ENVIRONMENTAL PROTECTION ACENCV
OFFICE OF ENFORCEMENT
E PA-330/2-79-005
Evaluation Of The
Hopewell Regional Wastewater Treatment Facility
Hopewell, Virginia
NATIONAL ENFORCEMENT INVESTIGATIONS CENTER
DENVER,COLORADO
AND
REGION III. PHILADELPHIA. PENNSYLVANIA

JANUARY 1979
\W<
PRO^


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ENVIRONMENTAL PROTECTION AGENCY
Office of Enforcement
EPA-330/2-79-005
EVALUATION OF THE HOPEWELL REGIONAL WASTEWATER
TREATMENT FACILITY
HOPEWELL, VIRGINIA
Arthur N. Masse
January 1979
National Enforcement Investigations Center - Denver, Colorado
and
Region III, Philadelphia, Pennsylvania

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TABLE OF CONTENTS
I INTRODUCTION 		1
II SUMMARY AND CONCLUSIONS		2
Summmary 		2
Conclusions 		2
Solids Handling System 		2
Plant Design		3
Influent Characteristics 		4
Operation and Maintenance 		5
Laboratory Methodology 		6
III PROCESS DESCRIPTION		7
IV STUDY FINDINGS 		9
Solids Handling System 		9
Plant Design	11
Influent Characteristics 		12
Operation and Maintenance 		15
Laboratory Methodology 		16
REFERENCES
Figure 1		8
Table 1 	13

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I. INTRODUCTION
EPA Region III requested the National Enforcement Investigations
Center (NEIC) to determine the reasons for the "consistent and severe"
violations of NPDES* permit limitations reported by the Hopewell, Vir-
ginia Regional Wastewater Treatment Facility (HRWTF). The Discharge
Monitoring Reports (DMR) submitted by the plant showed that they had
been in compliance with their effluent limitations only once since the
beginning of operations in August 1977. From October 1977 through Novem-
ber 1978, the monthly average effluent biochemical oxygen demand (BOD)
concentrations had averaged 135 mg/1 and the weekly average BOD concen-
trations had averaged 266 mg/1. The respective effluent limitations are
30 and 45 mg/1.
In the same time period, the monthly average effluent total sus-
pended solids (TSS) concentrations had averaged 180 mg/1 and the weekly
average TSS concentrations had averaged 625 mg/1. The respective
effluent limitations for TSS are 50 and 75 mg/1.
NEIC engineers reviewed the Regional Office and plant files and
inspected the Hopewell facility in October 1978. Plant contacts were
Mr. Thomas Kirtley and Mr. Joseph Joseph.
* National Pollutant Discharge Elimination System

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II. SUMMARY AND CONCLUSIONS
SUMMARY
Operator's data sheets and logs, pilot plant records, design draw-
ings, Discharge Monitoring Reports and correspondence among the City,
vendors and regulatory agencies were studied in an effort to determine
the reasons for the plant's inability to meet its permit limitations. A
detailed plant inspection was made, the laboratory procedures were eval-
uated and standard samples for BOD and TSS were left with the laboratory
staff to determine the accuracy of their results.
The suppliers of some of the major pieces of equipment that were
found to be inoperative were contacted and asked what was being done to
make their equipment perform as expected.
NEIC engineers concentrated their efforts on evaluation of the
plant's solids handling system, the plant design, the influent charac-
teristics, the operating and maintenance procedures and the laboratory
methodology.
CONCLUSIONS
Solids Handling System
The inability to remove suspended solids effectively before dis-
charge is the major cause of the very high BOD and TSS levels reported
in the effluent. Statistical analysis of the effluent BOD and TSS
data showed that most of the BOD in the effluent was associated with
suspended solids.

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3
A high solids recycle load to the aeration basins and secondary
settling tanks is one of the principal causes of the high suspended
solids in the final effluent. The recycle stream from the gravity
sludge thickeners to the aeration basins was reported to contain as much
as 453,000 kg (1,000,000 lb)/day of suspended solids, almost 100 times
the design load of 4,940 kg (10,906 lb)/day.
This high solids load in the supernatant from the gravity sludge
thickener is caused by several factors. One is the failure of the
dissolved air flotation (DAF) thickeners to concentrate the waste acti-
vated sludge. Because of this, the waste activated sludge must be con-
centrated in the gravity sludge thickeners which were designed to
thicken only the primary sludge.
In addition, the sludge disposal system, consisting of a heat
treatment system, vacuum filters and a multiple hearth incinerator is
not functioning at full effectiveness because of large and frequent
leaks in the heat treatment system. Because of this, solids cannot be
removed from the gravity sludge thickeners at the design rate.
The high solids load in the feed to the gravity sludge thickeners
and the inability to remove solids from these thickeners at the design
rate combine to increase the solids in the supernatant return to the
aeration basins.
Plant Design
Frequent shutdowns of one or more of the final settling tanks
result in an overload on the operating tanks and cause an increase in
the suspended solids content of the final effluent. The majority of the
shutdowns are a result of the failure of the sludge return pumps that
have been experienced. Two of the eight secondary settling tanks were

