EPA-R2-73 135 JANUARY 1973 Environmental Protection Technology Series Investigation of Use of Gel Material for Mine Sealing % PROl^ Office of Research and Monitoring U.S. Environmental Protection Agency Washington. DC 20460 ------- RESEARCH REPORTING SERIES Research reports of the Office of Research and Monitoring, Environmental Protection Agency, have been grouped into five series. These five broad categories were established to facilitate further development and application of environmental technology. Elimination of traditional grouping was consciously planned to foster technology transfer and a maximum interface in related fields. The five series are: 1. Environmental Health Effects Research 2. Environmental Protection Technology 3. Ecological Research 4. Environmental Monitoring 5. Socioeconomic Environmental Studies This report has been assigned to the ENVIRONMENTAL PROTECTION TECHNOLOGY series. This series describes research performed to develop and demonstrate instrumentation, equipment and methodology to repair or prevent environmental degradation from point and non-point sources of pollution. This work provides the new or improved technology required for the control and treatment of pollution sources to meet environmental quality standards. ------- EPA-R2-73-135 January 1973 INVESTIGATION OF USE OF GEL MATERIAL FOR MINE SEALING By Neville K. Chung Project 14010 EKW Project Officer Ronald D. Hill Mine Drainage Pollution Control Activities Environmental Protection Agency National Environmental Research Center Cincinnati, Ohio 45268 Prepared for OFFICE OF RESEARCH AND MONITORING U.S. ENVIRONMENTAL PROTECTION AGENCY WASHINGTON, D.C. 20460 For sale by the Superintendent ol Documents, U.S. Government Printing Office, Washington, D.C. 20402 - Price J1.25 ------- EPA Review Notice This report has been reviewed by the Environ- mental Protection Agency and approved for publication. Approval does not signify that the contents necessarily reflect the views and policies of the Environmental Protection Agency, nor does mention of trade names or commercial products constitute endorsement or recommendation for use. 11 ------- ABSTRACT Laboratory testing of commercially available chemical grouts was conducted to evaluate their potential use, in conjunction with a cheap filler, for remote sealing of mine voids. By close control of the setting time and proper distribution of the grout slurry it was believed that a mine seal could be placed through a borehole from the surface without the benefit of retaining bulkheads. A slurry mix consisting of an acrylamide grout with flyash or mine refuse as a filler was found to produce a strong controllable gel which resisted chemical attack in the laboratory over an eleven week exposure period. An attempt to demonstrate a novel technique for applica- tion of the selected grout slurry in a mine entry with high flow was not successful. The results suggest that the technique may be applicable in dry or low flow situations. However, the estimated cost of a mine seal using the gel material is presently not competitive with existing methods. Groundwater monitor wells were drilled for the purpose of determining the effect of mine sealing on groundwater conditions. Data reflecting pre-seal conditions was compiled, but because the sealing of the mine was not completed the monitoring program has been postponed. This report was submitted in fulfillment of Project Number CR-100 Contract 14010 EKW, under the joint sponsorship of the U. S. Environmental Protection Agency and the Commonwealth of Pennsylvania, by Dravo Corporation, Pittsburgh, Pennsylvania 15222. 111 ------- CONTENTS Section Page I CONCLUSIONS 1 II RECOMMENDATIONS 3 III INTRODUCTION 5 Previous Investigations 5 Purpose and Scope of Present Study 6 IV DEVELOPMENT OF SEAL MATERIAL 9 Chemical Grouts Tested 12 Fillers Tested 13 Testing Procedures 13 Evaluation of Grout Slurries 14 Selected Grout Mix 23 V LOCATION AND DESCRIPTION OF TEST SITE 25 Mine Location and Description 25 Acid Drainage Characteristics 28 VI GROUNDWATER MONITORING STATIONS 35 Location and Description of Monitor Wells 35 Sampling Program 38 VII MINE SEALING OPERATIONS 51 Double Bulkhead Seals 51 Sealing of Air Vent 54 Construction of Safety Bulkhead 54 Injection Nozzle Tests 57 ------- CONTENTS (Continued) Section Page VII MINE SEALING OPERATIONS Injection of Gel Material 57 VIII ACKNOWLEDGEMENTS 67 VI ------- FIGURES PAGE 1 Arrangement of Proposed Mine Seal 10 2 Injection Procedure for Grout Seal 11 3 Preparation of Test Cubes 15 4 Unconfined Compressive Strength Test 15 5 Test Cube Storage Controlled Humidity Vault 16 6 Elasticity of Flyash-AM9 Gel 19 7 Deformation and Failure of Test Cylinder 20 8 Compressive Strength and Volume Changes of Flyash-AM9 Gel Immersed in Acid Solution 21 9 Compressive Strength and Volume Changes of Mine Refuse-Flyash-AM9 Gel Immersed in Acid Solution 22 10 General Location Map 26 11 Mine Portal Area 27 12 Acid Drainage Flow Variation 29 13 Statistical Variation of Mine Drainage Flow 30 14 Iron, Acid and Sulfate Concentrations in Mine Acid Flow 31 15 Iron, Acidity and Sulfate Loading to Stream 32 16 Location of Wells and Surface Sampling Stations 36 17 Typical Groundwater Monitor Well 37 18 Double Bulkhead Seals 53 19 Pressure Gauge-Relief Pipe Installed in Place of Old Air Vent 55 Vll ------- FIGURES (continued) PAGE 20 Protection of Excavated Mine Entry 56 21 Concrete Bulkhead Details 58 22 View of Concrete Safety Bulkhead 59 23 Bench-Scale Test of Gel Material 60 24 Angle of Repose Achieved in Lab Test 60 25 Yard Tests of Injection Nozzle 61 26 Slurry Batcher and Weigh Bin 63 27 Slurry Injection Pipe and Pumping Equipment 64 28 View of Mine Entry through Observation Window in Bulkhead 65 Vlll ------- TABLES No. 1 Precipitation in Vicinity of Keystone State Park 33 2 Drilling Logs of Monitor Wells 39 3 Drilling Logs of Existing Park Wells 40 4 Results of Analyses - Sampling Station MD 41 5 Results of Analyses - Sampling Station CR 42 6 Results of Analyses - Sampling Station SP 43 7 Results of Analyses - Sampling Station C-l 44 8 Results of Analyses - Sampling Station C-2 45 9 Results of Analyses - Sampling Station B-l 46 10 Results of Analyses - Sampling Station B-2 47 11 Results of Analyses - Sampling Station B-3 48 IX ------- SECTION I CONCLUSIONS 1. A slurry consisting of an acrylamide grout with flyash or neutralized mine refuse as a filler can produce a stiff gel which may be useful in remote sealing of mine voids. The setting time is controllable, and the gel material is strong, resilient and resistant to attack by mine acid. 2. The cost of the materials and placement are at present higher than that for a concrete seal. Reductions are possible through use of a modified mix, possibly with cement as an admixture, and refinement of injection procedures. 3. Dilution and erosion of the gel material prevents successful formation of a gel seal in high flow mines. Application of the material and technique to dry or low flow situations has not been tested. 