325
1-13-72
1060
6.6k
26
9
16.8
501
1-20-72
1060
8.2k
16.9
U
0.6
Ma
1-28-72
1060
7.67
13.U
7
2.3
23U
                           All concentrations  in parts  per million

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There was a noticeable decrease in iron, sulfate, acidity
and total solids concentrations in the mine drainage
after the first two sampling tours.  This may have been
due to dilution from increased runoff resulting from
frequent rains during this period, or to changes in the
mine environment brought about by the construction
activity, or both.  Excavation of the fanway released
impounded acid water and permitted this corridor to
drain freely.
                       - 49 -

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                   SECTION VII

             MINE SEALING OPERATIONS

The decision to place two double-bulkhead concrete seals
and only one experimental chemical grout seal was prompted
by the higher-than-expected cost of the grouting materials
which were determined by laboratory testing to be suitable
for the proposed mine sealing method.  However, there were
other areas in which it was felt benefits could be derived
by substitution of the concrete seals at this site.

1.  The potential hydraulic head that could develop on the
seals if the mine filled to its highest level was 84 feet.
The maximum head on any existing seal of this type was
about 35 feet.  Therefore, it was possible that the oppor-
tunity would be afforded to evaluate the double bulkhead
concrete seals under a higher pressure than that to which
they had previously been exposed.

2.  Installation of previous double bulkhead seals
included grout stabilization of the retaining stone bulk-
heads prior to placement of the concrete seals.  It was
believed that this step could be eliminated.  Installation
of double bulkhead concrete seals at the Keystone State
Park test site permitted testing this modification of the
construction procedure.

Double Bulkhead Seals
The double bulkhead concrete seals were installed in the
east and west mine entries.  The bulkheads are normally
constructed by injecting coarse aggregate through vertical
drill holes across the mine corridor and vibrating the
material so that an alignment of intersecting truncated
cones are formed with a minimum of four feet diameter
contact zone at the mine roof.  Grout is injected into
the bulkheads and then a concrete plug is injected into
the space between the bulkheads.

Six-inch diameter injection holes were drilled across the
east and west entries for placement of the bulkheads and
concrete seal.  The alignment of the holes was not exactly
perpendicular to the bearing of the entries because they
were drilled before the middle entry was opened to permit
a survey.  This however would be the rule rather than the
exception since accurate mine maps are seldom available
and openings often have to be established by exploratory
drilling.  From the drilling logs the east and west entries
were estimated to be 12 to 14 feet wide and from 4 to 8
feet high depending on exact location.
                      - 51 -

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One hundred tons of aggregate, Pennsylvania Department of
Highway 2-B size and grading  (l/2"+0 , were placed and
vibrated in the west entry through the applicable drill-
holes, sixty tons for the forward bulkhead and forty tons
for the rear bulkhead.  In the east entry the forward
bulkhead consisted of seventy-seven tons and the rear
bulkhead sixty-eight tons of aggregate.

Attempts at taking pictures in the mine through boreholes
to examine the bulkhead location and assess the integrity
of the stone bulkheads were unsuccessful due to water and
high humidity which resulted in condensation on lens
surfaces.  A considerable amount of water was backed up
in the west entry, and attempts to dewater the area by
excavation in front of the entry, and by pumping were not
completely successful.

It was decided to inject the concrete seals without
dewatering.  A laboratory test showed that the concrete
would set satisfactorily when poured into an acid solution
simulating the mine acid, and based on the dimensions
of the mine cavity and the quantities of stone placed it
was concluded that in all probability the bulkheads were
satisfactory.  Eighteen cubic yards of concrete were
poured in the east entry and thirty-five cubic yards in
the west entry.  The completed seals are illustrated in
Figure 18.

The center plug areas of the seals were pressure grouted
through drill holes extending entirely through the concrete
plug to below the mine floor.  A total of 1472 cubic feet
of flyash-cement grout were injected in the east entry
seal.  For grouting of the west seal calcium chloride was
added as an accelerator because some seepage was noted
below this entry indicating possible water movement through
the seal area.  A total of 3584 cubic feet of grout were
injected at this location.

The total cost for both double bulkhead seals in place
is estimated at $30,000.  This includes the grouting of
the center plugs, but no curtain grouting.