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4
out of service at the time of the NEIC inspection because of pump fai-
lure and the plant staff stated that this is a frequent occurrence.
The inability to control the sludge level in the secondary settling
tanks is an additional cause of high suspended solids in the final
effluent. The sludge level finder installed on the secondary settling
tanks was ineffective because it was installed in the zone of influence
of the sludge return pumps. In addition, the plant as designed and
installed did not include a flow measuring device on the return sludge
line from each pump. Thus, it is not possible to measure the sludge
removal rate from the individual tanks. These two factors prevented
stable operation of the secondary settling tanks.
Surge loads of TSS and BOD resulting from upsets in the sludge
handling system contribute to uneven operation of the biological treat-
ment system and to a high solids concentration in the final effluent.
The return of all of the supernatant from the gravity thickeners directly
to the aeration tanks imposes an unnecessarily high and variable load of
BOD and TSS on the biological system. The supernatant from these
thickeners includes the water removed from the primary and secondary
waste activated sludges, incinerator scrubber water, filtrate from the
vacuum filters, decant tank overflow and the flow from all floor drains
in the solids handling area. The thickener supernatant could be returned
to the plant influent, allowing the primary settling tanks to equalize
these flows and remove some of the TSS and BOD.
Influent Characterises
Rapid, large variations in the temperature of the wastewater
entering the plant cause unstable operating conditions in the plant and
prevent effective bio-oxidation of the influent organics. An influent
temperature variation as high as 10°C (18°F) in one 24-hour period was
noted.

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5
Sudden surges in the BOD load to the plant also prevented the
development of a stable bio-mass and thus the effective removal of BOD
and TSS on a continuous basis. The analysis of daily composite samples
of influent did not show daily BOD loads over 150% of the design load
but the operators stated that surge loads as high as 600 to 700% of the
design BOD load were fed to the plant for periods up to six hours.
No data are available on the presence of biologically inhibitory
materials but samples of the influent and effluent have been taken and
are being analyzed for complex organic materials and heavy metals. A
subsequent report will discuss the findings of these analyses.
Operation and Maintenance
Operation of only three of the four parallel aeration systems
contributed to overloaded operating conditions and deterioration of
effluent quality. Only three of the aeration tanks'were kept in service
to prevent underloaded operating conditions which could result in endo-
genous respiration and impaired sludge settling characteristics. This
practice, however, resulted in extreme overloads to the operating sys-
tems during surge loads.
Efficient operation of the activated sludge plant is hampered by
the inability to measure the activated sludge waste rate. The flow
measuring devices in the sludge waste lines were inoperable at the
time of the inspection and, according to the plant staff, had not been
operable for some time.
The lack of control of the addition of nutrients (nitrogen and
phosphorus) to the system may be limiting the biological oxidation of
organic materials. The influent wastewater contains some nitrogen but
very little phosphorous. Phosphorous, as phosphoric acid, is added but

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6
it is not paced with the influent organic load as it should be. Nitro-
gen was not being added at the time of the visit.
Unequal distribution of flow to the final settling tanks results in
inferior effluent quality from the overloaded tanks. The flow over the
weirs of the final settling tanks varied enough from one tank to another
that it was immediately obvious visually.
Laboratory Methodology
The HRWTF was using correct analytical methods for the permit
parameters. Standard samples for BOD analysis were left with the labor-
atory and the results received were within acceptable accuracy. A
standard sample for TSS was also left with HRWTF but it was later dis-
covered that this sample had been prepared incorrectly by the supplier
so the TSS accuracy could not be checked.