4. A concrete seal can be placed between ungrouted stone bulkheads but settling of the concrete may occur due to movement of the unconsolidated aggregate, resulting in increased grout requirement in the subse- quent pressure grouting operation. - 1 - ------- SECTION II RECOMMENDATIONS 1. It is recommended that a groundwater monitoring program be included in plans for completion of mine drainage abatement work at the Salem No. 2 Mine at Keystone State Park, since information is lacking at the present time regarding the effect of mine sealing on groundwater conditions, and monitor wells have already been drilled at the Keystone site. 2. The location of the mine portal area on State property which is not developed presently for recreational use, and the existence of a reinforced concrete safety bulkhead with view ports and sample valve, make the site ideal for further test work. It is recommended that this asset be explored prior to making a final decision on sealing. If no testing is foreseen, closing of the drain valve and sample valve in the bulkhead will make it a concrete seal. 3. It is recommended that grout stabilization of the stone bulkheads be retained as normal procedure in construction of double bulkhead seals. - 3 - ------- SECTION III INTRODUCTION Acid mine drainage is formed by the oxidation of iron disulfides, usually pyrites, found in association with coal, when the pyrites are exposed to air and water. The result is a dilute solution of sulfuric acid and iron sulfate. Though there are available treatment techniques, such as neutralization with lime to adjust pH and precip- itate iron, it is generally agreed that measures aimed at preventing the formation of acid drainage hold the most promise for curbing this source of pollution, par- ticularly from inactive mines. There are presently over 3000 miles of streams in Pennsylvania affected by mine drainage, most of it originating from abandoned deep mines. Estimates for abatement have been set at two billion dollars, and the major portion of this cost is for source control. New techniques are constantly being sought, largely through research'and development programs sponsored by the U. S. Environmental Protection Agency and various State agencies. Previous Investigations Techniques which have been investigated for the prevention of mine acid formation are based on excluding oxygen from the pyritic surfaces. This is usually accomplished by sealing the mine openings to prevent entry of air and to cause the mine cavity to fill with water. Seal construction methods tested have included: a) placement of an aggregate mass followed by injection of grout into the aggregate. b) placement of a permeable limestone plug for in situ neutralization and sealing by precipitates. c) injection of quicksetting cement grout into expendable cloth retainers. d) formation of forward and rear retaining bulkheads with a quick-setting slurry followed by injection of a cement intermediate plug. e) placement of forward and rear retaining bulkheads of aggregate through vertical boreholes, followed by ------- stabilization of the bulkheads by injection of grout and injection of a concrete plug between the bulkheads. The last method, using two bulkheads of stone with a concrete plug between them, was recently employed in sealing over 100 mine openings in Butler County, Pennsylvania. Purpose and Scope of Present Study The work reported herein was undertaken to develop a new mine sealing technique using a chemical grout with a filler material as the sealant. A chemical grout is a mixture of chemicals which will produce a stiff gel from a dilute aqueous solution when properly catalyzed. The setting time is predictable and controllable, and the gel material is essentially impermeable. It was theorized that a chemical grout with a cheap filler such as flyash could produce a strong, chemically resistant, impermeable material suitable for a mine seal, and that by proper distribution of the grout slurry and control of the gel time the seal could be built up without the benefit of retaining bulkheads. Three major phases of activity were proposed: 1) Laboratory testing of commercially available grouts and filler materials to evaluate and select one or more formulations suitable for the proposed remote mine seal construction. 2) Demonstration of a technique for application of the gel material by sealing three entries of an abandoned deep mine located in Derry Township, Westmoreland County, Pennsylvania. 3) Post-construction surveillance to study the effective- ness of the seals, and to determine changes in ground- water quantity or quality resulting from placement of the seals. As the work progressed, information developed in each phase suggested or dictated changes to the original scope of work in succeeding phases. Two major changes were made: 1) Double bulkhead type concrete seals, with ungrouted stone bulkheads, were placed in two of the three mine entries, and only one chemical grout seal attempted. - 6 - ------- 2) The post-construction groundwater monitoring program was postponed. Although the surveillance program was not performed, a set of groundwater monitor wells were completed in order that background information regarding groundwater level and quality could be developed prior to placement of any mine seal. . This information, plus data on the flow and quality of acid drainage from the mine, and stratigraphic information developed from drilling of the monitor wells, are included in this report to provide a reference point for future work if performed at this site. The need for information regarding the effect of mine sealing on groundwater still exists, and it is assumed that this aspect will be investigated when the sealing of the mine is completed by injection of grout curtains. - 7 - ------- SECTION IV DEVELOPMENT OF SEAL MATERIAL Test Objectives As proposed, the experimental mine seal was to be built by injection of a gel material with controllable setting time into the mine cavity through a vertical borehole from the surface. The material would be self-supporting, eliminating the need for retaining bulkheads. Following placement of the seal, flyash would be pumped into the mine side of the seal. The purpose of this backstop was twofold. It was felt that if any leakage occurred flyash would be carried in suspension into the seal and plug the leak. Secondly any leakage that escaped the seal would be neutralized by the flyash. A sketch of the proposed seal is shown on Figure 1. The safety bulkhead shown is for protection during development and testing of the seal. Test work to develop a material suitable for the proposed mine seal included evaluation of five different chemical grouts with various combinations of flyash, mine refuse, sand and gravel as fillers. Characteristics of prime importance were a short, controllable setting time, resistance to chemical attack by mine acid, and sufficient strength to withstand expected forces. To avoid formation of a point seal at the injection hole which would prevent completion of the seal across the entire width of the mine roof, it was felt that it would be necessary to direct the grout slurry stream outward away from the injection hole, and slightly upwards, in order to build the seal up from the outer extremities in a concave shape, as shown on Figure 2. A short gel time of less than one minute would be required while building up the seal in order to give an economical angle of repose and prevent excessive running of the material along the mine floor. On the other hand during the final stages a longer gel time would be required to ensure dispersion and penetration of the grout into the remaining crevices. For maximum flexibility it was decided that the material should have a highly controllable gel time from greater than five minutes to a few seconds. The mine floor at the test site slopes upward from an elevation of 1016 feet at the entry to a maximum elevation of approximately 1100 feet. The maximum hydraulic head that could develop on a seal therefore is approximately 84 feet, equivalent to 36 psi. The maximum pressure which - 9 - ------- PLAN FLYASH INJECTION HOLE o I SEAL INJECTION HOLE ELEVATION FIGURE 1, ARRANGEMENT OF PROPOSED MINE SEAL ------- INJECTION NOZZLE y/^f\ ELEVATION 'A1 SECTION FIGURE 2, INJECTION PROCEDURE FOR GROUT SEAL ------- could be exerted by the overburden of about 30 feet was estimated at 35 psi, essentially equivalent to the maximum hydraulic head. Using a design safety factor of 3, which includes allowances for differences in filler materials and between laboratory techniques and field procedures, a compressive strength of 110 psi was selected as the desired strength of a seal material. Chemical Grouts Tested Five commercially available chemical grouts were tested: Trade Name Type Terranier-C Phenolic polymer AM-9 Vinyl polymer Cyanaloc-62 Methylol bridge polymer Terra Firma Chrome lignin Geoseal Phenolic polymer Terranier-C is a three-component system consisting of a principal reactant, a catalyst and a secondary reactant or crosslinking agent. The principal reactant is a phenolic powder which is dissolved in water to make one solution. A second solution is prepared containing the catalyst, sodium dichromate, and a formaldehyde cross- linking agent. A polymerization-crosslinking reaction occurs when the two solutions are mixed. AM-9 Chemical Grout is a four-component system consisting of a reactant, catalyst, inhibitor