c/EPA
               Unitod States
               Environmental
               Acency
                Municipal Environments! riosearch 1'PA GOO 'j '/;)() I 3
                Lotwratbry           Juiu.- I')/'.)
                Cincinnati OH 45260
               Resoofdi ond Development
Oxygen
Newtown  Creek

-------
                              U.S. DEPARTMENT OF COMMERCE
                              National Technical Information Service
                              PB-297 657
Oxygen                  at
Newtown
New York City Environmental Protection Administration
Prepared for
Municipal Environmental Research Lab, Cincinnati, OH

Jun 79

-------
                RESEARCH REPORTING SERIES

Research reports ol the Office ol Research ;ind Development  U S I nviionionnt/ii
Protection Agency have boon grouped into nine ',(,"11;!; I hose nm<> bruad cnle
oories wore established to facilitate further dc'velopmont and application ol en
vironinontal technology  (Jirnmation  ol trnditionril rjroupiruj  was consciuusly
planned to (osier technology Iransler and a n'axunu'n mlerlacf in K'l.ilc'd tic-Id';
The nine series are

      I   Environmental Health tllects Research
      2   Environmental Prelection Technology
      3   Ecological  Rese-aich
      4   Environmental Monitoring
      5   Socioc'"onomic Environmental Studies
      G   ScienUic and  Technical Assessment Reports (STAR)
      7   Interagency Energy-F:'^':ronm(;nt Research and D(>vL'lor)menl
      8   'Special Reports
      9   Miscellaneous Reports

This report has been assigned to the ENVIRONMENTAL PROTECTION TECH-
NOLOGY series. This series describes research performed to develop and dem-
onstrate instrumentation, equipment, and methodology to repair or prevent en-
vironmental degradation from point arid non-point sources of pollution This work
provides the new or improved technology required for the control and treatment
of pollution sources to meet environmental quality standards
 This document is available to the public through the National Technical informa-
 tion Service. Springfield. Virginia 22161

-------
1 HF.f'ORT NO.
 EPA-600/2-79-013
                             TECHNICAL REPOH1 DATA
                       (I'lcasc rent] tiisiniciiini! on ilie reverse lieftirt i
                         _
4. TITLE ANDSUOTITUG


  OXYGEN AERATION AT NEWTOWN CREEK
                                                 &. RLI'ORT DATE

                                                 _ J.un e . 19.75._. lJ>; a u i n g Da t a)
                                                 C. I'Ll'FORMINO OHGANIXAI ION COO I:
                         Paul J. Krasnoff
7. AUTHOR(S)
 Norman Nash
 William B.  Pressmen	
9, PERFORMING OfiG '\NIZATION NAME AND ADDRESS
 The  City of New York
 Departmenc of Environmental  Protection
 2358 Municipal Building
 New  York,  New York  10007
                                                  0. PERFORMING ORGANIZATION REPORT NO,
                                                  10. PROGRAM ELfcMENT NO.
                                                               NO".~
                                                  Grant No. S802714
 2. SPONSORING AGENCY NAME AND ADDRESS Cincinnati,  Oil
  Municipal Environmental Research Laboratory
  Office of Research  and  Development
  U.S.  Environmental  Protection Agency
  Cincinnati, Ohio 45268
                                                  13. TYPE OF REPORT AND PERIOD COVERED
                                                  Final,  05/72 - Q3/75	
                                                  HI. SPONSORING AGENCY CODE
                                                       EPA/600/14
15. SUPPLEMENTARY NOTES
  Project Officer:
                    Richard C.  Brenner, ( 513)-684-7657
16. ABSTRACT--A successful  initial feasibility  investigation of oxygen
  aeration at the 0.11-m3/sec  (2.5-higd) municipal  wastewater treatment
  plant in Batavia, New York,  prompted a larger  demonstration at New  York
  City's 13.6-m3/sec  (310-mgd)  Newtown Creek Plant.   A 34-mo evaluation
  was  performed in a self-contained set of  plant tanks using a 13.6-
  metric ton/day  (15-ton/day)  oxygen generator with  liquid oxygen backup
  for  oxygen supply and turbine mixers and  spargers  for oxygen
  dissolution.  For the 34-mo  period, at influent  flows of 0.44 to  1.53
  m3/sec (10 to 35 mgd) , effluent quality averaged 19 ing/1. each of  BOD
  and  suspended solids  for  removal efficiencies  of 88 and 86 percent,
  respectively.  Removals were not impaired by intentional hydraulic
  and  BOD overloading of the oxygenation system.   During the winter
  months, a fungus in the influent sewage caused the oxygenation system
  biomass to become filamentous,  resulting  in a  deterioration of sludge
  settling and thickening characteristics to varying degrees over the
  three winters of the  testing program.  While operating difficulties
  occurred, this condition  had no significant effect on the plant
  effluent quality.
                           KEY WORDS AND DOCUMENT ANALYSIS
               DESCRIPTORS
 Sewage  treatment, *Activated  sludge
 process,  *Oxygenation, Aeration
 tanks,  Sedimentation t^nks, *Oxygen,
 Upgrading
                                       b.lDF.NTIFIEHS/OPLN ENDED TERMS
                                       DTs solution,
                                       *0xygen activated
                                       sludge system,  *Pres-
                                       sure swing adsorp-
                                       tion oxygen gas
                                       generation, Submerged
                                       turbine sparger,
                                       *Covered tank
                                                             c. COSATI i'lcld/Croup
13B
IS. DISTRIBUTION STATEMENT

 Release  to  Public
                                       19. SECURITY CLASS (TliiS Report)
                                       Unclassified
                                                             21. NO. OF PAGES
                                       2O. SECURITY CLASS (This page)

                                       Unclassified	
                                                             22. PRICE
                                                                  - A® i
EPA Form 2220-1 (9-73)
                                           . S. GOVERNMENT PRINTING OFFICE: W?-557-060/1663 Region No. 5-11

-------
                                     EPA-600/2-79-013
                                     June  1979
    OXYGEN AERATION  AT  NEWTOWN  CREEK
                     by

                Norman Nash
            William B. Pressman
             Paul  J.  Krasnoff
  Environmental  Protection Administration
           The City of New York
         New York,  New York 10007
             Grant No. S802714
              Project Officer

            Richard C. Brenner
       Wastewater Research Division
Municipal Environmental Research Laboratory
          Cincinnati, Ohio 45268
MUNICIPAL ENVIRONMENTAL RESEARCH LABORATORY
    OFFICE OF RESEARCH AND DEVELOPMENT
   U.S. ENVIRONMENTAL PROTECTION AGENCY
          CINCINNATI, OHIO 45268

-------
                           DISCLAIMER
     This report has been reviewed by the Municipal Environmental
Research Laboratory, U.S. Environmental Protection Agency,  and
approved for publication.  Approval does not signify that the
contents necessarily reflect the views and policies of the  U.S.
Environmental Protection Agency, nor does mention of trade  names
or commercial products constitute endorsement or recommendation
for use.

-------
                            FOREWORD
     The Environmental Protection Agency was created because of
increasing public and government concern about the dangers of
pollution to the health and welfare of the American people.  Nox-
ious air, foul water, and spoiled land are tragic testimony to
the deterioration of our natural environment.  The complexity of
that environment and the interplay between its components require
a concentrated and integrated attack on the problem.

     Research and development is that necessary first step in
problem solution, and it involves defining the problem, measuring
its impact, and searching for solutions.  The Municipal Environ-
mental Research Laboratory develops new and improved technology
and systems for the prevention, treatment, and management of
wastewater and solid and hazardous waste pollutant discharges
from municipal and community sources, for the preservation and
treatment of public drinking water supplies, and to minimize the
adverse economic, social, health, and aesthetic effects of pol-
lution.  This publication is one of the products of that re-
search; a most vital communications link between the researcher
and the user community.

     As part of these activities, a pro^f-ct was undertaken in
New York City in mid-1970 to construct and demonstrate a large-
scale municipal oxygen activated sluage system as a follow-up
to successful feasibility studies completed several months
earlier at Batavia, New York.  The information documented in this
report from that project should be carefully evaluated by design
engineers and municipal officials responsible for wastewater
treatment process selection.
                                F]arcis T. Mayo, rxrector
                                Municipal Enviro:,.  nral Research
                                Laboratory-

-------
                           ABSTRACT


     A successful initial feasibility investigation of oxygon
aeration at the 0.11-m3/sec (2.5-mgd) municipal wastuwater treat-
ment plant in Batavia, New York, prompted a larger demonstration
at New York City's 13.6-m3/sec  (310-mgd) Newtown Creek Plant.
The U.S. Environmental Protection Agency desired to further
evaluate oxygen aeration on a scale sufficiently large to esta-
blish reliable engineering design and cost data, and the City
saw the process as a possibility for upgrading the plant's modi-
fied aeration process to step aeration efficiency.  A 34-mo
evaluation was performed in a self-contained set of plant tanks
using :< 13.6-metric ton/day (15-ton/day) oxygen generator with
liquid oxygen backup for oxygen supply and turbine mixers and
spargers for oxygen dissolution.  For the 34-mo period, at
influent flows of 0.44 to 1.53  m3/sec (10 to 35 mgd), effluent
quality averaged 19 mg/1 each of BOD and suspended solids  (SS)
for removal efficiencies of 88  and 86 percent, respectively.
Removals were not impaired by intentional hydraulic and BOD
overloading of the oxygenation  system.  During the winter months,
a  fungus in the influent sewage caused the oxygenation system
biomass to become filamentous,  resulting in a deterioration  of
sludge  settling and thickening  characteristics to varying degrees
over the three winters of the testing program.  While operating
difficulties occurred, this condition had no significant effect
on the  plant effluent quality.  Power and oxygen requirements and
sludge  production data are presented, and sludge volumes are com-
pared with those of the Newtown Creek diffused air plant and with
two New York City step aeration plants.

     This  report was  submitted  in  fulfillment of Grant No.
S802714 by the New York City  Environmental Protection Administra-
tion, Department of Water Resources,  under the partial sponsor-
ship of the  U.S. Environmental  Protection Agency.  This report
covers  the operating  period of  May  14,  19/2, to March  11,  1975.
Also contained in this report in Appendix B  is a description and
discussion of  the current proposal  by Union  Carbide Corporation
for conversion of the Newtown Creek  plant to an oxygen system.
                                IV

-------
                         CONTENTS
Foreword	.iii
Abstract	    iv
Figures	,	    vi
Tables	vii
Acknowledgements 	    ix

     1.   Introduction and Scope of Project.  .....     1
     2.   Conclusions and Recommendations	     5
     3.   System Description 	     8
     4.   Analytical  Methods 	    16
     5.   Summary of  Operations	    20
     6.   Equipment and Instrumentation Operating
            Experiences	    47
     7.   Discussion  of Results	    54

References	    66
Appendices

     A.   Detailed Description of Equipment	    67
     B.   Estimated Capital Cost for Conversion
          of the Newtown Creek Plant to Oxygen
          Activated Sludge 	    74

-------
                             FIGURES


Number

  1   Plant Layout 	    2

  2   Plan and Elevation Views of Oxygen Test Bay  ....   11

  3   Perspective Illustration of Oxygenation Equipment   .   12

  4   Photograph of Oxygen Reactor Deck	  .   13

  5   Oxygen System Gas Flow and Control Diagram .....   15

  6   Comparison of Newtown Creek Oxygen System and Air
        Plant BOD Removal Performance	   57

  7   Comparison of Nawtown Creek Oxygen System and Air
        Plant Suspended Solids Removal Performance ....   58

  8   Excess Solids Produced by Newtown Creek Oxygen
        System Superimposed on Batavia, New York Sludge
        Production Graph	   63
                                VI

-------
                             TABLES

                                                            P aft fi
Number                                                      £2iit

  1   Project Chronology 	 •   21,22

  2   Oxygen System Process Performance  .......«•   34

  3   Oxygen System Aeration Tank Performance   	   35

  4   Oxygen System Final Tank Performance and  Sludge
        Settling Characteristics  	   36

  5   Oxygen Supplied to Oxygen System  	   37

  6   Power for Oxygen Generation and Dissolution  	  37

  7   Oxygen System Sludge Production   ...  	  •   38

  8   Oxygen System Nutrient Removals   .  .  	   39

  9   Other Oxygen System Sewage  Characteristics  	   40

  10   Newtown  Creek Air  Plant  Process Performance   ....   41

  11   Newtown  Creek Air  Plant  Aeration  Tank  Performance  .   42

  12   Newtown  Creek Air  Plant  Final Tank  Performance
         and Sludge Settling  Characteristics   	   42

  13   Power Consumption  for  Aeration at Newtown Creek
         Air Plant	>	    43

  14   Newtown  Creek Air  Plant  Sludge Production  	    43

  15   Power Consumption  for  Aeration at Jamaica Step
         Aeration Air  Plant	    44

  16   Power Consumption  for  Aeration at 25th Ward
         Step  Aeration Air Plant	    44

  17    Sludge  Production at  Jamaica Step Aeration Air
         Plant	    45
                                vii

-------
                      TABLES  (continued)
18   Sludge Production at 26th Ward Step Aeration
       Air Plant  ....................   46

19   Comparison of Newtown Creek Wastewater Character-
       istics Before and After Introduction of Manhattan
       Flow ....... ,  .  ..............   74

20   Design Operating Conditions for Full-Scale Newtown
       Creek Oxygen System  .......... . .  ,  . .   78

21   Estimated Capital Cost  for Oxygen System Retrofit
       at Newtown Creek . .  „  ............. ,   79
                              viii

-------
                        ACKNOWLEDGEMENTS


     The authors wish to thank Quentin P. Monahan, Superintendent
of the Newtown Creek plant, Jerome Degen, Senior Chemist in
charge of the Industrial Wastes Control Laboratory at Newtown
Creek, and their capable staffs for their invaluable contribu-
tions to this project.