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III. PROCESS DESCRIPTION
3
Figure 1 is a flow diagram of the 189,000 m /day (50 mgd) Hopewell
Regional Wastewater Treatment Facility provided by plant personnel.
The figure contains information on equipment design, flow rates and
design loadings for BOD and TSS.
The treatment sequence at the HRWTF includes screening, grit
removal, primary sedimentation, activated sludge aeration using the
UNOX* pure oxygen process and final sedimentation. Primary sludge is
passed through a Hydrogritter (not in original design) for additional
grit removal and pumped to gravity thickeners. Waste activated sludge
was to be thickened in dissolved air flotation (DAF) units and mixed
with the thickened primary sludge. However, the DAF units are not
working so the waste activated sludge is pumped directly to the gravity
thickeners, bypassing the DAF units.
The thickened sludge (primary and waste activated) is treated in
Porteous heat treatment units which break down the cell structure and
make sludge dewatering easier. The heat treated sludge is then de-
canted, dewatered on vacuum filters and burned in a multiple hearth
furnace.
All of the recycle streams (heat treatment decant overflow, fil-
trate, furnace scrubber water) flow to the gravity thickener. The
thickener supernatant is pumped to the aeration tanks.
* Mention of commercial products, processes or equipment does not imply
endorsement by the Environmental Protection Agency.

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PAGE NOT
AVAILABLE
DIGITALLY

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IV. STUDY FINDINGS
SOLIDS HANDLING SYSTEM
Linear regression analysis of the effluent BOD and TSS data showed
a good correlation (correlation coefficient = 0.83) between these two
parameters. A similar analysis of the relationship between effluent TSS
and that part of the BOD not passing a laboratory filter (BOD contri-
buted by suspended solids) showed a correlation coefficient of 0.97.
These results indicate that one of the reasons for the high BOD in the
effluent is the inability to remove solids from the wastewater before
discharge. Much of this problem is believed to be the result of prob-
lems in the solids handling system.
The plant design [Figure 1] indicated that the recycle of solids to
the aeration tanks from the gravity sludge thickeners would amount to
4,530 kg (10,000 lb)/day. The data evaluated show solids recycle loads
from this source of up to 85,600 kg (189,000 lb)/day and it has been
reported^ that the solids concentration in this stream gets up to 2% in
a flow of 6 mgd (453,000 kg/day-1,000,000 lb/day).
There are two main reasons for this high load of solids leaving the
gravity thickeners. The first of these is that the gravity thickeners
are being used to thicken the waste activated sludge as well as the
primary sludge. They were designed to thicken only the primary sludge.
Dissolved air flotation units were installed to thicken the waste acti-
vated sludge but they have not been effective in accomplishing this and
have been bypassed. The units supplier (Komiine-Sanderson) was con-
tacted to determine the reasons for this failure to perform as anti-
2
cipated. Research work by Komiine-Sanderson and others has indicated
that the source of the problem is the anti-foaming agent added to the

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10
aeration tanks. This agent is necessary to prevent the formation of
massive amounts of foam in the aeration tanks and release of this foam
in the settling tanks.
Another cause of the high solids in the gravity sludge thickener
supernatant return to the aeration tanks is the inability to remove
solids from the thickeners at the design rate. If solids are not
removed at as high a rate as necessary, they build up in the thickeners
and eventually overflow in the supernatant.
The normal flow path for sludge from the gravity sludge thickeners
is to a sludge holding tank, then through a heat exchanger to the heated
reactor, and back through the heat exchanger to a decant tank. The
decant liquor flows to the gravity thickener and the separated heat-
treated solids are dewatered on a vacuum filter and burned in a multiple
hearth furnace. There are three heat exchanger-reactor systems installed
at the HRWTF but only one of these was operational at the time of the
NEIC inspection. The plant staff said that two'of the units are down
for repair most of the time. The major problem is that the head gas-
kets in the heat exchangers leak badly and the units cannot be operated
under these conditions.
These heat treatment units, known as the Porteous Process, were
supplied by the Envirotech Corporation. The Envirotech engineers con-
tacted3 said that the problem was the result of improper design by the
supplier of the heat exchangers. Envirotech is now welding the head
gaskets shut and believes that this will enable continuous operation of
the heat treatment system.
Proper operation of both the dissolved air flotation units and the
heat treatment system should result in a decrease in the amount of
solids being recycled to the aeration tanks from the gravity sludge
thickeners. This will decrease the solids load in the aeration tanks
and secondary settling tanks and decrease the suspended solids content
of the final effluent.