and initiator. The reactant is a mixture of two organic monomers, acrylamide and N,N*-methylenebisacrylamide. It is a granular material which is mixed with water to make a solution of desired strength. The catalyst is B-dimethylaminopropionitrile (DMAPN) an alkaline liquid. The inhibitor potassium ferricyanide, is added in very small quantities to control the reaction. The reaction is triggered by the initiator, ammonium persulfate, which is a very strong oxidizing agent. Two solutions are prepared, one containing AM-9, DMAPN and potassium ferricyanide, and the other ammonium persulfate. Gelation occurs by a polymerization-crosslinking reaction when the two solutions are mixed. - 12 - ------- Cyanaloc-62 consists of two components, a reactant and a catalyst. The reactant is a viscous liquid monomer which is diluted to desired strength with water. Polymerization occurs when a solution of sodium bisulfate, the catalyst is mixed with the reactant. Terra Firma consists of a lignosulfonate reactant which is catalyzed by sodium dichromate to form a chrome lignin gel. Both materials dissolve readily in water to make solutions of desired consistency for application. Geoseal is a two-component system consisting of a phenolic reactant and sodium hydroxide catalyst. The reactant is a powder which is not dissolved in water, but added directly to a solution of the catalyst. Polymerization occurs when the two are mixed in certain proportions which give a pH of between 9.5 and 10.2. Fillers Tested Flyash was the first material considered for testing as a filler. It is cheap and readily available, and was also proposed as a backstop behind the seal because of its particle size and alkalinity. For the laboratory testing 800 Ib of flyash was obtained from Duquesne Light Company's Elrama, Pa. station. This sample of ash had a particle density of 2.11 gm/cc and a bulk density of 1.05 gm/cc, indicating approximately 50% voids. Mine refuse from the mine site was investigated as a possible filler material since if successful this would also solve, at least partially, the problem of disposal of this unsightly acid producing waste material. The loosely compacted, claylike material was found to have a particle density of 2.35 gm/cc and a bulk density of 1.53 gm/cc, indicating 34% voids. The material is acidic with a pH of approximately 3.0. Shot gravel and Ohio River highway grade sand were tested briefly and found to offer no advantages over flyash or mine refuse as fillers for the proposed seal material. Testing Procedures Preliminary tests were run with each material to determine its particular characteristics and suitability as a potential mine sealant. Mix proportions, strength, gel time control, and compatibility with the fillers were evaluated. Once these tests were completed, practicable grout formulations were selected for further testing of physical properties and stability. - 13 - ------- Test cubes were prepared by mixing selected proportions of grout, water, filler and whenever necessary inhibitor or crosslinking agent, for thirty minutes to insure homogeneity, adding the catalyst or activator, and pouring the slurry into ASTM standard 2-inch cube molds shown on Figure 3. After solidification the cubes were placed in a storage vault with humidity, controlled at 100% to prevent dehydration. Two or three cubes were tested for compressive strength daily for one week. (Figure 4.) After the first week cubes were tested once per week for ten weeks. Figure 5 shows the controlled- humidity storage vault. Resistance to chemical attack from acid mine drainage was tested by submerging cubes in an acid solution prepared in the laboratory to simulate the most severe condition anticipated. This solution contained 200 ppm iron, 400 ppm sulfate, and had a pH of 2.0. Size, compressive strength, and weight of test cubes were checked weekly for ten weeks. The test solution was examined for discoloration and sediment, and changed weekly or whenever the pH value reached 3.5. Evaluation of Grout Slurries The preliminary tests which were conducted with each material eliminated some of the materials and certain combinations of materials from further, long-term testing. Shot gravel and highway grade sand were tested as fillers for added mass in combination with flyash and mine refuse. They were found to yield lower compressive strength than either flyash or mine refuse alone, and were therefore eliminated from further consideration as fillers. Tests with Terra Firma indicated that the gel time could be effectively controlled only by varying the water content, which affected the strength of the resultant gel. Catalyst concentration was dependent on monomer concentra- tion, which resulted in shorter gel times with increasing concentrations of the chemical grout. This system was also found to be incompatible with flyash due to the alkalinity which results in precipitation of trivalent chromium from the dichromate catalyst. Geoseal is catalyzed by sodium hydroxide at a pH between 9.5 and 10.2. The caustic not only initiates the reaction but is also necessary to dissolve the reactant to a true solution. Polymerization therefore begins as soon as the reactant is dissolved in the catalyst solution. This necessitates a batch, or one-shot, system of application - 14 - ------- FIGURE 3, PREPARATION OF TEST CUBES FIGURE M & IL UNCONFINED COMPRESSIVE STRENGTH TEST - 15 ------- FIGURE 5, TEST CUBE STORAGE IN CONTROLLED- HUMIDITY VAUL1 - 16 - ------- which severely limits control of gel time and precludes use of a very short gel time. A two-shot system was devised by preparing the grout solution with less sodium hydroxide than is necessary for gelation, and feeding the remainder of the required caustic in a separate stream. In theory this seemed feasible, but it could not be made to work. The material increased in viscosity but would not gel. An increased amount of caustic caused a gel which was attacked by moisture indicating only a partial reaction. The addition of either flyash or mine refuse to a solution of Terranier-C was found to start gelation immediately, apparently due to a catalytic effect of polyvalent cations in the fillers. It was discovered that a more stable mixture, usable for 30 to 40 minutes, could be prepared by adding dry Terranier-C to a flyash slurry or neutral- ized mine refuse slurry. Test cubes made in this manner were found to be hard and brittle with compressive strength of 70 to 115 psi. When the cubes were immersed in a synthetic mine acid solution, the solution turned a dark reddish-brown color characteristic of the polymer within one day. Leaching of color continued for about seven weeks, during which time the cubes shrank approximately 51 in volume, but no corresponding loss of strength was detected. This loss of color and shrinkage may indicate a condition which could eventually lead to failure; however the immediate problem with use of Terranier-C slurry as a mine sealant was the initiation of setting by the fillers. Cyanaloc-62 is acid catalyzed and therefore will not form a gel with alkaline flyash. With mine refuse as a filler gelling is initiated but proceeds very slowly, over a period of hours. Test cubes made with a grout mix consisting of 25 pounds mine refuse to 1 gallon of one-to- one by volume Cyanaloc-62 solution had compressive strength of 560 psi. However, after five weeks immersion in an acid solution the cubes began to show signs of deterioration. The surface developed a slimy appearance, and an 8% weight loss was measured. A sudden, severe loss of strength occurred during the eighth week. At the end of the ten week test period the strength loss was 421 due to attack by the acid. Test cubes stored at 1001 humidity showed no similar loss of strength. Testing of AM-9 chemical grout was narrowed down to and 15% solutions after preliminary tests. The exothermic - 17 - ------- polymerization reaction released enough heat to cause cracking of cubes made with a 30% solution, and a 5% solution produced a very weak gel. The 20% solution was eliminated from further testing after three weeks because indications were that satisfactory strength would be obtained with a 15% solution. Both flyash, and mine refuse neutralized with