     Stephen Y. Arella, Assistant Civil Engineer assisted in field
supervision and data reduction; Hank Innerfeld, Principal Engineer-
ing Technician, and Angelika Forndran, Assistant Civil Engineer,
performed some tabulation and reduction of the data.
                                IX

-------
                            SECTION 1

                INTRODUCTION AND SCOPE OF PROJECT

     Plant-scale feasibility studies in 1969 and 1970 at the
O.ll-mVsec (2.5-mgd) activated sludge plant in Batavia, New
York, indicated that significant improvement of the process could
be achieved by the use of pure oxygen instead of diffused air,
and that considerabie capital and operating savings were possible
if oxygen was used in the upgrading of existing plants  (1).  To
the City of New York, this offered a means of upgrading its
Newtown Creek Water Pollution Control Plant, which was designed
to treat 13.6 m^/sec (310 mgd) by modified aeration from a pop-
ulation of 2.5 rr.xllion in the boroughs of Manhattan, Brooklyn,
and Queens.  The plant began operation in September 1967, but
with only the flow from Brooklyn and Queens; delays in the con-
struction of a pumping station prevented the delivery of the
estimated 7,4-m3/sec (170-mgd) Manhattan flow through a force
main under the East River.  During the 34 mo of operation des-
cribed in this report, the flow to the plant, including that to
the oxygen aeration segment, averaged only 7.5 m3/sec (171 mgd).

     The Newtown Creek plant consists of 16 treatment modules
16.8 m (55 ft) wide and 190.5 m (625 ft) long, with flow-through
transverse baffles dividing each tank into ? pair of aerated grit
chambers, an aeration tank, and a settling tank, but with no pri-
mary settling tanks  (Figure 1).  After screening, the raw sewage
is pumped and divides north and south to enter channels leading
to two sets of eight modules.  From this point on, each module
is hydraulically separate from the others, except that the return
sludge from each battery of eight tanks is combined and returned
to the same battery.

     For its first 3 yr of service, the plant was operated at a
sludge age* averaging 0.35 day, but removals were only 37 per-
cent for BOD and 50 percent for SS, considerably below the res-
pective 60 and 70 percent design levels.  In January 1971, the
City, upon the recommendacion of consulting engineers who had pre-
pared a report on the upgrading of some of the plant's facilities,
decided to venture into the usually hazardous sludge age range be-
tween 0.7 day and 3.5 days.  The results were surprising:  by
the use of four of the seven engine-generators and five of the
*Defined as kg mixed liquor suspended solids  (MLSS) in aeration
 tank/kg SS in aeration tank influent/day.

-------
             STREET
                                          STREET
tu
LU
                                    1 SLUDGE '
                                    DIGESTION
       OXYGEN AERATION
            TEST BAY  	
         o   o
         O   O
    po    o
IPO
_A  IF     c i
-^ If     SLUDGE
"   	CONCENTRATION
                                   AERATED GRIT
                                   CHAMBERS
                          AERATION
                          TANKS
                     N
            SECONDARY
            CLARIFIERS
                                                      K
                                                    to
                                                      r
                Figure 1.  Plant layout.

-------
six blowers, by supplying an air to influent wastewater ratio of
9.0 m3/m3 (1.2 ft3/gal),  and by maintaining mixed liquor sus-
pended solids  (MLSS)  concentrations at 1800 mg/,1 (equivalent to a
sludge age of 1.0 day),  efficiencies were greatly increased to
average BOD and S3 removals of 81 and 74 percent, respectively.
However, this could only be viewed as a temporary success; the
inevitable arrival of 7.4 m3/sec (170 mgd) of additional sewage
from Manhattan would double the flow, halve the aeration time,
double  the final tank overflow rate, and make it impossible to
maintain the higher air to influent wastewater ratio and sludge
age.  Some method of improving the plant's efficiency was neces-
sary, and conversion to oxygen aeration offered a potential solu-
tion.  Therefore, in June 1970, the City applied for Federal
support  for a  0.88-m3/sec (20-mgd) test of the UNOX system*.

     The unique layout of the plant was helpful.  One module
could be isolated from the rest of the plant by the installation
of  its  own  influent pumps and its own return sludge pump.  Two
0.88-m3/sec  (20-mgd) pumps were provided, one constant-speed
and one  variable from 0.44 to 0.88 m3/sec  (10 to 20 mgd)  to take
suction from  the grit chamber, along with a 0.66-mJ/sec  (15-mgd)
variable-speed, return sludge pump to recycle settled  sludge  to
the head of  the aeration tank.  Thus, the oxygen activated  sludge
system  -.'ould  be a separate plant within  the Newtown Creek plant.
Provisions  were made for the measurement  of all  important physi-
cal and chemical characteristics by  an elaborate array of instru-
mentation.   Alum storage and feeding equipment* was installed for
a  test  of  phosphorus removal.  The  initially budgeted  cost  of
the project was $2,796,465, of which the  Federal government pro-
vided $1,574,625 and the City  $1,221,840.  Additional  overrun
costs of approximately $900,000 were shared by  the City and
Union Carbide.

      The program was designed  to  answer  these questions:

 1.    Would the use  of  oxygen  enable  Newtown Creek  to  increase its
BOD and SS removals  to  those  of  conventional  activated sludge
within  the existing  tank volume?

 2     Would the plant's  secondary  clarifier design  overflow  rate
 of 35  9 m3/day/m2  (880  gpd/ft2)  be adequate?   (As  a  precaution,
 the adjoining Module 10  was  kept out of  service to be used  for
 additional settling capacity  if  necessary.)


 *A proprietary oxygen  aeration system of the Union Carbide Cor-
  poration.

 *This equipment was never  used because a detergent phosphate ban
  implemented by the State  of  New York reduced influent phospho-
  rus at Newtown Creek to a level consistently below 3 mg/1.

-------
3.   Were the claims of lower sludge production and lower power
requirements for oxygeneration** valid?

4.   Could mixed liquor dissolved oxygen (DO) concentrations of
8-10 mg/1 be obtained without economic penalty?

5.   Could mixed liquor volatile suspended solids (MI/VSS) con-
centrations of 4500 mg/1 or greater be maintained?

6.   Would the activated sludge concentrate to 3 percent total
solids or more in the sedimentation tank and permit low sludge
return rates?
**0xygenation and oxygen aeration are used interchangeably in
  this report.

-------
                            SECTION 2

                 CONCLUSIONS AND RECOMMENDATIONS

     During the nearly 3-yr operating period of this project,
some problems were encountered which have made it difficult to
draw the type of broad conclusions that investigators hope for.
These problems included failure of the single return sludge pump
during two of the three winters, which required shutdowns and re-
starts of the process at low wastewater temperatures; the pre-
sence in the Newtown Creek influent of a fungal organism which
proliferated in both the air and oxygen aeration tanks; lower
removal efficiencies following the two cold-weather startups,
but satisfactory removals during the third uninterrupted winter
despite the continued presence of the fungi; a wide variety of
loading rates; and a number of mechanical, electrical, and in-
strumentation problems.  Therefore, the data have been separated
into several groups with different operating conditions and are
discussed in the light of those conditions.

1.   Over the life of the project, BOD and SS removal efficien-
cies were 88 and 86 percent, respectively.  The effluent aver-
aged- 19 mg/1 for both BOD and SS.

2.   During one phase of the test when the fungi were not present
(hereafter "non-filamentous"), and the flow was at the design
point of 0.88 m3/sec (20 mgd) (uniform rate, not diurnal), efflu-
ent quality averaged 9 mg/1 of BOD and 12 mg/1 of SS, for remov-
als of 94 and 92 percent, respectively.

3.   During two non-filmamentous phases at 0.88-m3/sec (20-mgd)
diurnal flows, effluent quality averaged 21 and 22 mg/1 of BOD
and SS, for removals of 87 and 86 percent, respectively.

4.   During non-filamentous phases at volumetric aerator load-
ings of 4.95 to 5.64 kg BOD/day/m3 (309 to 352 lb/day/1000 ft3)
and overflow rates of 47.3 to 65.6 m3/day/m2  (1160 to 1610 gpd/
ft2), the effluent BOD ranged from 21 to 24 mg/1 and the efflu-
ent SS from 17 to 26 mg/1, representing average removals of 90
and 85 percent, respectively.  These removals were obtained at
BOD loading rates of 123 to 140 percent of design and influent
flows of 128 to 177 percent of design.

5.   Slightly less successful efficiencies were obtained during
three phases, totaling nearly 6 mo, each following a shutdown of
the process and at low sewage temperatures.  Effluent quality

-------
averaged 21 mg/1 of BOD and 22 mg/1 of SS,  for removals of 86 and
84 percent, respectively.  Operation during these three low-temp-
erature process startup periods was characterized by the presence
of the influent fungi which caused varying degrees of difficulty
with sludge settling and wasting and with maintenance of the
desired MLSS concentration.  However, effluent quality was not
significantly affected.

6.   Removals during a fourth low-temperature phase extending
over 3 mo averaged 87 percent for both BOD and SS, with effluent
concentrations of 18 mg/1 of BOD and 13 mg/1 of SS, at the de-
sign diurnal flow of 0.88 m3/sec (20 ragd).  The fungi were pre-
sent in the influent, as they were during the preceding two
winters, but their concentration in the mixed liquor did not
appear to be as great.  Fungi concentrations were determined
numerically during this last period, but were only visually
estimated during other phases.

     This was the only winter operation that was not halted by
a failure of the return sludge pump.  There is reason to believe,
therefore, that the  lower efficiencies and larger volumes of ex-
cess sludge during the first two winter periods were caused by
the combination of startups of the process at low sewage temper-
.tures and the presence of the influent fungi.

7.   Excess solids production on a total suspended solids  (TSS)
basis during non-filamentous periods averaged 0.93 kg/kg BOD re-
moved, and 1.27 kg/kg  BOD  removed during filamentous periods.
For the Newtown Creek  modified aeration plant at comparable
sludge ages, the averages were 1.27  and  1.71 kg TSS/kg BOD re-
moved, 37  and  35 percent greater, respectively.

     Compared  to the 1 available yr  of data  from  the Jamaica
step aeration  plant,  oxygen produced  20  percent  less solids dur-
ing non-filamentous  periods, but 9 percent more  during  filament-
ous periods, at  sludge ages about one-third  of those under  step
aeration.  Compared  to the first 17  mo of operation  of  the  re-
cently-upgraded  26th Ward  step aeration  plant, oxygen  produced
33  percent less  solids during  non-filamentous periods  and  9  per-
cent  less  during filamentous  periods,  at half the  sludge  age.
However,  it must be  noted  that  these plants  were operated  at
significantly  lower  loading rates  and  on much weaker wastewaters
than  the  Newtown Creek plant.