Test holes were drilled in the center plug areas of the
double bulkhead seals downstream of the injection holes
five months after the seals were placed.  These holes were
cored all the way through the seals to the mine floor, and
revealed no discontinuity of material in either of the
two concrete seals, therefore it is apparent that the mine
entries are completely filled in the area of the seals.
Core recovery, from the mine roof to the mine floor, was
                      - 52 -

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  GRADE
  GRADE
.PORTAL
                               EAST ENTRY
                        l4'-0"t
                                                      - 6  DIA.DRILL
                                                         HOLE (TYP.)
             14'-0"t
                                                         foSftMsA S,'//
V*35C.Y. CONCRETE ^a
                               WEST FNTRY
               FIGURE 18,    DOUBLE BULKHEAD  SEALS
                            -  53 -

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    for the east seal and 40% for the west seal.  This
represents a relatively high loss but is not unusual for
this type of application and may indicate only that
portions of the cement matrix are weak enough to be shat-
tered by the core drilling.  The effectiveness of the
total mass as a seal would not necessarily be impaired.
Pressure testing would be required in order to assess
the effectiveness of the material within the seal area as
a hydraulic seal.

The boring logs showed that settling of the concrete
took place after the seals were poured.  This could have
been due in part to displacement of gob and migration of
material into or through the stone bulkheads as well as
movement of the bulkheads themselves.  In the east seal
nine inches of flyash-cement grout were found above the
concrete, and in the west seal twenty-two inches of grout
were recovered from between the mine roof and the concrete
seal.  This grout usage offset any saving that was realized
by elimination of the grouting of the bulkheads, therefore
there appears to be no advantage to elimination of this
step in the construction procedure.

Sealing of Air Vent
The existing 12" diameter vent pipe, located on the first
cross connection between the main entry and the fanway as
shown on Figure 3, was removed and replaced with a 4-inch
stainless steel pipe which was concreted in place.  This
pipe was fitted with a pressure gauge for possible use in
monitoring the progress of water buildup in the mine after
it is sealed.  The gauge is mounted on a flange which may
be removed entirely for sampling or measuring water level
when this is below the gauge elevation.  A 4" valve is
also provided to serve as a possible relief device should
it become necessary to lower the water level in the mine
after it has exceeded the elevation of the valve.  A
sketch of the gauge-relief pipe is shown on Figure 19.

Construction of Safety Bulkhead
Because of the experimental nature of the proposed chemical
grout-flyash seal, a reinforced concrete safety bulkhead
was constructed in the middle entry which was selected
for the test of the material.  The entry, which served as
the fanway when the mine was worked, was reestablished by
excavation, and a diversion channel was cut to divert the
drainage directly to the creek.  For protection and
security of the opening, a wooden entry way was built
twelve feet out from the face of the mine, with cyclone
fence double gate at the end.  The entrance is shown on
Figure 20.
                       - 54 -

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 4"S.S.PIPE
                   *.r •
                   •;.«.'
                   XI1.'
                               — PRESSURE GAUGE
4" EMERGENCY RELIEF PLASTIC
        BALL VALVE
                           CONCRETE
                                  L
                                     MINE ROOF
                          I2"± 0. D. RETAINER PLATE WELDED
                                    TO 4" PIPE
FIGURE  19,    PRESSURE GAUGE-RELIEF PIPE INSTALLED

               IN PLACE OF OLD  AIR VENT

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FIGURE 20,   PROTECTION OF EXCAVATED MINE ENTRY
                       - 56 -

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The reinforced concrete bulkhead was located approximately
18 feet in from the face of the mine.  A drainage channel
and 6" drain pipe was installed in the mine floor to permit
free drainage of the mine while the bulkhead was being
built.  A 4-inch diameter stainless steel pipe with plastic
ball valve was located approximately two feet up from the
mine floor to permit sampling, and to aid in the sealing
operation special plexiglass windows were included for
observation and light insertion.  Bulkhead details are
shown on Figure 21.  A photograph of the completed
installation is shown on Figure 22.

Injection Nozzle Tests
Preliminary tests in the laboratory, Figures 23 and 24,
showed that an AM9-flyash slurry consisting of 15 pounds
of flyash per gallon of 15% grout solution could easily
form a self-supporting mass with 20 to 25 degrees angle
of repose, but that proper distribution of the slurry was
essential to establishment of complete closure at the mine
roof.  It was felt that this distribution could be accom-
plished through a single injection hole by use of a
nozzle that would direct the slurry outward and slightly
upward so that the seal is built up from the outer
extremities as previously illustrated in Figure 2.