lime or flyash, were found to be compatible with AM-9. Test cubes were made using 10% and 15% AM-9 solutions with the follow- ing amounts of filler per gallon: a) 15 Ib flyash b) 20 Ib mine refuse, 22 gm CaO c) 7 Ib flyash, 14 Ib mine refuse All the components of the AM-9 system were easily handled and readily dissolved to true solutions with viscosities similar to water. Mine refuse alone was found to be unsuitable as a filler because of its acidity, but neutral- ization to a pH greater than 7 with either lime or flyash made it an acceptable filler. Gel time of AM-9 grout mixes was found to be highly controllable by varying the amounts of catalyst DMAPN, ammonium persulfate and potassium ferricyanide which together comprise the catalyst system. Grout mixes made with AM-9 were found to produce a material which had a certain degree of elasticity. Figure 6 is a plot of observed deformations of cubes made with 10%, 15% and 20% AM-9 solutions and flyash versus applied compres- sive stress. Elasticity of a test cylinder is illustrated on Figure 7 which shows extreme deformation at failure. It is believed that this property would be advantageous in formation of a tight seal, after leakage is stopped by pressure grouting or by flyash carried in suspension from the backstop. Compressive strength and size of test cubes immersed in an acid solution simulating mine drainage were measured weekly over an eleven week period. Figures 8 and 9 show the compressive strengths and volume changes observed for test cubes made using AM-9 with flyash alone and a combina- tion of mine refuse and flyash as fillers. From the graphs it would appear that the chemical stability of the cubes made with a combination of flyash and mine refuse as filler - 18 - ------- 160 FAILURE 140 120 IOO W 0. V) «> 80 UJ IX ui > 35 CO £ cc a. 2 O o 40 FAILURE -t- 1.7 1.6 1.5 1.4 1.3 CUBE HEIGHT (INCHES) 2.O 1.9 1.2 FIGURE 6, ELASTICITY OF FLYASH-AM9 GEL - 19 - ------- FIGURE 7. DEFORMATION AND FAILURE OF TEST CYLINDER - 20 - ------- 25O CO 0. ZOO ISO o z a t- co UJ > IOO (T a. 2 O u 4567 TIME (WEEKS) 8 IO II I 12 + 8 i o +2 -2 FIGURE 8, 4567 TIME (WEEKS) 8 IO II COMPRESS IVE STRENGTH & VOLUME CHANGES OF FLYASH-AM9 GEL IMMERSED IN ACID SOLUTION 12 - 21 - ------- 250 2 IU o: 190 (0 £.00 t U) IT 50 o o AM9 » 7 i 9 456 TIME (WEEKS) 8 IO i II 12 + 6 -4 TIME (WEEKS) FIGURE 9, OPPRESSIVE STRENGTH & VOLUME CHANGES FOR MINE REFUSE-FLYASH-AM9 GEL IMMERSED IN ACID SOLUTION - 22 - ------- is better than that of the cubes made with flyash alone as the filler. However it is believed that the observed variations in the strength and size of the cubes made with flyash alone were due to neutralization of flyash particles by acid at the surface of the cubes rather than to reaction with the chemical grout material itself, and a stable condition would be reached. When gels were formed at a lower pH by neutralizing the flyash with mine refuse (or vice versa) the observed strength and size were uniform. It should be noted that strength determinations are made by destructive testing and that therefore each determina- tion is_made on a different cube prepared from the same grout mix. As a result some variation of observed strength can be expected from cube to cube, regardless of the curing time or exposure conditions. Selected Grout Mix Of the five chemical grouts tested only AM-9 was found to meet all the essential requirements of adequate strength, good gel time control and resistance to mine acid. The compressive strength tests indicated that a 15% AM-9 solution would be required, whether flyash or mine refuse was used as the filler. On the basis of a seal 12 feet wide by 28 feet long, the cost of grouting chemicals alone was estimated at $9,000 per seal. This was considerably higher than original estimates, which had been based on use of a cheaper grout material, and it appeared that even if the material could be cheaply applied the overall cost would exceed that of alternate sealing techniques. It was agreed in a joint meeting with the project sponsors to proceed with only one experimental grout seal, and seal the other two mine entries with double bulkhead type concrete seals. Though the cost of the gel seal was expected to be uneconomical, it was felt that testing of the injection technique was still desirable since if successful, further research could be directed to reducing the cost of both the materials and the procedure. A grout slurry of 15 Ib flyash to one gallon of 15% AM-9 solution was selected for the test. Flyash offered certain inherent advantages over mine refuse as a filler for the proposed seal. Screening and neutralization were not required, as with mine refuse. Also, since one aspect of the proposed sealing operation consisted of pumping flyash into the mine side of the grout seal, the use of flyash as the filler would further simplify materials - 23 - ------- handling. The main reason for considering mine refuse lay in the disposal aspect. However, in view of the variable nature and quantity of this material from mine to mine, any success with use of the material at this mine would not necessarily be repeatable at another site - 24 - ------- SECTION V LOCATION AND DESCRIPTION OF TEST SITE Mine Location and Description The site selected for demonstration of the experimental sealing material and technique is an abandoned deep mine located in Derry Township, Westmoreland County, Pennsyl- vania. Most of the mine, including the portal area, is located within the Commonwealth of Pennsylvania's Keystone State Park, approximately 35 miles east of Pittsburgh. The location is shown on Figure 10. The mine, which was known as the Salem No. 2 Mine, covers approximately 300 acres, sloping upward at an approximate grade of 31 from an elevation of 1016 feet at the entrance to approximately 1100 feet at the highest point. There were three openings located a short distance below the spillway of Keystone Lake. The west opening was the main portal, while the middle opening served as a fanway. The third opening to the east was made by blowing a hole through the mine roof by an explosive charge set within the mine. The mine portal area is shown on Figure 11. The main entry extends approximately half a mile in a southerly direction beneath a wooded hill. Side entries run east and southwest from the main entry. Beneath the crest of the hill the mine lies some 200 feet below the ground surface. Other than the portal area the thinnest cover occurs in the southernmost extremities where the mine is 40 to 60 feet below the ground surface. A 12" air vent, located approximately 200 feet up from the main entrance as shown on Figure 11 was the only other opening found into the mine. No instance of subsidence was known to a former miner who worked in the mine for 20 years, and no evidence of holes or slumps were found during field inspections of the mined area. All three entries were blocked with rubble, and acid drainage appeared to be coming only from the middle entry in front of which the water was pooled. The overflow drained into the small creek below the Lake. This creek enters the Loyalhanna Creek, a tributary of the Allegheny River, approximately 1-1/2 miles downstream. - 25 - ------- NEW YORK PENNSYLVANIA KEYSTONE STATE PARK GREENSBURG -^MARYLAND > N VIRGINIA 25 5O FIGURE 10, GENERAL LOCATION MAP - 26 - ------- o FAN WAY OUTCROP SECONDARY PORTAL EXISTING FOUNDATIONS 200 SCALE FEET FIGURE 11, MINE PORTAL AREA - 27 - ------- Acid Drainage Characteristics^ The acid drainage from the mine was measured and sampled over a two-year period prior to the start of remedial activity, from October 1967 to August 1969. The flow generally ranged from 20,000 gallons per day (13.9 gpm) to 160,000 gallons per day (111 gpm), with the lowest flows occurring in late summer and fall, and the highest flows occurring usually during the first three months of the year. Figure 12 shows the flow variation over the two-year sampling period. Flow rates plotted are single measurements or averages of two to four measure- ments taken during a given month. Occasional peak flows up to 850,000 gallons per day (590 gpm) were reported; however ninety percent of the time the flow was less than 160,000 gallons per day, and half the time