8    During  the  three periods  of above design BOD loading  rates,
when  the  equipment was fully  stressed,  oxygen  system power re-
quirements averaged  0.95 kWh/kg  BOD  removed  (0.58 hp-hr/lb).
For the  single year  at the Jamaica  plant,  the  range  was 1.21 to
1 96  kWh/kg  BOD  removed  (0.74  to 1.19  hp-hr/lb).   In addition,
the first 17 mo  of operation  at the  recently upgraded  26th Ward
step  aeration  plant  produced  a range of  0.71 to  1.05 kWh/kg BOD
removed  (0.43  to 0.64 hp-hr/lb).   Caution should be exercised in

-------
directly comparing these numbers since the wastewater character-
istics and plant loadings were different for these two facilities
relative to Newtown Creek.

9.   At or above the design flow of 20 mgd, oxygen supply averaged
1.0 kg/kg BOD removed.  At flows below design, oxygen supply
ranged from 1.2 to 1.6 kg/kg BOD removed.

10.  The fungal organisms which affected cold weather operation
entered the plant in the influent sewage and concentrated in the
mixed liquor.  The Newtown Creek air plant, in which the organisms
were also present, was less seriously affected during the first
two winters, but more seriously in the third.

11.  Foam  (probably of Nocardia origin) twice developed in the
aeration tank, and once required a halt to the oxygen feed.  Some
means of suppressing or removing foam should be provided.

-------
                             SECTION  3

                        SYSTEM DESCRIPTION

     An oxygen aeration system  is a  high-rate activated  sludge
process which employs oxygen instead of air  for  the biological
removal of organic pollutants from wastewater.   In any system,
the rate of oxygen transfer  is  directly proportional  to  the con-
centration of oxygen in the  aerating gas;  thus,  pure  oxygen
should support a more concentrated biomass by making  more oxygen
available.  Because higher MLSS concentrations imply  higher con-
centrations of microorganisms,  reduced detention times and,
thus, smaller aerator volumes are claimed  to result for  a given
level of organic removal.

DESIGN FOR NEWTOWN CREEK

     Tank No. 9  (Figure 1) was  selected for  the  demonstration be-
cause its location adjacent  to  a wide plant  road allowed room for
the installation of the oxygen  generator,  liquid backup  tank, and
the control building.   The existing  aerator  piping and diffusers
were removed, and three full-width,  reinforced-concrete  baffle
walls and a lightweight, precast-concrete, gas-tight  cover were
installed.  A 0.9-m  (3-ft) gas  space was obtained between the
mixed liquor surface and the cover,  and separate openings in the
walls permitted the flow of mixed liquor and gas from one stage
to the next.  Thus, four co-current  gas and  liquid stages were
created, each 15.2 m long x  16.8 m wide x  5.5 m  high  (50 ft x 55
ft x 18 ft) with a 4.6-m  (15-ft) side water  depth  (SWD)  and a
total liquid volume of  75,700 m5 (1.23 mil gal).  The equipment
was designed for an average  flow of  0.88 m3/sec  (20 mgd) at an
influent strength of 250 mg/1 of BOD.

     A system of reinforced concrete beams and girders was in-
stalled to support the  mixers, and additional columns were in-
stalled in the tank to  transmit the  static and dynamic loads to
the existing foundation.  The cover  was designed to sustain an
internal positive pressure of 15.2 cm (6 in) of  water and an
external negative pressure of 10.2 cm (4 in), and to  support a
live load of 488 kgf/m2  (100 lb/ft2).  The cover was  free to
expand and contract with changes in  temperature.

     The primary oxygen supply for the UNOX  system was a Union
Carbide pressure swing  adsorption (PSA)  air  separation facility
which was designed to produce 473 std m3/hr  (16,700 scfh) of gas
containing 425 std m3/hr (15,000 scfh)  of pure oxygen.  The unit

-------
consisted essentially of an air compressor, aftercooler and at-
tendant cooling tower, adsorption beds and valve skid, and auto-
matic flow controls.  The PSA unit was backed up by a liquid
oxygen storage tank with an electric water bath vaporizer capable
of supplying up to 510 std m3/hr  (18,000 scfh) of pure oxygen.
Flow from the liquid oxygen storage tank was automatically con-
trolled by the pressure in the line, which fell when either the
PSA was not supplying oxygen or when  -.he system called for more
oxygen than the PSA could supply.  Evaporation losses from the
liquid oxygen storage tank were recovered by piping gaseous
oxygen which escaped from the tank into the oxygen feed line.

     Each stage contained two mixer-spargers suspended from the
cover for oxygen dissolution.  A  total of five compressors were
provided at the side of the tank, two for the first stage and
one each for the second, third, and fourth stages, to recirculate
the gas.  The compressed gas was  pumped through the hollow rotat-
ing shafts of the mixers and sparged  into the liquid  from the
bottom of the shafts.  Three-bladed,  1.8-m  (6-ft) diameter,
marine propellers attached to each shaft dispersed the oxygenated
wastewater and kept the solids in suspension.  The mixers were
equipped with automatic controls  for  shutdown if the  oil level
was too low, the vibration too extreme, or the seal air pressure
too low.

     Degritted influent sewage entered Stage  1 of the tank from
the grit chambers, which acted as a well for  the two  112~kw  (150-
hp) influent pumps. A magnetic flow meter monitored the influent
flow, which was recorded and totalized.

     The oxygen feed  to Stage  1 was controlled by the pressure in
the stage gas space;  if the pressure  dropped  below a  pre-set
limit,  an automatic valve opened  further to admit more oxygen.
This flow was monitored by a temperature-compensated  orifice
meter and recorded  and  totalized. The gas  in Stage 1 passed
first through a trap  to remove particulate matter and then into
a  18.4-std m3/hr  (650-scfm) recirculation  compressor.  Two com-
pressors were provided  for Stage  1; either  or both could be  used
if required.  The  recirculation  systems  for the  second and succeed-
ing stages were the same as for  Stage 1, except  that  manual  ad-
justment of  a bypass  valve controlled the  recirculation rate
in these stages.   The gas  leaving the fourth  and  final stage
was analyzed  for oxygen content  and metered,

     In anticipation  of denser  sludge,  the  final  clarifier sludge
collector drive was modified to  increase  its  speed  to 1.65 m/min
 (5.4 ft/min)  [before  the alteration,  two-speed  operation was  pos-
sible,  0.61  m/min  (2.0  ft/min)  and  0.91  m/min (3.0  ft/min)].
Later,  to decrease  wear on the  mechanism,  the speed was  reduced
to 1.34 m/min  (4.4  ft/min), the  minimum possible  after  the modi-
fication.

-------
 A  0,66-m3/sec  (15-mgd),  variable-speed,  return  sludge  pump  and  a
 1.14-m-Vmin  (300-gpm)  waste  sludge  pump  were  provided,  along
 with  magnetic  flow  meters  and  recording  and  totalizing  equip-
 ment.

      Section and  plan  views  of  the  Newtown Creek  oxygen test
 bay,  including both reactor  and  secondary clarifier, are shown
 in Figure  2.   A perspective  illustration of  the oxygenation
 equipment  and  oxygen reactor are presented in Figure 3.   The
 reactor deck and  turbire-sparger drives  are  shown photographic-
 ally  in Figure 4.

 CONTROL SYSTEM
     Sensing devices were  installed  in Stages  1 and  4  to
monitor the concentration  of volatile hydrocarbon gases in  the
reactor gas space.  In the event of  a hydrocarbon entering  the
reactor with the influent  wastewater and reaching a  concentration
in the gas space of 25 percent of the lower explosive  limit  (LEL)
of hexane, an alarm would  sound and  automatically halt the  feed
oxygen flow.  The PSA compressor would then supply purge air at
a rate to completely renew the reactor gas space within 15 min.
If the gas space hydrocarbon concentration continued  to rj.se,
another alarm would sound  at 50 percent LEL and the  recirculation
compressors would be shut  down to eliminate them as  a potential
ignition source.  After any hydrocarbon alarm  situations, the
equipment could be returned to operation only  manually and only
after the hydrocarbon level decreased to below the 25 percent
LEL concentration.

Oxygen Feed

     Oxygen feed flow to the system  was automatically controlled
by the gas pressure in the first stage.  If the organic load in-
creased, the oxygen uptake rate rose, the pressure in the gas
space decreased, and a pressure-regulating device compensated
to allow increased oxygen feed.  If  the PSA could not supply
enough oxyg=>,n to maintain system pressure, liquid oxygen was
automatically vaporized and added.   If the organic loading de-
creased, the oxygen uptake rate would fall and the system pres-
sure would rise, causing suction throttling of the PSA compres-
sor and a reduced flow of oxygen to  the system.

Oxygen Vent

     As the organic loading to the system changed, the fourth
stage vent gas purity changed and adjustments  had to be made
to return the purity to the desired  level.  An increased organic
loading caused the vent gas purity to decrease, and a decreased
loading caused the purity to increase.   Adjustments to the vent

                               10

-------
    PUMPS
RAW	
SEWAGE
RAW 	
SEWAGE
^
FIVE GAS RECIRCULATING
    COMPRESSORS

 D   D     D     D
                                    EIGHT SUBMERGED
                                    PROPELLER MillERS
                            O
            O
                  O
                O
                             200'
                                                     55'
                                                                SECONDARY
                                                                EFFLUENT
                                                   400'
           ( DRIVE
         	1 PROPELLER
ASSEMBLY  I SPARGER
               MIXER
            n
                                  n
                                         PLAN  VIEW
                                          NO SCALE
                      n

'id

kr

<







L

<
cd
1
I

t

»
*.-..!-.» rrf
Bw

n — ~=S. — — O -m -Q ' — "~*

D~ — u~- O — *- Q
— E-
SECONDARY
EFFLUENT
GRIT 1 FOUR-STAGE OXYGEN AERATOR ' 	 y /"^SECONDARY
CHAMBER!



WD = 15

I


^— SLUDGE
RECYCLE






T CLAR1FIER
_ ..] U/nr:19 '


ELEVAT ON 1
NO SCALE !

FT - 0.305 M







I
SLUDGE
WASTING



                 Figure 2.  Plan and  evaluation views of oxygen  test bay.

-------
 SEDIMENTATION
 TANK No. 9
                              AERATION TANK No. 9
                                                                       CHIT
                                                                     CHAMBERS
   PSA OXYGEN
 GENERATION SYSTEM
Figure 3.   Perspective  illustration of oxygenation equipment.

-------
                                                                0
                                                                •p
                                                                C
                                                                fO
                                                                (1)
                                                                c
                                                                OJ
                                                                en
                                                                >i
                                                                x
                                                                0

                                                               4-1
                                                                O
                                                                fO
                                                                J-l
                                                                tn
                                                                O
                                                                4J
                                                                O
                                                                X
                                                               ^

                                                                
-------
gas purity were accomplished by controlling the flow rate through
the vent valve.  If the purity fell below the desired level, the
vent flow was manually increased; if the purity rose above the
desired level, the vent flow was manually decreased.  The entire
oxygen system gas flow and control network is diagrammed in
Figure 5.

Liquid Flows

     The influent sewage flow rate was automatically maintained
at an operator-selected level.  An automatic flow variation pat-
tern could be achieved by the use of a programmer to simulate
the diurnal flow variations of the existing air activated sludge
plant.  The return sludge flow rate could be set at a constant
rate or at a pre-set  fraction of the influent flow, and  the waste
sludge flow rate was  manually controlled using a variable-speed
pump.
                                 14

-------
             REACTOR
             PRESSURE
             CONTROL
                 ^^^
NOTES:

 I HP = 0746 KW
 I PSIG = 703 KGF/M2
        <        I,    i    I
>^=j      JLJ=|     Ju^  JS
'S'"*'1*5'*:*15*5'*^
                 Figure  5.   Oxygen  system gas  flow and control  diagram.