Tests were conducted with an injection nozzle consisting
of two 3/8" nozzles at 180 degrees, inclined upward at
30 degrees, from the horizontal.  To avoid plugging of the
injection piping when using short gel times the initiator
was added just ahead of the nozzle.  As a result of the
tests it was concluded that a satisfactory distribution
could be achieved with the nozzle, and that mixing of the
ammonium persulfate solution with the grout slurry just
ahead of the nozzle was adequate to produce a controllable
gel.  The nozzle tests are illustrated on Figure 25.
Pumping of the grout slurry was not continued to build up
a plug in the test area in view of the high cost of the
grout materials.  It was hoped that with the viewing
ports built into the reinforced concrete safety bulkhead
the progress of the actual seal placement could be
monitored closely enough so that precise step by step
procedures would not have to be previously determined by
large scale testing.

Injection of Gel Material
Due to cold weather injection of the AM9-flyash grout was
delayed several weeks.  It was decided to wait until at
least two days of above freezing temperatures were
reasonable assured before attempting to place the seal.
                       - 57 -

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                                                   DEEP DRAINAGE TRENCH
             6 DIA.SCH.IO S.S.PIPE
             (TYPE 3O4) ENCASED IN
             CONCRETE.
4"DIA.SCH.IO S.S.PIPE ft
4"FLGD. PLASTIC BALL
VALVE FOR SAMPLING FLOW
a EMERGENCY RELIEF.
I
                4'-6
                                  (MINE CLEARANCE)
                             PLAN
                                                   -6"DIA.INJECTION HOLE
                                                     TO GRADE

  s
  (0
         1  I2"SQ.PLEXIGLASS WINDOW
           6"DIA.PLEXIGLASS WINDOWS

                              ELEVATION
                                                  SLIP ON FLANGE WITH
                                                  BLIND FLANGE
               FIGURE  21,     CONCRETE  BULKHEAD
                             -  58  -

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                                        .
                                          -
                                           -'  »•"• •
                                          *•*"


                                                        "»
FIGURE 22,    VIEW OF CONCRETE SAFETY  BULKHEAD
                        -  59  -

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FIGURE 23,    BENCH SCALE TEST OF GEL MATERIAL

                                               If
FIGURE 24,   ANGLE OF REPOSE ACHIEVED  IN LAB TEST
                       -  60  -

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                                   .  r
                                   «     -
                                                       \

,  •
                                 .'«*-?
                                       p

FIGURE 25,   YARD TESTS OF  INJECTION NOZZLE

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On February 28, 1972, with a warm trend predicted,
preparations were made for the grouting operation.  The
next day, final tests were run to check out equipment
and determine approximate proportions and gel times, using
water from the site at prevailing temperature and flyash
from the batch to be used in the actual grout mix, and on
March 1 injection of the grout into the mine began.  Flyash,
AM-9 and catalyst DMAPN were batch mixed in a 2500 gallon,
two-compartment slurry batcher, shown on Figure 26 with a
material weigh bin above it.  From the batcher the slurry
was pumped to a small hopper feeding progressive cavity
type injection pump of 30 gpm capacity.  Ammonium persul-
fate, the reaction initiator, was fed by a smaller pump
into the injection pipe just ahead of the nozzle.  The
injection pipe and pumps are shown on Figure 27.

Lights were inserted in the 6" diameter ports in the
safety bulkhead for illumination of the mine cavity, but
visibility was poor due to condensation and obstructions
which blocked view of the injection point.  Figure 28
shows the view through the bulkhead.

The injection nozzle was oriented to direct the slurry
stream toward the walls and the grout pumped at a rate of
30 gallons per minute with a gel time of approximately
15 seconds.  The anticipated result of this procedure was
that a wedge shaped mass would be built up on each side
of the mine corridor, starting at the walls and sloping
downward toward the middle where the mine drainage was
observed to be flowing.  With proper control of the gel
time it was hoped that the two wedge shaped formations
could be gradually extended into the drainage channel
eventually damming the flow and causing it to spread out
behind the grout dam.  However, this was not successful.
Observation of the drainage from the mine indicated that
much of the grout material was being lost.  The gel time
was decreased from fifteen seconds to as low as five
seconds with no success in stopping grout loss.  A
satisfactory gel was apparently achieved on both sides
of the entry, as evidenced by inability to remove the
catalyst injection hose when the operation was terminated,
but the flow in the middle of the mine floor was too high
to permit a gel to form.