less than 60,000 gallons per day, as shown by the statistical analysis of all recorded flow measurements, Figure 13. Concentrations of iron, acidity and sulfate in the mine drainage over the sampling period are shown on Figure 14, and the corresponding loadings in pounds per day are shown on Figure 15. Again the values plotted are either single determinations or averages of two to four samples taken during a given month. The total pollution load due to the mine drainage is related primarily to the flow quantity and only secondarily to contaminant concentra- tions. Peak loads generally coincided with high flow periods. Inasmuch as the mine drainage flow, and consequently the pollution load, may be a function of the wetness or dry- ness of any given period, an evaluation of abatement measures should take into consideration the amount of precipitation in the area over the study period. The terrain above the mine is conducive to fairly rapid surface runoff on all sides of the rounded hilltop. However infiltration that does occur will find its way into the mine cavity which, by virtue of its areal extent and the relatively unimpeded routes it provides, should be the principal flow control for subsurface water. Precipitation data for the Keystone State Park area for the years 1967, 1968 and 1969 is given on Table 1. - 28 - ------- t-o VQ 600,000 500,000 IOO.OOO 0 NDJFMAMJJASONDJFMAMJJA 1967 1968 1969 FIGURE 12, ACID DRAINAGE FLOW VARIATION ------- w o 500,000 400,000 300.00O 200,000 100,000 90,000 80,000 ^ 70,000 & 60.0OO * 50,000 " 40,000 30,000 20,000 10,000 1 I » 1I 1 1 * 10 2O 30 40 50 60 70 80 PERCENTAGF OF TIME EQUAL TO OR LESS THAN 90 95 98 99 FIGURE 13, STATISTICAL VARIATION OF MINE DRAINAGE FLOW ------- 3000 -2000 j IOOO 0 N 1967 D J FMAMJJASONDlJFMAMJJA 1968 ^ "969 1000 Q_ CL 800- 600- g o 400 i 200 ONDIJFMAMJJASOND 1967 4 1968 JFMAMJJA 1969 4OO Z a 300 200 IOO ONDIJ FMAMJ JASONO 1967 4. 1968 J FMAMJJA 1969 FIGURE W, IRON, ACID & SULFATE CONCENTRATIONS IN MINE ACID FLOW ------- TO 3347 ts> I 1600 1400 o x. c/> CD s £ 800 fi _/ ) « > 600 H Q IAOO 200 \ \ ON D ' J F MA M J A S 0 N D (967 «L- 1968 F M A M J 0 A 1969 FIGURE 15, IRON, ACIDITY & SULFATE IN MINE ACID FLOW ------- TABLE I PRECIPITATION IN VICINITY OF KEYSTONE STATE PARK (Average of Measurements at Blairsville, Vandergrift & Derry) Inches of Precipitation 1967 Jan. Feb. March April May June July Aug. Sept. Oct. Nov. Dec. ANNUAL 1.28 2.82 6.59 4.55 4.21 1.69 5.02 3.88 3.50 3.02 2.82 2.46 41.84 1968 Jan. Feb. March April May June July Aug. Sept. Oct. Nov. Dec. 2.47 1.25 3.39 2.05 6.88 1.61 4.15 4.69 2.80 1.93 3.85 3.80 38.87 1969 Jan. Feb. March April May June July Aug. Sept. Oct. Nov. Dec. 2.70* 1.03* 1.45* 4.54* 2.57* 3.64* 6.01 2.16 2.15 2.81 3.12 4.93 37.11 * No data from Derry. Donegal data used. - 33 - ------- SECTION VI GROUNDWATER MONITORING STATIONS Location and Description of Monitor Wells In order to provide the means of evaluating the impact of the sealing of the mine on groundwater in the area, a set of groundwater monitor wells were drilled in the locations shown on Figure 16. Well A-2, located on top of the hill above the mine, was drilled to a depth of 200 feet, or to approximately 15 feet of the top of the mine, in order to evaluate the dewatering effects on the strata comprising the hill above the mine by the mined area. Two wells were origi- nally proposed, one on each of the two rounded hilltops; however Well A-l was later eliminated. Wells B-l, B-2 and B-3 were drilled for the purpose of monitoring the groundwater in the immediate surrounding area in order to determine its response to the inundation of the mined area. Drilling depths were 230 feet, 225 feet and 200 feet respectively. Wells C-l and C-2 near to Keystone Lake and Creek, were drilled to 100 feet below their bottom elevations in order to give warning of possible deep flow lines and inputs of mine drainage polluted groundwater through the bottom of the lake or stream as a response to vertical pressure buildup as the mine fills. Depth of C-l is 156 feet, and the depth of C-2, 110 feet. All of the monitor wells are 6 inches diameter with 6-1/4" I.D. casing extending from 1 foot above grade to below bedrock. A screwed cap is provided on each well to prevent entry of foreign matter. Ten feet high markers, consisting of 6 inch diameter plates mounted on 1-1/2" diameter pipe, were erected at each monitor well to facilitate location and identification. A typical monitor well is shown on Figure 17. Water was encountered during drilling of all the wells except well A-2 located on the crest of the hill. In general the wells at higher elevations such as B-l and B-2 yielded small quantities of water. At wells C-l and C-2 which are at a low elevation and lie close to the lake and stream, water was encountered at two separate elevations. - 35 - ------- < ' EXISTING WATER WELLS // ' '/ ' ' x V A ! M x ^f / o / ;-' NEW MONITOR WELLS AND SAMPLING STATIONS / FIGURE 16, LOCATION OF WELLS AND SURFACE SAMPLING STATIONS ------- MARKER c +1 o 1 \ \ ^ <-\ V > -<: y I^^-G-DIA. j ROUND ROD WELDED TO CAP /-I>2"DIA. ^ J i 1_, ^_ or.DPurpn PAD - < * < ; ^c tc u c r^" U-^H --O 1 § 1 ! _^J « (5 ^ ^ S r S ^ ; 'o 1 , ., 1 ' ^^ &/4 I.D. CASING /^ ROCK 6_^- 6"DIA.HOLE FIGURE 17, TYPICAL GROUNDWATER MONITOR WELL 37 ------- The drilling logs of the monitor wells are tabulated on Table 2, and logs of water wells previously drilled in the park on Table 3, as an aid to defining the stratigraphy of the area for future interpretation of groundwater changes resulting from water buildup in the mine. The locations of the existing water wells are shown on Figure 16. Well No. 4 was not completed. Sampling Program In addition to the groundwater monitoring wells, surface sampling stations SP and CR were established upstream and downstream of the point where the mine drainage entered the creek and at the mine opening itself, designated station MD. Location of these sampling points are shown on Figure 16. Since the surveillance program has been postponed, there is of course no data reflecting a change in the hydro- geological environment due to mine water impoundment. However, samples were taken from the monitor wells and surface sampling stations on a more-or-less weekly schedule over a two-month period prior to the scheduled sealing, in order to establish background data on water quality and level. These samples were analyzed for pH, total iron, sulfate, acidity and total solids. On each sampling tour the water level in the monitor well was measured. The data from the "pre-sealing" sampling program is presented on Tables 4 through 11. At stations C-l and C-2 samples were taken from two depths approximately coincident with the levels at which water was encountered during drilling. Monitor well A-2 was dry throughout the sampling period. Some observations concerning the analytical data can be made. Iron concentrations were generally higher in the samples taken at the higher level in wells C-l and C-2 indicating possible influence of mine drainage. Total solids concentrations in the samples taken January 20 at Sta. C-2 showed a sudden three-fold increase, but there was no corresponding increase in acidity, iron or sulfate concentration. On the contrary there was a reduction in acidity. It is believed that this sudden change in groundwater quality was due to contamination by a cement-flyash grout mixture that was pumped into the west entry the preceding week. This reinforces the evidence of contamination of well C-l by water from the mined area. - 38 - ------- TABLE 2 DRILLING LOGS OF MONITOR WELLS Well A- 2 Strata D«pth 0-4 4-21 21-33 33-49 49-56 56-67 67-83 83-92 92-94 94-94)4 94K>107 107-123 123-145 145-146 146-148 148-151 151-200 Descrip- tion Clay Sand Rock Shale Sand Rock Shale Sand Rock Shale Sand Rock Shale Coal Fire Clay Sandy Shale Sand Rock Shale Coal Sandy Shale Solid Rock Well B-l Strata Depth 0-10 10-14 14-35 35-37 37-55 55-81 81-124K2 124)4-125 125-127 127-134 134-141 141-156 156-168 168-169'/2 169H-206 206-215 215-217 217-222 222-230 Descrip- tion Sand Clay Shale Sand Rock Shale Sand Rock Shale Coal Fire Cloy Shale Sand Rock Sandy Shole Sand Rock Coal Sand Rock Sandy Shale Sand Rock Sandy Shale Sand Rock Water at 