-------
                            SECTION 4

                       ANALYTICAL METHODS

BOD

     Total and filtrate BOD analyses, in two dilutions, were
performed daily on influent and effluent samples.  Samples for
filtrate BOD were filtered through Whatman No. 1 paper.  Begin-
ning in January 1973, dissolved oxygen readings for BOD were
taken with a DO meter and probe (Weston and Stack Model 300
meter with Model 3A probe, and Model 350 meter with Model 33
probe)  instead of the Winkler titration method previously used.
Winkler titrations were used to calibrate the meter daily.  DO
readings by meter saved time and proved to be reliable.

     The procedures outlined in Standard Methods for the Examina-
tion of Water and Wastewater (2) were used, except in the deter-
minations of initial DO levels of the sample dilutions, which
were done according to the practice of the New York City Depart-
ment of Water Resources as described in the following paragraph.

     DO measurements of the dilution water were taken on the day
the dilutions were prepared.  The post-incubation DO levels of
the seed controls (5 and 10 percent seed incubated for 5 days)
were applied to those measurements to calculate the DO of the
dilution water (I percent seed) after 5 days of incubation.  The
final DO levels of the incubated sample dilutions were then sub-
tracted from this calculated blank to obtain the depletions due
to the samples.  An extensive comparison was performed of this
method and the standard method of taking the initial DO reading
of each sample dilution.  BOD values obtained by the two techni-
ques were very close, well within the accuracy of the BOD test.

     Although the final effluent often was supersaturated, handl-
ing, compositing, and shaking dissipated the supersaturation by
the time the BOD analysis was begun.  The dilutions, therefore,
had essentially the same initial DO level as the dilution water,
despite the high percentage of effluent used in the dilutions.

     Laboratory work generally was not performed on weekends;
Saturday and Sunday samples were refrigerated until Monday.
Dilutions which normally would have been removed from the incu-
bator on Saturday and Sunday were removed on Friday and Monday,
and the resulting BOD values adjusted to 5-day values according
to Strester & Phelps (3).  The validity of applying the factors

                                16

-------
was confirmed by experiment.

SOLIDS

     Suspended solids analyses were performed or, daily influent,
effluent, Stage-4 mixed liquor, and return sludge samples.  Glass
fiber filters  (Whatman GF/C with Gooch crucibles, permitted by
Standard Methods  (2) as an alternate) were initially used for all
samples.  Mixed liquor and return sludge samples were diluted
prior to withdrawing an aliquot for filtration.

     Starting  in May 1973, Buchner funnels were used instead of
Gooch crucibles for mixed liquor and return sludge samples because
their larger filtration area permitted larger aliquots to be
filtered v;ithout dilution.  Some ceramic mateial was cut from the
funnel-:  to keep their weight within the capacity of the analytical
balance.  Volatile  suspended solids were determined after ignition
at  550 C.

     Total solids and total volatile solids determinations were
performed in accordance with Standard Methods  (2).  Suspended
solids and volatile suspended  solids values were substracted from
these to obtain dissolved solids and volatile dissolved solids
values.  Dissolved  solids analyses were performed twice a week on
influent and effluent samples, but were discontinued in June 1973,

SETTLING DATA

     Two 1000-ml  graduated  cylinders, one  equipped with a 1-rpm
mechanical stirrer, were  filled with well-dispersed, fresh,
Stage-4  mixed  liquor.  Readings of the volume of  settled  sludge
were  taken after  1,2,3,5,7,10,15,20,25, and  30 min.

     The settling rate in ml/min was determined  for each  time
increment, and the  highest  of  these  rates  was  taken as  the  initial
settling rate  (ISR) and reported as  m/hr  (ft/hr).

     The 30-min settled volume was used to calculate  the  sludge
volume  index  (SVI)  and sludge  density  index  (SDI) as  specified  in
Standard Methods  (2).

pH  AND ALKALINITY

      pH  analyses  were performed  on daily  influent and  effluent
samples  and,  starting  in  March 1973,  on Stage-4  mixed  liquor
settling test samples, using  a Hach  Model 2075  pH meter with  a
combination  electrode.  Alkalinity determinations were performed
twice  a  week  on influent  and  effluent samples  by potentiometric
titration  to  pH 4.5.

      Turbidity determinations  were made  twice  a week  on the
supernatant  liquor  from  settled influent  and effluent samples

                                17

-------
using a Hach Model 2100 turbidimeter,   Doth samples required 15
min of settling to remove large particles which caused erratic
meter readings.  Commercial Jackson Turbidity Unit (JTU)  stand-
ards were used for calibration.  These analyses were discontinued
in July 1973.

COD

     COD analyses were performed on daily influent, effluent,
effluent filtrate (Whatman No. 1 paper), and return sludge
samples.  Mercuric sulfate was added to the digestion flask to
inhibit the interfering effect of chlorides.  Fifty-mi samples
or aliquots diluted to 50 ml were used.  Influent and return
sludge samples were digested in the presence of a strong dichro-
mate solution  (0.25N); a weaker solution (0.025N) was used for
the effluent samples.  Refluxing for 1% hours was found to be
sufficient for complete digestion.

NUTRIENTS

     Total Kjeldahl nitrogen (TKN),  ammonia nitrogen, total
phosphate, and soluble orthophosphate analyses were performed
on influent and effluent samples, but not every day.  The
analyses were alternated so that total Kjeldahl and ammonia
nitrogen analyses were run daily one week,  and total and soluble
orthophosphate analyses were performed daily the following week.
The samples were preserved with 40 mg/1 of  mercuric chloride and
refrigerated until analysis.  Nitrate and nitrite nitrogen analy-
ses were performed on fresh influent and effluent samples twice
a month until March 1973, after which they were done only once
a month.

     All nutrient analyses were performed with a Technicon Auto-
analyzer system.  An Autoanalyzer I was used until November 1973,
and the Autoanalyzer II system thereafter.

     Ammonia nitrogen analyses were performed according to the
automated method in Methods for Chemical Analysis of Water and
Wastes (MCAWW)  (4).   Samples were not distilled prior to analy-
sis .

     Samples for total Kjeldahl nitrogen analysis were digested
and distilled according to Standard Methods (2), except that
0.02N sulfuric acid was user" for collection instead of boric
acid.  Following distillation, the arr-nonia nitrogen analysis,
described above, was performed.

     Total phosphate and soluble orthophosphate analyses were
performed by the automated stannous chloride method until
November 1973, when it was replaced by the automated single re-
agent method  (ascorbic acid method).  Both methods are described
in MCAWW (4).

                               18

-------
     The automated hydrazine reduction method in MCAWW (4) was
used for nitrate and nitrite nitrogen analyses.

TOG

     Beginning in October 1972, total organic carbon analyses
were performed on daily influent and effluent samples with a
Beckman Model 915 TOG analyzer using the procedure recommended
by the manufacturer.  The samples were preserved by adding mer-
curic chloride to a concentration of 40 mg/1 and then refrigera-
ted.  Before analysis, they wore acidified and purged with nitro-
gen to remove inorganic carbon and then homogenized in a blender
for 5 min for greater uniformity and reproducibility.
                               19

-------
                             SECTION 5

                       SUMMARY OP OPERATIONS

      The  Newtown  Creek oxygen system was  placed  in  operation  May
 14,  1972.   The  testing program was  concluded  on  March  11,  1975.
 In  the  intervening  34  mo,  a  broad range of operating conditions
 comprising  a  total  of  12 evaluation phases was imposed on  the
 system.   Throughout, an extensive array of data  were collected
 daily.

      The  chronology of events is summarized in Table 1.  Each
 operating phase,  shutdown, and restart is discussed individually
 below.  Operating and  performance data generated on the  oxygen
 aeration  system for Phases 1-12 are presented in phase-average
 form in Tables  2-9  at  the  end of this section.   For comparative
 purposes, operating and performance data  developed  for the  same
 period of time  for  the Newtown Creek conventional air  aeration
 plant are also  recorded at the end  of this section  in  Tables  10-
 14,  along with  power consumption and sludge production data for
 two  City  step aeration air plants (Jamaica and 26th Ward)  in
 Tables 15-18.

 STARTUP  (MAY  14-SEPTEMBER  16,  1972)

     The  intent was to break  in the process while collecting  data
 at a flow of  0.44 mj/sec (10  mgd) for 1 to 2  mo,  and then  at  0.66
 m-Vsec  (15 mgd) and possibly  one other intermediate point  before
 reaching  the design flow of  0.88 m3/sec (20 mgd)  in late summer
 1972.  The summer,  however, was characterized by many  equipment
 and  instrumentation problems;  these are discussed in Section  6
 of this report.   In mid-September 1972, with  the flow  at 0.88
 mj/sec  (20 mgd),  it was found  that  most of the data already col-
 lected to that point were unusable;   large errors were  discovered
 in the metered influent sewage  flow, return sludge  flow, and
 oxygen feed flow.    The  data collected through mid-September 1972
 are, therefore, not presented.

 PHASE 1 (SEPTEMBER  17-NOVEMBER  25,  1972)

     With the flow at  0.88 m3/sec (20 mgd) and the  instrumenta-
 tion considered reliable, Phase  1 was begun.  Waste sludge  data,
however, are not presented until  Phase 3,  after  the defective
magnetic flow meter was replaced  (see Section 6).   The flow was
kept at a constant 0.88 m3/sec  (20  mgd)  until the last week,  when
a diurnal variation based on the  air plant influent pattern and

                                20

-------
                 TABLE  1.   PROJECT CHRONOLOGY
Dates Phase
5/14-9/16/72
9/17-11/25/72 1
11/26-12/9/72
12/10/72-
2/1/73 2

2/2-2/24/73
2/25-4/5/73 3
4/6-5/31/73 4
6/1-6/30/73 5
7/1-7/7/73

7/8-8/11/73 6
8/12-9/1/73 7
9/2-9/15/73
No. of
Days
126
70
14
54

23
40
56
30
7

35
21
14
Influent
Flow Rate
(mgd) * Remarks
11-20 Startup; faulty
meters
20.8 Warm weather; design
flow Cconstant)
Shutdown for return
sludge pump repair
17.7 Restart; winter oper-
ation; variable flows
(constant) ; fungus
Shutdown for tank
cleaning; restart
15.1 Winter operation;
75% design flow (con-
stant) ; fungus
20.3 Warm weather; design
flow (diurnal)
25.6 Overload; diurnal
flow
Flow increased; pro-
cess unstable; PSA
difficulties
30.0. Overload; diurnal
flow
35.4 Overload; diurnal
flow
Flow reduction due
9/16-10/8/73
                                             to PSA compressor
                                             motor bearing fail-
                                             ure; process recov-
                                             ery
23
10.1
     Underload;  diurnal
     flow
(conti/nued  on next page)
                               21

-------
                      _TABLE 1.   (continued)
    Dates
Phase
 10/9-10/13/73




 10/14-10/25/73    9


 10/26/73-2/5/74




 2/6-4/30/74      10



 5/1-8/5/74       11




 8/6-8/25/74


 8/26-12/12/74
12/13/74-
  3/11/75       12
No. of
 Days
            12


           103




            84



            97




            20


           109




            89
 Influent
Plow Rate
  (mgd)*
                                                     Remarks
                    Flow reduction due to
                    sludge collector re-
                    pair;  process recov-
                    ery.

            14.6    Foam problem; under-
                    load;  diurnal flow

                    Shutdown for foam
                    problem and return
                    sludge pump repair;
                    restart

            19.7    Winter operation;
                    design flow (diurn-
                    al) ;  fungus

            19.1    Spring & summer  oper-
                    ation;  design flow
                    (diurnal);  recover
                    from fungus

                    Flow changed pre-
                    vious  to shutdown

                    Shutdown for PSA
                    rehabilitation;  re-
                    start
           20.1    Winter operation;
                   design flow  (diurn-
                   al) ; fungus
*1 mgd = 0.044 m3/sec = 3785 m3/day
                               22

-------
                           3
ranging from 0.61 to 1.05 m /sec  (14 to 24 mgd) was introduced.
The flow for the period averaged  0.91 m3/sec (20.8 mgd).  The
aerator detention time, including return sludge flow/ was 1.1 hr;
the volumetric organic loading v/as 2.61 kg BOD/day/m-J (163 lb/
day/1000 ft3);  and the food-to-microorganism (P/M) loading was
0.63 kg BOD/day/kg MLVSS (see Table 3).  The MLSS concentration
was 4860 mg/1,  and the SDI averaged 2.2 g/100 ml.  The final tank
detention time (Table 4)  was 2.3 hr and, at an average return
sludge flow of 30 percent, the return sludge concentration was
16,200 mg/1.  The overflow rate was 39 m3/day/m2  (950 gpd/ft2),
and the solids loading 244 kg/day/m^ (50 Ib/day/ft^).  Process
performance  (Table 2) was excellent:  94 percent  total BOD
removal, 95 percent filtrate BOD, 83 percent COD, 92 percent
suspended solids, and 77 percent TOG.