The flow from the. mine measured by a v-notch weir was
found to be approximately 150 gallons per minute.  This
was considerably higher than the 40 to 50 gallons per
minute measured a week earlier and was due to runoff
brought about by the sudden onset of very warm weather.
The air temperature rose to above 70°F during this period.
                       -  62  -

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FIGURE 26,   SLURRY BATCHER AND WEIGH BIN
                 - 63  -

-------

FIGURE 27,   SLURRY INJECTION PIPE AND PUMPING
             EQUIPMENT
                   -  64  -

-------
FIGURE 28,  VIEW OF MINE ENTRY THROUGH
            OBSERVATION WINDOW IN BULKHEAD
                -  65  -

-------
Due to the high flow much of the grout was diluted to the
point where it failed to gel, and the material that did
gel at the edge of the flowing water was washed away.
Some gelled material was collected outside the mine
entrance indicating that some of the grout had indeed
formed weak gels which were transported away by the flow-
ing water.

In view of the previously established high cost of grout
materials and the difficulties experienced in applying
the injection technique with the high mine flow, the
decision was made after consultation with State and
Federal project sponsors, to terminate the test.  It was
felt that the method may be successful in low flow
situations, and with higher injection rate to minimize
dilution and erosion of the grout, but the cost remained
prohibitive.

Acid drainage abatement activities and sampling at the
mine site have been interrupted to permit compilation and
review of all information relative to the project prior
to completion of the work.  In order to retain the possi-
bility of using the mine entry for further experimental
work, the reinforced concrete safety bulkhead was left
free-draining to minimize accumulation of gob which may
block off the view ports.

Work remaining to complete normal abatement procedures
at the Salem No. 2 mine, if no further experimental work
is planned, consist of injection of a grout curtain in
the strata adjacent to the mine entries.
                       -  66  -

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                    SECTION VIII

                  ACKNOWLEDGEMENTS

Mr.  Ronald D. Hill, Chief, Mine  Drainage Pollution
Control Activities, National  Environmental Research
Center, Cincinnati, Ohio, who was the EPA Project Officer,
and  Dr. David R. Maneval who  served as Project Director
for  the Department of Environmental Resources, Common-
wealth of Pennsylvania, offered  many helpful suggestions
and  comments during the course of this investigation.
Their valuable assistance is  gratefully acknowledged.

 This  report was prepared by Neville K. Chung, Dravo Corporation,
 Pittsburgh, Pennsylvania 15222.
U. S. GOVERNMENT PRINTING OFFICE : L973 — 514-151/140
                        - 67  -

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    Acc«*ulcn Number
 w
                            Sabjoct Field & Group
                   SELECTED WATER RESOURCES ABSTRACTS
                          INPUT TRANSACTION FORM
    OitfartlzaUon
               Dravo Corporation
    Title
         Investigation of use of gel material for mine  sealing
         Chung, Neville K.
                                        Project D*ml£p*ttoa
                                         EPA, Grant No.  14010  EKW
                                        Woto
               Environmental Protection Agency report
               number, EPA-R2-72-135, December 1972.
 23 I Dt>*cHplon (Starred Pint)

         *Acid mine  water, *Mine drainage, *Mine sealing, Abatement
    \ldentifior* (Starred Flrmt)
         Chemical grout
    Abstract
           Laboratory testing of commercially available chemical grouts was  conducted to
 evaluate their potential use, in conjunction with a cheap  filler,  for remote sealing of
 mine  voids.   By close control of the setting time and proper distribution of the grout
 slurry it was believed that a mine seal could be placed  through a  borehole  from the
 surface without the benefit of retaining bulkheads.
      A slurry mix consisting of an acrylamide grout with flyash or mine  refuse as a
 filler was found to produce a strong controllable gel which resisted chemical attack in
 the laboratory over an eleven week exposure period.

      An attempt to demonstrate a novel technique for application of the  selected grout
 slurry in a  mine entry with high flow was not successful.  The results suggest that
 the technique may be applicable in dry or low flow situations.  However,  the estimated
 cost  of a mine seal using the gel material is presently  not competitive  with existing
 methods.

      Groundwater monitor wells were drilled for the purpose of determining  the effect of
 mine  sealing on groundwater conditions.  Data reflecting pre-seal  conditions was compiled,
 but because  the sealing of the mine was not completed the  monitoring program has been
 postponed.
Abstractor,
       Neville R. Chung
             Dravo Corporation
  WR:I02
  WRSIC
       (REV. JUt-Y IB41I
SEND. WITH COPY OF DOCUMENT. TO: HATER RESOURCE* SCIENTIFIC INFORMATION CENTER
                          U.S. DEPARTMENT OF THE INTERIOR
                          WASHINGTON. D. C. 2O24O
                                                  CPO! 1S70 - 4O7 ->91

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