125' Well B-2 Strata Depth 0-18 18-61 61-63 63-66 66-77 77-120 120-123 123-126 126-146 146-159 159-183 183-186 186-190 190-192 192-213 213-218 218-224 224-225 Descrip- tion Clay Shale Coal Fire Clay Sandy Shale Sand Rock Coal Fire Clay Sand Rock Shale Sand Rock Shale Coal Fire Clay Sand Rock Shale Coal Fire Clay Water at 176' Well B-3 Strata Depth 0-1 1-16 16-21 21-26 26-28 28-39 39-43 43-46 46-52 52-79 79-98 98-102 102-104 104-106 106-110 110-111 111-126 126-135 135-140 140-200 Descrip- tion Topsoil Clay Shale Solid Rock Shale Solid Rock Coal Fire Clay Solid Rock Shale Solid Rock Shale Coal Clay Solid Rock Coal Solid Rock Shale Coal Shale Water at 49 ' Well C-l Strata Depth 0-9 9-45 45-49 49-55 55-62 62-72 72-85 85-90 90-91 91-100 100-123 123-134 134-137 137-151 151-155 155-156 Descrip- tion Topsoil &Clay Sand Rock Coal Shale Sand Rock Shale Sand Rock Sandy Shale Coal Shale Sand Rock Shale Sandy Shale Shale Coal Shale Water at 49', 140' Well C-2 Strata Depth 0-8 8-10 10-28 28-30)4 30)6-34 34-38 38-40 40-45 45-70 70-75 75-84 84-93 93-95 95-104 104-108 108-110 Descrip- tion Topsoil &Clay Shale Solid Rock Coal Shale Sand Rock Shale Limestone Shale Sand Rock Shale Sand Rock Shale Sandy Shale Sand Rock Shale Water at 28 ', 65 ' ------- TABLE 3 DRILLING LOGS OF EXISTING PARK WELLS Well No. 1 Strata Dt pth 0-18 18-30 30-32 32-70 70-75 75-80 80-85 85-110 110-165 165-170 170-210 210-245 245-270 270-300 Description Clay Gray Shale Coal Gray Shale Gray Sand Coal Gray Shale Gray Sand Gray Shale Coal Gray Sand Gray Shole Gray Sand Gray Shale and Sand Wafer at 50', 110', 245' Well No. 2 Strata Depth 0-9 9-11 11-25 25-37 37-50 50-52 52-55 55-60 60-70 70-75 75-80 80-82 82-130 130-135 135-145 145-170 Description Clay Dark Shale Gray Shale Dark Shale Gr. Sand Rock Coal Gray Shale Sand Rock Gray Shale Sand Rock Gray Shale Black Shale Gray Shale Sand Rock Sandstone Gray Shale Water at 37', 40', 55', 105', 135', 160' Well No. 3 Strata Depth 0-10 10-50 50-60 60-65 65-115 115-120 120-125 125-130 130-150 150-155 155-175 175-205 205-210 Description Cfay Gray Shale Gray Sand Coal Gray Send Gray Shale Gray Sand Coal Gray Shale Coal Gray Shale Gray Sand Gray Shale Water ol 25', 150', 175' Well No. 5 Strata Depth 0-20 20-65 65-80 80-85 85-87 87-90 90-100 100-110 110-140 140-150 150-160 160-185 185-190 190-200 200-220 220-295 295-300 Description Clay Gray Shale Gray Sand Gray Shale Gray Sand Coal Gray Shale Gray Sand Gray Shale Gray Sand Coal Gray Shale Coal Gray Shale Gray Sand Gray Shale Gray Sand Wafer af 35', 80', 200' Well No. 6 Strata Depth 0-15 15-40 40-47 47-48 48-50 50-70 70-90 90-100 100-105 105-110 110-135 135-140 140-150 150-175 175-190 Description Cloy Gray Shale Gray Sand Coal Gray Shale Gray Sand Gray Shale Gray Sand Brown Shale Coal Gray Shale Coal Gray Shale Gray Sand Gray Shale Water at 30', 45', 65', 100', 115' o I ------- PH Iron Sulfate Acidity ("hot") T. Solids TABLE 4 RESULTS OF ANALYSES 11-19-71 2.81+ 105 1930 535 8l?2 11-30-71 2.62 3^8 1000 603 2811 SAMPLING 12-8-71 2.73 67.0 650 Uo? 1281 STATION MD 12-13-71 2.72 75 650 U25 1561 12-21-71 2.71 57.2 666 teu 1371 1-6-72 2.82 62. U 5M* 369 2025 1-13-72 2.86 56 532 1*60 1179 1-20-72 2.88 56.5 600 U58 1360 1-28-72 2.91 146.2 620 1*85 8691* All concentrations in parts per million ------- TABLE 5 RESULTS OF ANALYSES 1 to 1 PH Iron Sulfate Acidity T. Solids 11-19-71 6,27 5.29 23.5 7.38 239 11 -30 -71 7.62 8.3 16 1.6 279 SAMPLING 12-3-71 7.20 5.08 3U.O 3.1 116 STATION CR 12-13-71 7.^7 6.6 51 1.6 189 12-21-71 7.56 3.8 U5 l.U 10U 1-6-72 5-85 2.2 26 11.7 156 1-13-72 6.73 2 3^ 6.1 158 1-20-72 7.26 3.5 te 3.6 206 1-28-72 6.83 2.6 33 6.3 141 All concentrations in parts per million ------- TABLE 6 RESULTS OF ANALYSES pH Iron Sulfate Acidity T. Solids 11 19-71 7.50 O.Ul 26.5 2.0 98 11-30-71 7.2U 0.8 26 3.3 109 SAMPLING 12-8-71 7-29 2.U6 26.5 3-1 101 STATION SP 32-13-71 7.96 U.3 16 l.l 86 32-21-71 7-93 1.1* 15 1.2 78 1-6-72 7.85 ND 16 1.3 96 1-13-72 7.26 1 17 3.2 lUi 1.20-72 7.9^ ND 16 1.3 99 1.28.72 6.80 1.0 15 10.9 179 All concentrations in parts per million ------- TABLE 7 RESULTS OF ANALYSES SAMPLING STATION C-l 11-19-71 11-30-71 12-8-71 12-13-71 12-^1-7: Water Level (ft) PH Iron Sulfate Acidity T. Solias (u) (L) (u) (L) (u) (L) (u) (L) (u) (L) 101* 7.68 7.63 0.93 1.58 12.0 10.5 7.0 5.75 29U 387 10U3 10146 8.11 8.01 7.87 1.8 12. U 12.1* 15 15.7 12.8 0.6 1.2 U.2 283 385 U07 10U7 8.51 8,53 10.7 8.6 ND 5 U.2 3.8 556 358 10UU 8.U9 8,U2 12.5 8.1 2 U 2.6 2.U 525 373 I 1-6-72 10U3 7.67 7.95 9.0 5^ 2 2 7.9 3.8 357 3^6 1-13-72 10U3 7.76 7.57 12 8 5 u 7.U n.5 381 U35 1-20-72 10UU 8.5U 8.35 9-1 6.9 2 2 5.0 ND 356 328 1-28-72 10UU 7.87 8.31 8.0 5.8 u U U.6 5.5 313 312 All concentrations in parts per million (U) Sample taken at upper elevation, approximately 1030* (L) Sample taken at lower elevation, approximately ND None Detected ------- TABLE 8 RESULTS OF ANALYSES SAMPLING STATION C-2 Water Level (ft) pH (U) (L) Iron (U) (L) in Sulfate (U) (L) Acidity (U) (L) T. Solids (U) (L) 11-19-71 1011 7.2'i 7.69 3.59 3.^9 29-7 18.5 9-25 3.75 251 U58 11-30-71 1011 7.02 8.26 10. U 6.7 33 11 10.8 O.U 209 193 12-8-71 1010 6.76 7.57 10.3 7-77 31.0 19.2 U.o 7.3 183 302 12 -13 -71 1012 8.50 8.89 12.7 8.8 16 5 1.2 8.0 238 U6U 12-21-71 1010 8.M4 8.80 10.8 7.0 16 5 0.9 7.1 173 269 1-6-72 1012 7.09 7.55 lU.O 8.6 16 6 11.2 10.8 308 369 1-13-72 1032 6-93 7.^7 15 9 lU 8 22.8 11.0 320 352 1-20-72 1013 8.60 8.73 15.8 12.5 5 5 6.2 6.0 983 911 1-28-72 1013 8.55 8.83 10.8 8.5 3 h 3.5 3.8 783 656 All concentrations in parts per million (U) Sample taken at upper elevation, approximately 990' (L) Sample taken at, lower elevation, approximately 955' ND None Detected ------- TABLEJ) RE S ULTS OF ANAL YSE S CTv Water Level (ft) pH Iron Sulfate Acidity T. Solids SAMPLING STATION B-l 12-13-71 1219 8.6** 9-9 13 2.8 651 12-21-71 1217 8.5U fl.7 16 2ji 6U9 1-6-72 1218 7.78 3.3 15 2.9 1*39 1-13-72 1219 7.53 6 13 l'.3 652 1-20-72 1218 8.55 5.8 11 2.1 J*U3 All concentrations in parts ner million ------- TABLE 10 Water Level (ft) pH Iron Sulfate Acidity T. Solids RESULTS OF ANALYSES SAMPLING STATION B-2 11-30-71 1177 7.19 U.2 2»* 5-1 533 12-8-71 1177 7.15 6.60 2U.2 17.6 U22 12-13-71 1171* 8.08 7.3 7 1.0 UU9 12-21-71 1179 8.05 7.8 7 1.1 i+17 1-6-72 1183 7.50 6.1 7 16.0 555 1-13-72 1188 7.21 5 8 28.9 393 1-20-72 1189 8.10 7.8 7 1.3 UoU All concentrations in parts per million ------- TABLE 11 CO RESULTS OF ANALYSES SAMPLING STATION B-3 Water Level (ft) pH Iron Sulfate Acidity T. Solids 11-19-71 10U9 6.7^ 2.79 11.0 10.75 260 11-30-71 1055 7.93 ND 15 0.8 350 12-8-71 1056 6.33 6.1*9 2U.7 lU.9 519 12-13-71 1055 8.27 11.3 6 0.6 503 12-21-71 1057 8.10 12.5 5 1.6 U99 1-6-72 1059 6.50 U.9 13 18.1 325 1-13-72 1060 6.6k 26 9 16.8 501 1-20-72 1060 8.2k 16.9 U 0.6 Ma 1-28-72 1060 7.67 13.U 7 2.3 23U All concentrations in parts per million ------- There was a noticeable decrease in iron, sulfate, acidity and total solids concentrations in the mine drainage after the first two sampling tours. This may have been due to dilution from increased runoff resulting from frequent rains during this period, or to changes in the mine environment brought about by the construction activity, or both. Excavation of the fanway released impounded acid water and permitted this corridor to drain freely. - 49 - ------- SECTION VII MINE SEALING OPERATIONS The decision to place two double-bulkhead concrete seals and only one experimental chemical grout seal was prompted by the higher-than-expected cost of the grouting materials which were determined by laboratory testing to be suitable for the proposed mine sealing method. However, there were other areas in which it was felt benefits could be derived by substitution of the concrete seals at this site. 1. The potential hydraulic head that could develop on the seals if the mine filled to its highest level was 84 feet. The maximum head on any existing seal of this type was about 35 feet. Therefore, it was possible that the oppor- tunity would be afforded to evaluate the double bulkhead concrete seals under a higher pressure than that to which they had previously been exposed. 