SHUTDOWN (NOVEMBER 26-DECEMBER 9, IJ72)

     During the week of November 9, 1972, it became apparent that
the return sludge pump would have to be taken out of service for
replacement of its bearings.  Since the repairs were expected to
take only 2 to 3 days, the aeration tank was not  drained; raw
sewage addition was halted on November 26, but some oxygen feed
was maintained, about 3.2 metric  tons/day (3.5 tons/day).  The
job, however, required 10 days to complete because the bearings
in stock proved to be the wrong size and it took  the manufac-
turer a week to locate and deliver the proper bearings.   The re-
sult was that Phase 2 began with the handicap of  anaerobic return
sludge.

PHASE 2 (DECEMBER 10, 1972-FEBRUARY 1, 1973)

     The influent flow was resumed on December 6, 1972,  initially
at 0.22 m^/sec (5 mgd) and increasing to the design 0.88 m^/sec
(20 mgd) by December 19.   Performance during this period was not
as good as it had been before the shutdown.   Total and filtrate
BOD and SS removals fell to 83-87 percent and COD removal to 76
percent.  Sludge compaction also deteriorated with the SDI aver-
aging 1.8 g/100 ml compared to 2.2 before the shutdown

     In January 1973, a microscopic examination told the story:
filamentous organisms had become established in the system.  An
attempt was made to stabilize the process by reducing the influ-
ent flow, but the filamentous forms persisted.  It was,  there-
fore, decided to shut down the process, empty the tanks, and then
start up again and establish a new culture.

SHUTDOWN (FEBRUARY 2-24,  1973)

     Advantage was taken of this otherwise unhappy event to in-
spect the interior of the aerator.  No noticeable corrorsion and
only an insignificant accumulation of grit was found.  No rags
were wrapped around the mixer blades and shafts;  this was an un-

                               23

-------
  expectedly happy development because Newtown Creek has  a heavy
  *nrt  inar',       ?fPa^S  and minor Codifications  also  were made,
                                                               of
PHASE 3 (FEBRUARY 25-APRIL 5, 1973)

     The purpose of this phase was to continue the collection of

                                /SSC (2° mgd)  Which was be» in
   ae2bn              1;                      c  was  e^»
 Phase 2, but with diurnal  flow variations.  The defective waste
 sludge magnetic flow meter had been replaced on March 2  1973
 and so the data would be complete for the first time.  The inten-
 tion was to maintain a sludge age of 3.5 days and slowly move
 from an initial 0.22-m3/sec  (5-mgd) flow to 0.88 m3/sec  (Tmqd)

 favoTa hea?^d h^ &t ^ highe? Sludge ^ ' competition wSu?d
 favor a healthy biomass over any intruding forms.  However, al-
 ?Sf F   I" ^tavtuP' filamentous organisms became apparent and, by
 the first days of March, with the flow at 0.53 m3/sec (12 mad)
 operation had become impaired .  The f il nmentous f orSs ,  which were

 Preval'ent'th^  f  1S^aS,a fUn
-------
 PHASE 4  (APRIL 6-MAY 31, 1973)
 n *i Jfi<:? ^S ^°W at the desi9n Point, a diurnal variation from
 0.61 to 1.05 m-Vsec (14 to 24 mgd) and averaging 0.88 mVsec  (20
 mgd) was instituted on April 6, 1973, and Phase 4 was under way
 For the next 3 wk, with the fungus still present and the sludge
 age dropping even farther to 1.3-1.4 days, treatment efficiency
 remained good.  Total BOD, filtrate BOD, and SS removals hovered
 around 90 percent, and COD removal was in the 75-80 percent
 range.  By the end of April, as the sewage temperature topped
 60 F indicating the end of the winter temperatures, the fungus
 in the sludge diminished and finally, in early May, disappeared.

      But some questions remained.   If the shutdown had not occur-
 red and required a winter restart, would the healthy culture have
 prevented the intrusion of filamentous forms?  If the fungus was
 indeed a cold weather occurrence that would have to be tolerated
 could the design flow be treated throughout the winter?  To answer
 these questions, another full winter of operation would be requir-
 ed.   With the mutual concurrence of the City and EPA, the proiect
 was, therefore,  extended to the end of April 1974.

 PHASE 5 (JUNE 1-30,  1973)

      One of  the  program's  objectives was to stress  the process to
 performance  breakdown.   Therefore,  since the plant  was perform-
 ing  well at  0.88 m3/sec  (20  mgd),  influent flow was  increased  on
 June 1,  1973,  to 1.10  m3/sec (25 mgd)  with diurnal  variations
 from 0.74  to 1.31 m3/sec (17 to 30  mgd).   The increased flow de-
 creased the  aerator  detention  time,  including return sludge flow,
 to only 0.81 hr.   A  sharp  increase  in BOD  strength  to 240 mg/1
 more than  doubled the  volumetric organic loading to  4 95  kq
 BOD/day/m-^  (309  lb/day/1000  ft3) and  also  doubled  the F/M loadina
 to 1.38  kg BOD/day/kg  MLVSS.   The  final  tank  detention  time drop-
 ped  to  1.85  hr,  and  the  final  tank  solids  loading and overflow
 rate  increased to 308  kg/day/m2  (63  Ib/day/ft2)  and  47  m3/day/m2
 (1160 gpd/ft^) ,  respectively.   Process efficiencies  for  this phase
 were  very respectable:   90 percent  total BOD  removal,  89  percent
 filtrate BOD removal,  and  77 percent  COD removal.   SS  removal,
 however, fell appreciably  to 26  mg/1  and 83 percent  removal   TOC
 removal was  68 percent,  about  the average  of  Phases  1-4.

 PROCESS STABILIZATION  (JULY  1-JULY  7,  1973)

     Flow was increased; process disruption was  caused by  PSA
 problems, and efforts were made  to stabilize  conditions.

PHASE 6  (JULY 8-AUGUST 11, 1973)

     Encouraged by the results at 1.10 m3/sec  (25 mgd), influent
                               25

-------
 flow was  increased  to  1.31 m3/sec  (30 mgd) with  a  diurnal  varia-
 tion from 0.92  to 1.58 m3/sec  (21  to  36 mgd).  Aerator  detention
 time,  including  return, decreased  to  0.74  hr;  the  volumetric  or-
 ganic  loading increased to 519 kg  BOD/day/m3  (324  lb/day/1000
 ft3);  and the F/M loading increased to  1.53 kg BOD/day/kg  MLVSS.
 The final tank  detention time decreased to 1.6 hr, and  the over-
 flow rate rose  to 55 m3/day/m2  (1360  gpd/ft2).   Removals were 90
 percent for total BOD, 88 percent  for filtrate BODf  86  percent
 for SS, and 71  percent for TOG.

 PHASE  7 (AUGUST  12-SEPTEMBER 1,  1973)

     After 5 wk  and no process deterioration at  1.31 m3/sec  (30
 mgd),  influent  flow was increased  to  1.53  m3/sec  (35 mgd)  on
 August 12, 1973, but with a modified diurnal pattern.   Since  the
 peak flow of 1.84 m3/sec (42 mgd)  that would have  been  required
 exceeded  the combined capacities of both influent  pumps, the
 diurnal variation was altered somewhat to  obtain the average
 flow of 1.53 m3/sec  (35 mgd) by means of a sustained peak  flow of
 1.62 m3/  sec (37 mgd), which was the combined capacity  of  the two
 pumps, and a minimum flow of 1.05  m3/sec (24 mgd).  This latest
 flow increase represented the greatest stress that could be ap-
 plied  to  the system.  If the biological process could not  be
 broken at this  flow, the maximum tolerable loading would remain
 unknown.

     Things went very well until September 1 when  a bearing on
 the PSA compressor failed, shutting down the oxygen generator.
 Therefore, this phase, which was intended  to last  for a month,
 had to be cut short.  Nevertheless, the 3  wk of operation  proved
 very successful.  At an average flow of 1.55 m3/Sec  (35.4  mgd),
 effluent  total BOD and SS concentrations were only 21 and  17
 mg/1, respectively, for removal efficiencies of 89 and  87  per-
 cent.  COD and TOG removals increased to 80 and 75 percent, res-
 pectively.  Filtrate BOD removal fell to 83 percent, but the
 influent  strength was 15 percent lower too.  These results were
 obtained  at an aerator detention time, including return sludge
 flov/, of  only 0.67 hr; a volumetric organic loading rate of
 5.64 kg BOD/day/m3  (352 lb/day/1000 ft3);  and an F/M loading  of
 2.22 kg BOD/day/kg MLVSS.  Settling tank detention time was 1.3
 hr, and the overflow rate averaged 66 m3/day/m2  (1610 gpd/ft2).

 PROCESS RECOVERY (SEPTEMBER 2-15,  1973)

     The  bearing failure which shut down the PSA on September  1,
 1973, reduced the total oxygen supply capacity to  the 16.3 metric
 tons/day  (18 tons/day) of the Driox vaporizer.  Then on September
 3, the motor operating the automatic liquid oxygen feed valve
burned out, preventing automatic control of oxygen feed to main-
tain a predetermined gas space pressure.   The reduced oxygen
supply capacity and the crude manual control on the liquid oxygen
 feed required a cutback in influent flow from 1.53 to 0.53 m3/sec

                               26

-------
 (35 to 12 mgd).   A return to 1.53 m3/sec (35 mgd)  was not immin-
 ent,  and so on September 7, a diurnal pattern designed to yield
 an average flow of 0.44 rn3/sec (10 mgd)  was implemented in pre-
 paration for Phase 8,   On September 10,  the PSA was returned to
 service once again allowing automatic control of oxygen feed.

 PHASE 8 (SEPTEMBER 16-OCTOBER 8,  1973)

      By September 16,  1973, the procass  had reached equilibrium
 after the precipitous  flow reduction from 1,53 m3/sec (35 mgd)
 to 0053 m3/Sec (12 mgd)  and then  to 0.44 m3/sec (10 mgd)  and
 Phase 8 was begun.

      Since the data collected during the first summer of  opera-
 tion  could not be used because of inaccurate instrumentation,
 this  phase was  an attempt to backtrack  to collect  data to fill
 the void at low-flow loadings.  At an average flow of 0.44 rn3/
 sec (10.1 mgd),  with diurnal variations  from 0.31  to 0.53 m3/Sc-c
 (7 to 12 mgd),  the aerator detention time,  including return,
 averaged 2.4 hr;  the volumetric organic  loading was 1.44  kg BOD/
 day/m3 (90 lb/day/1000 ft3);  and  the F/M loading was 0.39 kg BOD/
 day/kg MLVSS.   The final tank detention  time was 4.7 hr.   The
 final tank overflow rate and solids loading were only 19  m3/day/
 m2 (460 gpd/ft2)  and 112 kg/day/m2 (23 Ib/day/ft2),  respectively.
 At these low loadings  and at the  high sewage temperature  of 72
 F,  removals were  89 percent of  total BOD,  87 percent of SS,  92
 percent of filtrate BOD,  82 percent of COD,  and 77 percent of
 TOG.

      An out~of-line slude-collector snaft  threatened to cause
 serious damage  to the  equipment.   Repa.Lrs were begun on October
 9.  The process  suffered somewhat  during the 24 hr required for
 the repairs,  and  the flow had  to  be reduced.   It was not  until
 October 14  that  the flow was  up to 0.66  m3/sec (15 mgd) and the
 next  phase  could  begin.

 PHASE  9  (OCTOBER  14-25,  1973)

      Biological  frothing  developed in the aerator  before  the
 phase  was wel] established  and  required  its  early  termination.
 The data, while representing only  12  days of  operation, never-
 theless  are  presented  as  a  phase because  they  represent the  last
 period  of operation at low  flow and  loadings.