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11
PLANT DESIGN
Frequent maintenance requirements on the sludge return pumps in the
final settling tanks cause frequent shutdown of these tanks with the
resultant overload of the tanks remaining in operation. The drive shaft
between the motor and the sludge return pump is over 16 ft long and
frequent bearing trouble has necessitated shutdown and maintenance.
More conventional design would have the motor and pump located in pipe
galleries below the settling tanks and would include a piping system so
that failure of one pump would not force shutdown of a settling tank.
Sludge level finders were installed to enable the maintenance of
a constant sludge level and stable conditions in the settling tanks but
these sludge finders were installed in the zone of influence of the
sludge return pump. Therefore, they do not give a correct measure of
the depth of sludge in the settling tanks and have not promoted stable
operation.
The sludge return pumps are variable speeds but the design did not
include flow monitoring devices on the individual pump discharge lines.
Without a flow monitoring device, the sludge return rate cannot be con-
trolled to the degree necessary to maintain stable operation of either
the final settling tanks or the aeration tanks.
All of the recycle streams from the solids handling system are
returned to the main stream just before the aeration tanks. This
arrangement maximizes BOD and TSS load and the effect of upsets in the
sludge handling system on the biological system. More conventional
design would divert these recycle streams to the head of the plant, thus
taking advantage of the BOD and TSS removal and equalization capabilities
of the primary settling tanks.

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12
INFLUENT CHARACTERISTICS
The plant was designed to treat an influent to which industry con-
tributes over 80% of the hydraulic load, 90% of the BOD load and 70% of
the TSS load [Table 1].
Table 1 also shows the maximum temperature reached by several of
the contributors to the HRWTF during August 1978, the hottest month for
the individual contributors. In July 1978, the wastewater temperature
at the plant influent ranged from 40 to 54°C (104-129°F). Efficient
biological systems can be operated at temperatures in this range but
high variations in temperatures will decrease the efficiency.4'5'6 The
inlet temperature at HRWTF changed as much as 10°C (18°F) from one day
to the next.
Between June 1 and October 10, 1978, the hydraulic flow to the
plant exceeded 50 mgd only three times, the maximum flow being 10,200
m /day (62.7 mgd). The BOD design influent load was exceeded 29 times
during this period, the highest daily load being 95,700 kg (211,000
lb)/day. With only three of the four aeration tanks on stream, this is
equivalent to a BOD load of 127,500 kg (281,000 lb)/day - twice the
design BOD load. The influent TSS exceeded the design load four times
in this time period, with the maximum daily load being over 227,000 kg
(500,000 lb)/day. This high load was reported to be a result of back-
washing wastes from the Virginia American Water Co.^
The only information available to the investigators on BOD loads
to the plant was the daily average values which, as stated above, reached
95,700 kg (211,000 lb)/day. However, the operators stated® that BOD
loads to the plant got as high as 600 to 700% of design for periods of
up to six hours. These loads were reported to be caused by spills and
upset conditions at the contributing industries.

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Table 1
Design Flows and Loads to Hopewell
Regional Wastewater Treatment Facility
Source
n Flow
BOD
TSS
High Temp
m /day
(mgd) kg/day (lb/day)
kg/day
(lb/day)
Aug 78
°C (°F)
Industrial







Firestone
2,600
(0.7)
1,100 (2,418)
50
(116)
40
(104)
Hercules
38,200
(10.0)
28,700 (63,327)
8,300
(18,332)
42
(108)
Allied
17,000
(4.5)
6,800 (15,000)
1,100
(2,330)
49
(120)
Chemical






(140)
Continental
81,400
(21.6)
17,100 (37,800)
27,000
(59,500)
60
Forest







Industries







Domestic







Fort Lee
9,500
(2.5)
1,700 (3,850)
2,500
(5,410)
-
-
Hopewel 1
15,100
(4.0)
2,800 (6,160)
3,900
(8,658)
30
(86)
Old Dominion
4,900
(1.3)
-
6,800
(15,000)
-
-
Totals
168,700
(44.6)
58,200(128,555)
49,650 (109,346)
-
-
Reserve
20,300
(5.4)
5,800 (12,808)
6,000
(13,252)
-
-
Totals
189,000
(50.0)
64,000(141,363)
55,650 (122,598)
-
-
* Taken from "Hopewell Regional Wastewater Treatment Facility Aqreement,"
July 1, 1975.