2. Installation of previous double bulkhead seals included grout stabilization of the retaining stone bulk- heads prior to placement of the concrete seals. It was believed that this step could be eliminated. Installation of double bulkhead concrete seals at the Keystone State Park test site permitted testing this modification of the construction procedure. Double Bulkhead Seals The double bulkhead concrete seals were installed in the east and west mine entries. The bulkheads are normally constructed by injecting coarse aggregate through vertical drill holes across the mine corridor and vibrating the material so that an alignment of intersecting truncated cones are formed with a minimum of four feet diameter contact zone at the mine roof. Grout is injected into the bulkheads and then a concrete plug is injected into the space between the bulkheads. Six-inch diameter injection holes were drilled across the east and west entries for placement of the bulkheads and concrete seal. The alignment of the holes was not exactly perpendicular to the bearing of the entries because they were drilled before the middle entry was opened to permit a survey. This however would be the rule rather than the exception since accurate mine maps are seldom available and openings often have to be established by exploratory drilling. From the drilling logs the east and west entries were estimated to be 12 to 14 feet wide and from 4 to 8 feet high depending on exact location. - 51 - ------- One hundred tons of aggregate, Pennsylvania Department of Highway 2-B size and grading (l/2"+0 , were placed and vibrated in the west entry through the applicable drill- holes, sixty tons for the forward bulkhead and forty tons for the rear bulkhead. In the east entry the forward bulkhead consisted of seventy-seven tons and the rear bulkhead sixty-eight tons of aggregate. Attempts at taking pictures in the mine through boreholes to examine the bulkhead location and assess the integrity of the stone bulkheads were unsuccessful due to water and high humidity which resulted in condensation on lens surfaces. A considerable amount of water was backed up in the west entry, and attempts to dewater the area by excavation in front of the entry, and by pumping were not completely successful. It was decided to inject the concrete seals without dewatering. A laboratory test showed that the concrete would set satisfactorily when poured into an acid solution simulating the mine acid, and based on the dimensions of the mine cavity and the quantities of stone placed it was concluded that in all probability the bulkheads were satisfactory. Eighteen cubic yards of concrete were poured in the east entry and thirty-five cubic yards in the west entry. The completed seals are illustrated in Figure 18. The center plug areas of the seals were pressure grouted through drill holes extending entirely through the concrete plug to below the mine floor. A total of 1472 cubic feet of flyash-cement grout were injected in the east entry seal. For grouting of the west seal calcium chloride was added as an accelerator because some seepage was noted below this entry indicating possible water movement through the seal area. A total of 3584 cubic feet of grout were injected at this location. The total cost for both double bulkhead seals in place is estimated at $30,000. This includes the grouting of the center plugs, but no curtain grouting. Test holes were drilled in the center plug areas of the double bulkhead seals downstream of the injection holes five months after the seals were placed. These holes were cored all the way through the seals to the mine floor, and revealed no discontinuity of material in either of the two concrete seals, therefore it is apparent that the mine entries are completely filled in the area of the seals. Core recovery, from the mine roof to the mine floor, was - 52 - ------- GRADE GRADE .PORTAL EAST ENTRY l4'-0"t - 6 DIA.DRILL HOLE (TYP.) 14'-0"t foSftMsA S,'// V*35C.Y. CONCRETE ^a WEST FNTRY FIGURE 18, DOUBLE BULKHEAD SEALS - 53 - ------- for the east seal and 40% for the west seal. This represents a relatively high loss but is not unusual for this type of application and may indicate only that portions of the cement matrix are weak enough to be shat- tered by the core drilling. The effectiveness of the total mass as a seal would not necessarily be impaired. Pressure testing would be required in order to assess the effectiveness of the material within the seal area as a hydraulic seal. The boring logs showed that settling of the concrete took place after the seals were poured. This could have been due in part to displacement of gob and migration of material into or through the stone bulkheads as well as movement of the bulkheads themselves. In the east seal nine inches of flyash-cement grout were found above the concrete, and in the west seal twenty-two inches of grout were recovered from between the mine roof and the concrete seal. This grout usage offset any saving that was realized by elimination of the grouting of the bulkheads, therefore there appears to be no advantage to elimination of this step in the construction procedure. Sealing of Air Vent The existing 12" diameter vent pipe, located on the first cross connection between the main entry and the fanway as shown on Figure 3, was removed and replaced with a 4-inch stainless steel pipe which was concreted in place. This pipe was fitted with a pressure gauge for possible use in monitoring the progress of water buildup in the mine after it is sealed. The gauge is mounted on a flange which may be removed entirely for sampling or measuring water level when this is below the gauge elevation. A 4" valve is also provided to serve as a possible relief device should it become necessary to lower the water level in the mine after it has exceeded the elevation of the valve. A sketch of the gauge-relief pipe is shown on Figure 19. Construction of Safety Bulkhead Because of the experimental nature of the proposed chemical grout-flyash seal, a reinforced concrete safety bulkhead was constructed in the middle entry which was selected for the test of the material. The entry, which served as the fanway when the mine was worked, was reestablished by excavation, and a diversion channel was cut to divert the drainage directly to the creek. For protection and security of the opening, a wooden entry way was built twelve feet out from the face of the mine, with cyclone fence double gate at the end. The entrance is shown on Figure 20. - 54 - ------- 4"S.S.PIPE *.r ;.«.' XI1.' PRESSURE GAUGE 4" EMERGENCY RELIEF PLASTIC BALL VALVE CONCRETE L MINE ROOF I2"± 0. D. RETAINER PLATE WELDED TO 4" PIPE FIGURE 19, PRESSURE GAUGE-RELIEF PIPE INSTALLED IN PLACE OF OLD AIR VENT ------- FIGURE 20, PROTECTION OF EXCAVATED MINE ENTRY - 56 - ------- The reinforced concrete bulkhead was located approximately 18 feet in from the face of the mine. A drainage channel and 6" drain pipe was installed in the mine floor to permit free drainage of the mine while the bulkhead was being built. A 4-inch diameter stainless steel pipe with plastic ball valve was located approximately two feet up from the mine floor to permit sampling, and to aid in the sealing operation special plexiglass windows were included for observation and light insertion. Bulkhead details are shown on Figure 21. A photograph of the completed installation is shown on Figure 22. Injection Nozzle Tests Preliminary tests in the laboratory, Figures 23 and 24, showed that an AM9-flyash slurry consisting of 15 pounds of flyash per gallon of 15% grout solution could easily form a self-supporting mass with 20 to 25 degrees angle of repose, but that proper distribution of the slurry was essential to establishment of complete closure at the mine roof. It was felt that this distribution could be accom- plished through a single injection hole by use of a nozzle that would direct the slurry outward and slightly upward so that the seal is built up from the outer extremities as previously illustrated in Figure 2. Tests were conducted with an injection nozzle consisting of two 3/8" nozzles at 180 degrees, inclined upward at 30 degrees, from the horizontal. To avoid plugging of the injection piping when using short gel times the initiator was added just ahead of the nozzle. As a result of the tests it was concluded that a satisfactory distribution could be achieved with the nozzle, and that mixing of the ammonium persulfate solution with the grout slurry just ahead of the nozzle was adequate to produce a controllable gel. The nozzle tests are illustrated on Figure 25. Pumping of the grout slurry was not continued to build up a plug in the test area in view of the high cost of the grout materials. It was hoped that with the viewing ports built into the reinforced concrete safety bulkhead the progress of the actual seal placement could be monitored closely enough so that precise step by step procedures would not have to be previously determined by large scale testing. Injection of Gel Material Due to cold weather injection of the AM9-flyash grout was delayed several weeks. It was decided to wait until at least two days of above freezing temperatures were reasonable assured before attempting to place the seal. - 57 - ------- DEEP DRAINAGE TRENCH 6 DIA.SCH.IO S.S.PIPE (TYPE 3O4) ENCASED IN CONCRETE. 