      Some of the  data  obtained  during this period  must  be  viewed
with extreme caution because of the  inordinately high MLSS  con-
centrations observed (average 9040  mg/1).  The  samples  undoubt-
edly were contaminated by the aerator froth.   The  aerator  deten-
tion time  (sewage  flow plus recycle  sludge flow) was  1.6  hr  and
the volumetric organic loading  1.75  kg BOD/day/m3  (109  lb/day/
1000 ft3).  -The final  tank detention time was  3.2  hr, and  the
overflow rate was  27 m3/day/m2  (660  gpd/ft2).   Removals averaged

                                27

-------
91 percent of total and filtrate BOD, 07 percent of SS, 82 per-
cent of COD, and 31 percent of TOC.

SHUTDOWN  (OCTOBER 26, 1973-JANUARY 1, 1974)

     By October 26, 1973, the foam had become so pronounced that,
in order  to protect the stage blowers, the oxygen feed to the
system was halted and air feed via the stage compressors was in-
stituted.  However, beginning on October 27, frequent stage com-
pressor shutdowns indicated that they had indeed been affected.
It was then necessary to dismantle and clean all the compressors
and their related oxygen piping.  While this was being done, the
influent  flow was reduced to  0.44 m3/sec  (10 mgd) and the air
feed was  continued in an effort to sustain the process until the
cleaning  operation was completed.

     The  foam which plagued the operation was light brown and
frothy,  similar to the "head" on a chocolate milkshake.   Its
appearance  was markedly different  from  the white foam which
results  from aeration of a wastewater containing detergents, a
common  sight at many treatment plants.  Bench-scale dosage of
the foam with a commercial defearning agent was  not effective.
A similar foaming  condition at  the Jamaica  step  aeration  plant
a year  earlier  resulted  from  an infestation or  Nocardia,  and an
EPA specialist  (6) confirmed  the presence of these organisms in
the UNOX mixed  liquor.   The foam appeared only  in  the  oxygen bay
and never was evident  in the  parallel air modules.  A  means of
removing the foam  was  not  provided in this  installation,  but
some mechanism  for removal  appears desirable.

     By November  12,  the foam had  subsided,  and so, with  the
compressors and their  piping  cleaned, oxygen  feed  was  resumed
The  flow was increased gradually  from 0.44  m3/sec  (10  mgd)  until
 it reached 0.88 m3/sec (20 mgd)  c  > November 25.  Throughout the
episode, filamentous organisms we. e  present,  although  not as
predominant forms.

      Early in December,  further problems with  the  return sludge
 pump bearings became apparent and on the llth  the  pump was taken
 out of service again.   To  prevent a  repetition of  the conse-
 auences of the first shutdown, the tanks were drained and the set-
 tling tank cleaned.   Repairs to the  pump included replacing the
 upper and lower pump bearings, building up the impeller wearing
 ring to  reduce excessive clearance,  and replacing the worn shaft
 packing  sleeve.  Some preventive maintenance also was performed
 on the sludge collection mechanism,  and a piping modification
 was made to the sludge wasting system.   An inspection of the
 tank interior revealed no grit buildup, no rag accumulation
 around the mixers, and no apparent  concrete deterioration.
                                 28

-------
RESTART (JANUARY 2-FEBRUARY 5, 1974)

     On January 2, 1974, after all repairs were completed, opera-
tion was resumed.  By the 17th, the fungus had reappeared.
Nevertheless, the flow was very gradually increased and by Feb-
ruary 6 the process had stablized at 0.88-m3/sec  (20 mgd) diurnal
flow.

PHASE 10 (FEBRUARY 6-APRIL 30, 1974)

     The intention was to operate during what was left of the
1973-1974 winter at 0.88 m3/sec  (20 mgd) and to combat the fungus
by any means except reducing  the flow.  From the  beginning, the
phase was characterized by severe fungal proliferation; in fact,
the dominant microorganism in  the mixed liquor was the fungus,
often to the complete exclusion of  the microbial  forms.  The
fungus, with its long-branching mycelia, interfered with the
settling and compaction of the sludge.  Consequently, as during
the previous winter, the sludge blanket extended  the entire
length of the clarifier and the wasting rate frequently had to
be increased to control it.   The poor compaction  resulted in  an
average return sludge concentration of only 5220  mg/1 for the
phase and a  low  for 1 wk of less than 4000 mg/1.

     These were  in contrast to averages of more than 16,000 rng/1
for  summer operation and were  less  than half of those obtained
during the previous winter.   The weak return sludge concentra-
tions depressed  the MLSS concentration, which  averaged only
2400 mg/1 for the phase and experienced a weekly  low of  less
than 1700 mg/1.  From mid-February  to mid-April,  the sludge age
averaged only 1.0 day,  considerably less  than  the 1.3-2.0-day
range experienced the previous winter.  The SDI slipped  to  a  low
of 0.4 g/100 ml  during  the week  of  February 10  and  0.6 during the
next'2 wk compared to a weekly low  of  1.0 during  the previous
winter and averages of  over 2.0  during  summer  operations  and  well
over 1.0 the previous winter.  Although it  appeared desirable to
increase the sludge age  to  the level  of the previous winter,  the
low  MLSS concentration  dictated  by  the  filaments  and  the  self-
imposed constraint of maintaining  the  influent rate made  that
impossible.

     The fungus  was not unique to  the  UNOX  system.   During  this
phase  and also  in Phase 3,  the organisms  were  present  in the
air  plant, too;  however,  visual  observation indicated  that  their
numbers were fewer and  their  effects  far  less  severe.   The  aver-
age  SDI of  1.4  g/100  ml for the  air plant during  this  period  was
only slightly  less than the average of  1.7  for the preceding  sum-
mer.   At a sludge age of 1.3  days,  the  air  plant  MLSS  concentra-
tion averaged  1700 mg/1 and the  return  sludge concentration 8800
mg/1 (Tables 11 and  12).
                                 29

-------
     Microscopic examination of the plant influent revealed that
the fungus was entering in the raw sewage.  It may have origin-
ated in the discharge of some connected industry, or conditions
in the interceptor system may have promoted its development.
Once in the plant, if conditions were favorable, retention and
concentration could have caused it to proliferate.  It was ob-
vious that further work would have to be done.

PHASE 11  (MAY 1-AUGUST 5, 1974)

     Although the EPA grant-funded program ended on April 30,
1974, operations and data collection were continued.  Phases
11 and 12, therefore, although not parts of the grant program,
are included in this report to present the most recent findings.

     This phase was a continuation of Phase 10 into warm weather
at 0.88-m^/sec (20 mgd) diurnal flow.  Although the fungi dis-
appeared as the wastewater temperature rose to 60 F and above,
a healthy biomass did not reappear as in the previous summer and
removal efficiencies averaged only 84 percent for total BOD and
82 percent for SC.

     The PSA was taken out of service on June 17 for replacement
of a failed compressor motor bearing, and the biological process
was entirely dependent on the liquid oxygen backup system until
August 1.

FLOW REDUCTION (AUGUST 6-AUGUST 25, 1974)

     Flow was gradually reduced preparatory to the approaching
shutdown.

SHUTDOWN  (AUGUST 26-OCTOBER 31, 1974)

     This 9 wk shutdown was a planned operation, primarily to
upgrade the performance of the PSA.  Due to a malfunction of
certain of the PSA switching valves early in the test, two of
the four adsorption beds became contaminated by moisture, re-
ducing the output of the unit to 9.1 metric torn; of oxygen/day
(10 tons/day).  Union Carbide could have rehabilitated the beds
at any time, but instead elected to supply liquid oxygen at its
own cost up to the PSA design rate of 13.6 metric tons oxygen/
day (15 tons/day).

     The upgrading consisted of replacing the adsorbent material
in the two beds and portions of the material in the other two,
replacing all valves and rebuilding all valve activators, and
increasing the capacity of the PSA compressor and some piping.
The result of the refurbishing was that although an output of
13.6 metric tons oxygen/day (15 tons/day) was guaranteed, the
unit in fact thereafter delivered 15.2 metric tons oxygen/day
(16.7 tons/day)  with virtually no downtime.

                               30

-------
     In addition to the work on the PSA,  inspection and preven-
tive maintenance were provided for all other oxygen system
equipment during this shutdown period.

RESTART (NOVEMBER 1-DECEMBER 12, 1974)

     Because of the unanswered questions relating to the fungal
proliferation during winter operations, the City and Union
Carbide embarked upon an extensive investigation which lasted
throughout the 1974-1975 winter.  The aims of the program were
to identify the fungus, determine whether it was peculiar to
Newtown Creek or was ubiquitous in New York City wastewater,
and find some means of eliminating it.  To accomplish these ob-
jectives, Union Carbide provided a 1.89 I/sec (30-gprn) oxygen
pilot plant on which to test the effects of possible fungicides
before they were applied to the 0.88-m3/sec (20-mgd) system and
a consultant was engaged to identify the fungus and recommend
steps for its control.  A second Union Carbide oxygen pilot plant
was stationed at the Wards Island step aeration air plant to
compare air and oxygen performances in cold weather at that
location.

     The Newtown Creek oxygen module was restarted at 0.22~ro^/
sec  (5-mgd) constant flow.  Influent flow increased to 0.88-
mVsec  (20-mgd) diurnal by December 12, 1974.

PHASE 12  (DECEMBER  13, 1974-MARCH 11,  1975)

     The fungi persisted throughout this period, but their ef-
fect on the process was insignificant.  Nevertheless, the fungus
control program was begun.  It was soon found that, although
several species of  fungi were present  in the mixed  liquor of
both the air and oxygen systems, the predominant form was the
arthrospore producer "Geotrichum"  (10).

     Sampling of the influents at three other New York City
plants and one drainage area not yet  served by a plant revealed
the presence of the same organism  in concentrations generally
similar to those at Newtown Creek.  At Newtown Creek,  the fungus
concentration increased moderately in  the air plant mixed liquor
but significantly  in the mixed  liquors of both the  full-scale
and pilot oxygen systems.   At  the  three other plants  sampled,
the fungi did not  significantly proliferate in the  mixed  liquor.
The growth in the  V7ards Island oxygen  plant was  about  the same
as in  the full-scale air piant.  Apparently, Newtown  Creek's
waste  is unique in that it  is  conducive to  the growth  of  these
organisms.

     The pilot  plant employed  at Newtown Creek was  a  Union  Car-
bide four-stage oxygen system  equipped with turbine/spargers  for
oxygen dissolution and an external circular clarifier.  The
pilot  plant treated an average  of  1.1  I/sec  (17.5  gpm)  on a

                                31

-------
diurnally-varying pattern approximating those of the field oxy-
gen module and f {Ill-scale air plant.  The f irst .^tempt at com-
batting the fungus was to operate at a high sludge retention
time (SRT), but this was not successful.  An SRI of 4.3 days
maTnt lined 'for 2 wk did not diminish the fungi but al BO did not
harm the process, whose effluent averaged 11 mg/1 of total BOD
and 13 mg/1 of S3.

     Since the phosphorus content of the waste during Phase 10
was onlv 2 4 mg/1, the lowest up to that time,  it was considered
possible that nutrient deficiency might have slowed the growth
of Se normal biomass population and permitted  the fungus to be-
                                                   duin  which
of   e norma    o
come predominant.  Therefore, after a short P«iod during which
the 4 3-day  SRT was reduced to a normal level, 2-3 mg/l ot
phosphoruswas aOded to the pilot plant influent.  However,
2 wk of phosphorus supplementation had no effect   The ef-
fluent during this period averaged 17 mg/1 of total BOD and
15 mg/1 of SS.

     Two wk of chlorine addition followed at a dosage of 9 mg/1.
Not only did this have no effect on the fungus, but it ^jured
the process, whose effluent deteriorated to 29 mg/1 of total
BOD and 32 mg/1  of SS.

     A third additive, hydrogen peroxide, was  assessed using  jar
tests but  failed to  improve  sludge settling even  at dosages up
to  200 mg/1.