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14
In July 1978, the industries contributing to the HRWTF, conducted a
g
statistical study indicating a calculated BOD range from 37,000 to
89,200 kg (82,000 to 197,000 lb)/day in the influent (ratio of 2.4:1)
and a TSS range from 18,500 to 75,200 kg (40,800 to 166,000 lb)/day
(ratio of 4.1:1). These ranges could be reduced by revised operating
procedures at the contributing industries. For example, Hercules has an
83,200 m^ (22x10^g) holding basin at their plant, 56,800 (15x10^g) of
this being available for surge capacity. Hercules also has a "chemical
cotton" process which, because of market conditions, is on stream for 10
days and off for 4 days on a regular cycle. The effluent stream from
the chemical cotton process, which enters the holding basin, averages
22,700 m^/day (6 mgd) and has an average BOD of 800 mg/1. All other
waste streams entering the holding basin average 15,100 m /day (4 mgd)
and have an average BOD of 1,600 mg/1. When the chemical cotton process
shuts down after 10 days of operation, the flow from the holding pond to
the HRWTF is reduced to a lower level for 4 days. During this time
period, the BOD concentration in the holding pond is increasing because
the lower strength chemical cotton wastes are not entering the pond. At
the end of the four day "off period" for the chemical cotton process,
this process is started up and the volume into the holding pond is
increased. At this time, the holding pond is at its maximum BOD con-
centration. Also at this time, the flow rate to the HRWTF is increased,
causing the maximum possible load from Hercules to the HRWTF and un-
stable slug loading to the HRWTF.
CFI and Firestone also have holding ponds but their sizes and
methods of operation were not determined.
Little information is available on the presence of heavy metals or
complex organics in the plant influent. If present, these materials
could inhibit the biological process. A pilot plant study of the UN0X
process conducted by a consulting engineering firm found that the Fire-
stone and City of Hopewell discharges contained chemicals that inhibited

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15
biological activity.^ Inhibitory materials were found later when con-
ducting a BOD study.^ However, in the latter study it was reported
that the bacteria could be acclimated to degrade all of the chemicals in
the influent. Samples of the influent and effluent were taken by the
EPA (Region III) and are being analyzed for complex organic chemicals
and heavy metals. The results of these analyses and the effect of the
influent characteristics on the biological system will be discussed in a
subsequent report.
OPERATION AND MAINTENANCE
During the inspection, only three of the four aeration tanks were
on stream. The fourth was not on stream because it was believed that,
during normal operation, the organic content of the wastes would not be
high enough to prevent endogenous respiration and the formation of
solids that would not settle. This practice served to amplify the
overload conditions when sudden surges in the influent BOD were received
from the industrial contributors. Since the inspection, all four aera-
tion tanks have been put in service and the effluent quality has improved.
The flow monitoring devices on the activated sludge waste lines
were not working at the time of the NEIC visit	and, according to the
operating staff, had not been working for some	time. Control of the
activated sludge waste rate is one of the most	important activities
available for maximizing the performance of an	activated sludge system.
The inability to measure this waste rate makes	efficient operation
difficult, if not impossible.
Biological treatment systems require the presence of nitrogen and
phosphorous as nutrients for growth of the organisms. Facilities for
adding both of these nutrients to the wastewater were provided at HRWTF.
However, nitrogen was not being added at Hopewell and phosphorous is
being added but no information was available on whether or not either

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16
nutrient was present in sufficient quantity. Conventional practice
calls for adding nutrients so as to maintain fixed ratios between BOD
and nitrogen and BOD and phosphorous.
The inspection revealed unequal distribution of mixed liquor into
the final settling tanks. The flow over the weirs was obviously dif-
ferent between tanks. No correlation was noted between effluent quality
and the rate of flow over the weirs but unequal distribution would
undoubtedly degrade effluent quality during periods of high hydraulic
load.
LABORATORY METHODOLOGY
The BOD and TSS procedures used and the associated laboratory
equipment were judged as satisfactory. Standard samples for BOD analyses
having true BOD concentrations of 28.7 and 264 mg/1 were left with the
HRWTF for analysis. The laboratory reported values of 30 and 295 mg/1,
respectively. Both of these values are within acceptable limits.
Standard samples for TSS analyses were also left with HRWTF but
it was later determined that the samples had been incorrectly prepared
by the supplier so no accuracy check of the HRWTP TSS analyses was
possible.

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REFERENCES
1.	Private communication
2.	Record of telephone conversation with Komiine-Sanderson,
December 7, 1978
3.	Record of telephone conversation with Envirotech Corporation,
December 5, 1978.
4.	Record of telephone conversation with Dr. Basim Sayigh, Snell
Environmental Group, Lansing, Michigan, December 5, 1978.
5.	Record of telephone conversation with Dr. A.A. Friedman, Syracuse
University, December 5, 1978.
6.	Record of telephone conversation with Dr. Lin, University of New
Brunswick, December 5, 1978.
7.	"Plant Influent Sheet" August, 1978.
8.	Telephone conversation with Hopewell plant, December 1978.
9.	"Basis for Statistical Analyses," July 26, 1978.
10.	"Wastewater Treatment - Pilot Plant Report for the City of Hope-
well - Hopewell, Virginia," February 1974, Union Carbide Corporation.
11.	"Management Study for the Hopewell Regional Wastewater Commission,"
Arthur Beard Engineers Inc., June 1978.

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