4"DIA.SCH.IO S.S.PIPE ft 4"FLGD. PLASTIC BALL VALVE FOR SAMPLING FLOW a EMERGENCY RELIEF. I 4'-6 (MINE CLEARANCE) PLAN -6"DIA.INJECTION HOLE TO GRADE s (0 1 I2"SQ.PLEXIGLASS WINDOW 6"DIA.PLEXIGLASS WINDOWS ELEVATION SLIP ON FLANGE WITH BLIND FLANGE FIGURE 21, CONCRETE BULKHEAD - 58 - ------- . - -' »" **" "» FIGURE 22, VIEW OF CONCRETE SAFETY BULKHEAD - 59 - ------- FIGURE 23, BENCH SCALE TEST OF GEL MATERIAL If FIGURE 24, ANGLE OF REPOSE ACHIEVED IN LAB TEST - 60 - ------- . r « - \ , .'«*-? p FIGURE 25, YARD TESTS OF INJECTION NOZZLE ------- On February 28, 1972, with a warm trend predicted, preparations were made for the grouting operation. The next day, final tests were run to check out equipment and determine approximate proportions and gel times, using water from the site at prevailing temperature and flyash from the batch to be used in the actual grout mix, and on March 1 injection of the grout into the mine began. Flyash, AM-9 and catalyst DMAPN were batch mixed in a 2500 gallon, two-compartment slurry batcher, shown on Figure 26 with a material weigh bin above it. From the batcher the slurry was pumped to a small hopper feeding progressive cavity type injection pump of 30 gpm capacity. Ammonium persul- fate, the reaction initiator, was fed by a smaller pump into the injection pipe just ahead of the nozzle. The injection pipe and pumps are shown on Figure 27. Lights were inserted in the 6" diameter ports in the safety bulkhead for illumination of the mine cavity, but visibility was poor due to condensation and obstructions which blocked view of the injection point. Figure 28 shows the view through the bulkhead. The injection nozzle was oriented to direct the slurry stream toward the walls and the grout pumped at a rate of 30 gallons per minute with a gel time of approximately 15 seconds. The anticipated result of this procedure was that a wedge shaped mass would be built up on each side of the mine corridor, starting at the walls and sloping downward toward the middle where the mine drainage was observed to be flowing. With proper control of the gel time it was hoped that the two wedge shaped formations could be gradually extended into the drainage channel eventually damming the flow and causing it to spread out behind the grout dam. However, this was not successful. Observation of the drainage from the mine indicated that much of the grout material was being lost. The gel time was decreased from fifteen seconds to as low as five seconds with no success in stopping grout loss. A satisfactory gel was apparently achieved on both sides of the entry, as evidenced by inability to remove the catalyst injection hose when the operation was terminated, but the flow in the middle of the mine floor was too high to permit a gel to form. The flow from the. mine measured by a v-notch weir was found to be approximately 150 gallons per minute. This was considerably higher than the 40 to 50 gallons per minute measured a week earlier and was due to runoff brought about by the sudden onset of very warm weather. The air temperature rose to above 70°F during this period. - 62 - ------- FIGURE 26, SLURRY BATCHER AND WEIGH BIN - 63 - ------- FIGURE 27, SLURRY INJECTION PIPE AND PUMPING EQUIPMENT - 64 - ------- FIGURE 28, VIEW OF MINE ENTRY THROUGH OBSERVATION WINDOW IN BULKHEAD - 65 - ------- Due to the high flow much of the grout was diluted to the point where it failed to gel, and the material that did gel at the edge of the flowing water was washed away. Some gelled material was collected outside the mine entrance indicating that some of the grout had indeed formed weak gels which were transported away by the flow- ing water. In view of the previously established high cost of grout materials and the difficulties experienced in applying the injection technique with the high mine flow, the decision was made after consultation with State and Federal project sponsors, to terminate the test. It was felt that the method may be successful in low flow situations, and with higher injection rate to minimize dilution and erosion of the grout, but the cost remained prohibitive. Acid drainage abatement activities and sampling at the mine site have been interrupted to permit compilation and review of all information relative to the project prior to completion of the work. In order to retain the possi- bility of using the mine entry for further experimental work, the reinforced concrete safety bulkhead was left free-draining to minimize accumulation of gob which may block off the view ports. Work remaining to complete normal abatement procedures at the Salem No. 2 mine, if no further experimental work is planned, consist of injection of a grout curtain in the strata adjacent to the mine entries. - 66 - ------- SECTION VIII ACKNOWLEDGEMENTS Mr. Ronald D. Hill, Chief, Mine Drainage Pollution Control Activities, National Environmental Research Center, Cincinnati, Ohio, who was the EPA Project Officer, and Dr. David R. Maneval who served as Project Director for the Department of Environmental Resources, Common- wealth of Pennsylvania, offered many helpful suggestions and comments during the course of this investigation. Their valuable assistance is gratefully acknowledged. This report was prepared by Neville K. Chung, Dravo Corporation, Pittsburgh, Pennsylvania 15222. U. S. GOVERNMENT PRINTING OFFICE : L973 514-151/140 - 67 - ------- Acc«*ulcn Number w Sabjoct Field & Group SELECTED WATER RESOURCES ABSTRACTS INPUT TRANSACTION FORM OitfartlzaUon Dravo Corporation Title Investigation of use of gel material for mine sealing Chung, Neville K. Project D*ml£p*ttoa EPA, Grant No. 14010 EKW Woto Environmental Protection Agency report number, EPA-R2-72-135, December 1972. 23 I Dt>*cHplon (Starred Pint) *Acid mine water, *Mine drainage, *Mine sealing, Abatement \ldentifior* (Starred Flrmt) Chemical grout Abstract Laboratory testing of commercially available chemical grouts was conducted to evaluate their potential use, in conjunction with a cheap filler, for remote sealing of mine voids. By close control of the setting time and proper distribution of the grout slurry it was believed that a mine seal could be placed through a borehole from the surface without the benefit of retaining bulkheads. A slurry mix consisting of an acrylamide grout with flyash or mine refuse as a filler was found to produce a strong controllable gel which resisted chemical attack in the laboratory over an eleven week exposure period. An attempt to demonstrate a novel technique for application of the selected grout slurry in a mine entry with high flow was not successful. The results suggest that the technique may be applicable in dry or low flow situations. However, the estimated cost of a mine seal using the gel material is presently not competitive with existing methods. Groundwater monitor wells were drilled for the purpose of determining the effect of mine sealing on groundwater conditions. Data reflecting pre-seal conditions was compiled, but because the sealing of the mine was not completed the monitoring program has been postponed. Abstractor, Neville R. Chung Dravo Corporation WR:I02 WRSIC (REV. JUt-Y IB41I SEND. WITH COPY OF DOCUMENT. TO: HATER RESOURCE* SCIENTIFIC INFORMATION CENTER U.S. DEPARTMENT OF THE INTERIOR WASHINGTON. D. C. 2O24O CPO! 1S70 - 4O7 ->91 ------- |