     The  final attempt at control was  adjustment  of the  PH of the
mixed liquor, although it was  expected to be very costly on a
full -plant scale.  More  than 2 yr of data indicated that the  pH
of  the  influent, which ranged  from 6 . 3 to 6 . 9 , was depressed  by
about 0.4  unit during passage  through  the oxygenation aerator
£  was  considered possible  that  this  drop could  have  sparked  the
 growth  of the  fungus.  However,  10 days of  lime  addition at  100
mg/T increased  the pH of the mixed  liquor  to 7.0 but  had no  ef-
 fect on the fungi.

      The 1974-1975 winter operation  in the  0.88-m3/sec  (20-mgd)
 oxygen  system during Phase  12 differed from the  past  winters  in
 ?wo respects.   Firs?, it was not interrupted by  a breakdown of
 the return sludge pump,  nor for any  other reason.  Second, al-
 though  the fungus was present from beginning to end  its concen-
 tration in the mixed liquor appeared to be less than those of
 the first two winters.   Effluent quality averaged 18 mg/1 of
 total BOD and 13 mg/1 of SS for removals of 87 percent   The
 average sludge  age was 1.6 days, and the SDI was  1.5 g/100 ml.

      The reduced quantity of  the fungus in the mixed liquor  dur-
 ing this phase  may explain the improved overall  process perform-
 ance of the thirdwinter, but the reasons for the lower fungal
 concentration are purely speculative.  One possibility  is that
                                 32

-------
after the shutdowns and restarts of the first two winters, the
rapid growth of the fungus aborted the development of a proper
activated sludge culture, but. Phase 12 with no shutdown and
cold-weather restart began with a population that was able to
contain the fungi.
                                33

-------
                          TABLE  2.    OXYGEN  SYSTEM  PROCESS  PERFORMANCE
.,,-.-.._, . •• 	 —
I'h-se
ll-i d'*; f
1234
19/17- 12/10/72- 02/25- 04/00- (
5
6
7
8
)9/16- 1
9
0/14- 0
10
•S/^M/74 0
11
12
2/13/74-
I3/11/7S
11/25/72 02/01/73 04/05/73 05/31/73 00/3U//i UB/I1//J uv/ui//o iu/uo/u iw--/-- _-y -..,.. --, - .
How 3
Sewage, m /day
Ueturn Sludge', m /day
(mgd)
". Sludge Return
B011
Influent (mg/1)
Effluent (mg/1)
°u Removal
filtrate BOD
Influent (mg/1)
Effluent (mg/1)
* Removal
COD
Influent (mg/1)
Effluent (mg/1)
°-a Removal
Suspended Solids
Influent (nig/l)
1 Volatile
Effluent (mg/1)
"» Volati le

°u Remova 1
TOC
Influent [mg/1)
Effluent (mg/1)
t* llemoval
78,700
(20.8)
23,800
(6.3)
30
156
9
94
84
4
95
356
61
83
79
12
76


90
21
77
67,000
(17.7)
26,900
(7.1)
40
157
21
87
78
13
83
365
88
76
146
77
22
87


99
35
65
57,200
(15.1)
28,800
(7.6J
50
151
17
89
88
12
86
364
75
79
145
74
18
89


99
30
70
76,800
(20.3)
35.200
(9.3)
46
168
17
90
96
11
89
365
77
79
159
76
18
83


109
54
50
96.900
(25.6)
41,600
(11.0)
43
.740
24
90
130
14
89
320
7i
77
149
75
26
77


104
33
68
113,600
(30.0)
38,600
(10.2)
34
215
22
90
98
88
290
64
78
119
75
17
71


96
71
134,000
(35.4)
34,100
(9.0)
25
198
21
S9
82
14
83
308
62
81)
131
83
17
82


lOh
75
3R.200
(10.1)
9,500
(2.5)
25
178
19
89
•Jft
3
112
363
65
82
136
84
18
83
87


103
24
77
55.300
(14.6)
14,400
(3.8)
26
149
:3
91
70
6
91
314
57
S2
135
SO
17
76
87


110
21
8!
74.600
(19.7)
43,100
(11. -I)
58
136
26
81
77
16
79
50'
87
72
126
72
27
70
79


104
.12
60
72,300
(19.1)
23,400
(7.5)
39
14ft
24
84
SO
13
S4
-
142
79
26
82


-
75.700
(20.0)
21 .600
(5.7)
29
140
IS
S7
87
It)
S3
2S9
70
77
101
81
13
S2
S7


-
	 •- — ' 	 	 	 	 	 ...,.,
* Data for Phases 1-11 may
                    be in error because of air entrapment in return sludge magnetic flow meter.

-------
                       TABLE  3.    OXYGEN  SYSTEM  AERATION  TANK  PERFORMANCE_

Phase
Dates
MUSS (mg/U
". Vo kit i 1 e

Sludge Age* (days)
Sludge Retention
Time*" (days)
Detention Time (hr)
(Q« !()***
0
OJ '
Ul
HOD Loading, kg/day/m,
(Ib/day/ I 000 ft )
roll Loading, kg/day/m,
(Ib/day/ 1000 ft )
H/M Loading
(kg HOD/day/kg M1.VSS1
K/M Loading
(kfi Crn/day/kg MI.VSSI
	 	 - -. 	
IrtDbC O. U A l vj i. i\ .j
1 2 ^
4860 4980 '1010





1.1 1-3 1-3
1.4 1.7 2.0

2 61 2.24 1 .84
(163) (MO) (115)
S Or. 5.21 4.42
(372) (3251 (276)
0.63 0.55 0.57
1.45 1.28 1.38
~. 	 — 	 	 	

4 S 6
/06- 06/01- 07/08- 08y
3Q50 4530 4150
79 79 8?

1 5 1.5 1-4

14 1.3 1.2

1.0 0.8 0.7
1.5 1.2 1-0

1 74 4.95 5.19
(171) (309) (324)
5.9b O.bO 7.00
(372) (412) (437)
0.88 1.38 1.53
1.92 1.84 2.07
— — 	 	 	
	
7 8
mi/73 10/08/73 1
3130 4760
81 79

0.8 4.3

0.8 5.5

0.7 2.4
0.8 3.0

5.64 1.44
(352) (90)
8.78 2.95
(548) (184)
2.22 0.39
3.45 0.79

	
9 10
0/14- 02/06- OS.
0/25/73 04/30/74 OS
(9040)* 2400
80 78

1.2

0.9

1.6 1.0
2.0 1.5

1.75 2.)b
(109) (135)
3.6S 4.87
(250) (304)
I. IS
2.61

	
/Ol- 12/13/74-
/OS/74 03/1 1/7S
3870 2630
S4

1.8 1-6

1.2

1.1 1.2
1.6 1.5

2.24 2.2t>
(JJO) (141)
4.79
(2931
1.02
2. IS

   Samples prohalily contaminated hy foam.
   Oil 111 1 IL'S li l uuiH' * / "-"-•' • «• *••" • ••—	•'             'i-i    IA
'   Defined as kg M1.SS ill reactor/kg SS in reactor int luent/day.     ff]uenl/aay

-------
       TABLE 4.   OXYGEN SYSTEM FINAL TANK  PERFORMANCE AND SLUDGE SETTLING CHARACTERISTICS
to
en
Phase
Dates
FINAL TANK PERFORMANCE
Return Sludge SS
(mg/1)
"o Volati le
Return Sludge COD
(mg/1)
Detention Time, Q (hr)
Overflow Rate, m'/dav/iu^
(gpd/ft")

Solids Loading, kg/day/m"
(lb/day/ft )
Weir Loading, m /day/m
(gpd/ lineal ft)
SI.IJUGI- SETTLING
CIIARACTI-KISTICS
Sludge Hensity Index
Unstirred (g/100 ml)
Stirred at 1 rpra (g/100 ml)
Initial Settling Rate (1SR)
Unstirred (m/hr)
Stirred at 1 rpm (m/hr)
Wastrwarer Temperature (C)
Amtiient Temperature (C)
1
09/17-
11/25/72


16,200
83

20,000
2.3
39
(950)

2-14
(50)
1,615
(130,000)



2.2
-

3.2
3.4
19
14
2
12/10/72-
02/01/73


13,000
81

17,900
2.7
33
(810)

230
(47)
1,374
(1 10,600)



1.8
-

2.6
2.7
14
3
3
02/25-
04/05/73


11,500
80

15,400
3.1
28
(690)

171
(35)
1,172
(91,400)



1.2
2.2

1.6
3.0
14
9
4
04/06-
05/31/73


13,200
80

17,000
2.3
37
(920)

220
(45)
1,576
(126,900)



1.9
2.7

3.8
4.1
67
17
5
06/01-
06/30/73


16,300
79

18,800
1.9
47
(1160)

308
(63)
1,987
(160,000)



2.3
2.9

4.3
4.3
21
25
6
07/08-
08/11/73


lb,200
80

22,r-00
1.6
55
(1360)

313
(64)
2,329
(187,500)



2.3
2.8

4.4
4.6
24
28
7
08/12-
09/01/73


13.000
81

16,200
1.3
66
(1610)

259
(53)
2,749
(221,300)



2.1
2.5

5.5
5.5
24
28
8
09/16-
10/03/73


17,300
79

21,400
4.7
19
(460)

112
(23)
784
(63,100)



2.7
3.0

5.0
5.0
tt
"
9
10/14-
10/25/73


18,600
80

22.500
3.2
,,
(660)



1 . 1 35
(91,400)



2 0
2.S

2.0
2.1
21
IS
10
02/06-
CW/30/74


5,200
78

6.700
2.4
37
(900)

137
(28)
1,529
(123.100)



1.2
1.6

S.4
•1.0
12
S
11 12
05/01- 12/13/74-
08/05/74 03/1 1/7S


12,700 9,400
77 SI

13,200
2.S 2.4
35 37
(S70) (910)

190 I"1"
(39) (26)
1,483 1.SS3
(119.400) (125,000)



I."* IS



-
21 13


-------
                               TABLE  5.    OXYGEN  SUPPLIED  TO  OXYGEN  SYSTEM
Phase
Dates
kg/ra sewage
(tons/mil gal sewage)
kg/kg BOD removed
kg/ kg COD removed
kg/kg COD destroyed

Phase
Dates
kWh/m sewage
(hp-hr/mil gal sewage)
kWh/kg BOD removed
(hp-lir/lb BOD removed)
kWh/kg 02 supplied
(hp-hr/lb 02 supplied)
1
09/17-
11/2S/72
0.16
CO. 67)
1.1
0.6
-
TABLE 6
i
09/17-
11/25/72
0.22
(1117)
1.54
(0.94)
1.37
(0.83)
2
12/10/72-
02/01/73
0.16
(0.67)
1.2
0.6
-
3
02/25-
04/05/73
0.19
(0.79)
1.4
0.7
1.9
4
04/06-
05/31/73
0.16
(0.66)
1.0
0.6
2.0
5
06/01-
06/30/73
0.17
(0.70)
0.8
0.7
2.1
6
07/08-
08/11/73
0.16
(0.68)
0.8
0.7
3.5
7
08/12-
09/01/73
0.15
(0.62)
0.8
0.6
1.7
8
09/16-
10/08/73
0.24
(1.02)
1.5
0.8
1.3
9
10/14-
10/25/73
0.23
(0.93)
1.6
0.9
2.0
10
02/06-
04/30/74
0.13
(0.53)
1.2
0.6
3.5
11 12
05/01- 12/13/74-
08/05/74 03/11/75
0.16 0.17
(0.65) (0.72)
1.3 1.4
0.8
3.1
POWER FOR OXYGEN GENERATION AND DISSOLUTION
2
12/10/72-
02/01/73
0.27
(1371)
1.96
(1.19)
1.63
(0.99)
3
02/25-
04/05/73
0.33
(1676)
2.49
(1.52)
1.74
(1.06)
4
04/06-
05/31/73
0.24
(1218)
1.59
(0.97)
1.54
(0.94)
5
06/01-
06/30/73
0.20*
(1015)
1.01*
(0.62)
1.28*
(0.78)
6
07/08-
08/11/73
0.17*
(863)
0.95*
* (0.5S)
1.17*
* (0.71)
7
08/12-
09/01/73
0.15*
(761)*
0.90*
(O.SS)*
1.10*
* (0.67)*
8
09/16-
10/03/73
0.48
(2436)
2. 95
(l.SO)
1.89
(1.15)
9
10/14-
10/25/73
0.33
(1676)
2.42
(1.48)
1.48
(0.90)
10
02/06-
04/30/74
0.26
(1320)
2.38
(1.45)
1.89
(1.15)
11 12
05/01- 12/13/74-
08/05/74**03/11/7S
0.24
<_I21S)
1.S4
(I. IS)
1.39
(O.S4)
*  Includes 0.37 kWh/kg (451  hp-hr/ton) additional power to generate purchased cryogenic oxygen above 13.600 kg/day  US tons/day) PSA design capacity.
**  335-kW (450-Kp} PSA air compressor motor out of service for bearing repair from June 17 to August 1, 1974.

-------
                           TABLE  7.    OXYGEN  SYSTEM  SLUDGE  PRODUCTION
	 .,.- 	 	
riinso
UateS
1 2
3
09/17- 12/10/72- 02/25-
11/25/72 02/01/73 04/05/73
IVasTcd, i" /day
(gal/day)
Total SS, dry kg
(dry Ib)
Wasted/day*

In effluent/Jay

Total produced/day

Wasted, kg/kg
Rflll removed
Wasted, Kg/m' sewage
(Hi/mil gal sewage)
U) Produced, kg/kg
CO R01) removed
Produced, kg/m' sewage
(Ib/mil gal sewage)
Volatile SS, dry kg
(dry Ib)
Wasted/day*

In effluent/day

Total produced/day

has toil, kg/kg
RO[| removed
Wasted, kg/m' sewrifje
(Hi/mil gal •scv.agi-)
Produced, kg/kf.
HOP removed
Produced, kg/in' sewage
(Hi/mil gnl sewage)

(187


8
(17
1
(2
9
(20

-
0
(1

-
n
(i


6
(14
-
(2
7
(16

-
710
,000)


,100
,900)
,000
,300)
,1(10
.200)

1.0ft
.143
,190)

1.20
.161
,340)


,500
, 300)
900
,000)
,400
,3110)

O.R5
(1.11.1
-

-
0
(1
(950)

0 . 96
.ISO
,080)
4
04/Ob-
05/31/73
900
(239,000)


11,900
(26,300)
1,400
(3,000)
13,300
(29,300)

1.03
0.156
(1,300)

1.14
0.173
(1,440)


9,500
(21,000)
1,100
(2,500)
10,600
(23,500)

O.S2
0. 1J4
(1 .030)

0.92
0.139
(1 .It-Ill
5
06/01-
06/30/73
860
(228,000)


14,100
(51,100)
2,500
(5,600)
16,600
(36,700)

0.67
0.145
(1,210)

O.RO
0.172
0,450)


11 ,10(1
(24,500)
2 , 000
(4,30(1)
1 3 , 1 00
(2R.SOO)

0.53
0.115
(960)

0.62
0 . 1 36
(1.1 50 i
6
7/08-
08/11/73
890
(234,000)


14,300
(31 ,(,(10)
2,000
(4,300)
16,300
(35,900)

0.65
0.126
(1,050)

0.74
0.14.)
(1,200)


11,500
(25,300)
1 ,400
(3,000)
12,"00
(28,3001

0.52
0.101
(840)

0.59
0.113
(940)
7
08/12-
09/01/73
1.300
(343.000)


16,900
(57,30(0
2,300
0,000)
1«,200
(42,300)

0.71
0.126
(1 ,05(1)

0.81
0.143
(1,190)


13,700
(30,200)
1,900
(4,100)
15,600
(34.3001

0.5R
0.102
(850)

0.66
0.116
(970)
8
09/16-
10/08/73
190
(51,000)


3,400
(7,4(10)
700
(1,500)
4 , 1 00
(8,900)

O.SS
O.ORR
(730)

0.66
0. 106
(880)


2,600
(5,800)
600
(1,500)
3,200
(7,100)

0.43
0.1168
(570)

0.53
0.08'i
(700)
g
10/14-
10/25/73
350
(9.3,000)


6,500
(Il.JOO)
1 .000
(2,100)
7,500
(16.JOO)

0.87
0.119
(900)

0.99
0.136
(1.130)


5.200
(11,500)
7PO
(1,6(10)
5,900
(I-.IOO)

0.60
0.095
(790)

0.79
0.10S
(900)
10
02/06-
04/30/74
2,00(1
(529.000)


10,400
(23,0001
2,
-------
OXYGEN SYSTEM NUTRIENT REMOVALS

- _ . . — , 	
Dates
Total I'liosjihatp
(mi:/ 1 as P)
Influent
l-fflucnt
", Itentova 1
Soluble Orthophosphate
(mn/l as P)
Influent
Kfflucnt
",. Removal
Ammonia NitroRen
(IIIR/I as N)
Influent
r.ffluent
TKN
dnR/1 as N)
Influent
P.ff luent
Nitrite Ni frozen
[mil/1 as N)
Influent
lU'Cluent
Ni l rate NitroRen
(mi;/ I as N)
Influent
lit fluent

1 2 3
09/17- 12/10/72- 02/25-
11/25/72 02/01/73 04/05/73
~"
4.3 3,9 3.6
<.C> 2.6 1.5
40 33 5R

TC •* *> 17
1.7 1.4 1.1
32 36 35

9.3 9.0 9.4
8.0 9.0 9.7

22.0 22.4 22.0
1 .! . 4 1 4 . 4 1 - 05/01- 12/U/74-
10/25/73 04/30/74 08/05/74 03/11/75

4.1 2.4 - 2.1
2.3 0.7 - n-6
44 71 - 71

3.0 1-6 - !••»
1.8 0.3 - "-->
40 SI - 79

11.3 10.6 - 10-*
8.8 R.5 - 9.0

21.1 20.7 - 1S..1
12.0 13.1 - 12.6
_
o.i- O.H
0.11 0.11

1.74 1.97
1.67 1.61

-------
                         TAELE  9.     OTHER   OXYGEN  SYSTEM  SEWAGE  CHARACTERISTICS
                                 j         i         3         4        5        6        7        8         9        10       U       12
                             09/17-    W10/72- 02/25-    OJ/06-    06/01-    07/08-    08/12-    09/16-    10/14-    02/06-    OS/01-    12/13/74-
                             11/^5/72  OV01/73  04/05/73  05/31/73  06/30/73  08/11/73  09/01/73  10/08/73  10/25/75  04/30/74  OS/OS/74   03/11/75
Alkulinity
lmg/1  as CaOXJ

   influent                        ««        71        76       80       77        71        76        68        SO       76
   Effluent                        95        83        94       85       78        79        7,        74        74       /8


Dissolved Solids (.mg/1)

   Influent                      U56      1003      1038      992      1544        ------
   liffluiM.t                      1087       847       991      976      1 2• 8      <'•'      "-7       b-6       6'4       6'5      fS      *'o       I'*       t*
   >;...,, i                                          6.2      6.3       6.2       5.9       6.1      5.9      O.O       6.-       to..
   "fluent                        -       6.6      6.6      6.6       6.6       6.4       6.6      6.5      "-3       6.5       6.6

-------
TABLE 10.  NEWTOWN CREhK  AIR  PLANT PROCESS PERFORMANCE
Phase
Lljtes

I'low (Per 3;iv)
Su«;ige (mud)*
lieturn Sludge (ingj)*
"a Sludge iiettirt)
UOI)
Influent (inc/M
l;f f 1 ueilt 1 nit;/ 1 )
•I keitiova 1
l-i It rjte Hill)
Influent (mjj/1)
ft' fluent, lnm/l)
'ii Keinox';il
Suspended Sol ids
Influent (nn;/ll
-. Vn 1 .1 1 i 1 e
1. ('fluent I ing/ 11
'u Ueinovj 1
1 2 3
09/17- 12/10/72- 02/25-
11/25/72 02/01/73 04/05/73

]0.6 10.4 11.1
2.0 2.1 2.2
19 21) 20

156 !57 151
24 33 41
85 79 73

84 7K 83
111 27 27
88 tv. <>9

1-19 14() MS
79 7^ 74
4(1 47 .10
73 t>8 "2
4 5 6 7 8 9 JO 11 12
04/06- 06/01- 07/08- 08/12- 09/16- 10/14- 02/06- 05/01- 12/13/74-
05/31/73 06/30/73 Oi/'l/73 09/01/73 10/08/73 10/25/73 04/30/74 OS/05/74 03/11/75

10.4 12.0 12.0 12.1 12.4 i?.0 9.7 11.1 11. S
2.4 2.4 2.4 2.4 2.4 2.3 2.2 2.1 1.9
20 20 l!) 20 19 19 22 IS 17

168 240 215 19S 178 14S 1 31) l-'fa 'JU
37 46 35 41 30 24 23 32 2'->
78 81 84 79 S3 84 ST. 7S 79



159 14'.; 119 131 13o 13S 120 142 H SI
45 50 45 41 49 4b 53 .is
7: „„ hj 09 o4 (-h 72 .^ 56.

-------
                 TABLE  11.    NEWTOWN  CREEK  AIR  PLANT  AERATION  TANK  PERFORMANCE
Phase
totes
MI.SS  '.me/')


ShiJgu Age" (days)
                               !        2        3        4        S        6        7        8        9        1C        11        12
                           09/17-    12/10/72- OV75-    04/06-    06/01-    07/08-   08/12-    09/16-    10/14-    02/06-    05/01-    12/13/74-
                           11/25/72  02/01/^3  04/05/73  05/31/73  06/30/73  08/11/73 09/01/73  10/08/73  10/25/73  04/30/74  08/05/74  03/11/75
                               2(IO°
                                1.5
                                        jciOO
                                         1.5
                                                 1800
                                                          1800
                                                          1.3
                                                                   1800
                                                                   1.2
                                                                           1700
                                                                            1.4
                                                                                    1900
                                                                                     1.4
                                                                                             1900
                                                                                              1.3
                                                                                                      1800
                                                                                                       1.3
                                                                                                               1700
                                                                                                                        1700
                                                                                                                         1.2
                                                                                                                                 1600
                                                                                                                                 1.6
 . tent '.on 'rime  (hr)
            Q  » I?
            Q
                               2.27
                               2.71
^ 30
V?6
-> 17
2.(>0
i 3(1
2.77
2.00
2.40
2.03
2.43
1.98
2.37
2.41
2.96
2.13
2.53
2.15
2.50
HUH Uncling    ,
(lb/ Jay/ 1000 ft )«
                                 88
                                                           93
 •  Defined as kg MI.SS in  reactor/kg SS in reactor  influent/day.

 " 1  Ib/day/I»00 ft  = 0.016 kg/Jay/n .
                                                                    154
                                                                            138
                                                                                              118
                                                                                                        96
                                                                                                                 71
                      T'XBLE  \2.    NEWTOWN  GREEK  AIR   PLANT  FINAL   TANK  PE RFORNHNfT
                                        A N D   S L I) n G. E  S E T T L I N G  G11A R A G T E R I S T I G S

Phase
Dates
Keturn Sludge SS
(ma/1)
". Volatile
Detention Time, Q Ihrl
Overflow Kate IgpJ/ft")
So 1 ids Loading,
(Ib/day/ft")'
We i r Load in^
(g(>J/ lineal ft)**
Sludge Density Index
Unstirred (jj/100 ml )
-.
_ _ .. 	 . 	 , 	 ! 	 — — 	 ' 	 	
, > 3 4 S 6 7 S 9 10 11 12
09/17- 12/10/72- 02/25- 04/06- 06/01- 07/08- 08/12- 09/16- 10/14- 02/06- OS/01- 12/13/74-
11/25/72 02/01/73 04/05/73 05/31/73 06/30/73 08/11/73 09/01/73 10/08/73 10/25/73 04/30/74 OS/05/74 03/11/75
,, sun 10500 10300 10 ooo 10.300 in.&on 11.000 11.400 10,200 s.soo 10,200 9,300
"8I, ' 87 ' ."II 80 78 79 80 79 83 79 78 79
4. .11! 4.50 4.22 4.50 3.91 3.93 3.86 3.77 3.8S 4.82 J.ll 4.117
.,.,,1 4SO 510 48" 550 550 560 570 ShO 450 520 550
,j.(, .j.ci 9.1 8.5 9.8 9.3 10.4 10.7 9.S 7.7 S.7 S.I
66,300 1-5,001) 69,400 05,000 75,000 75.000 75,600 77. ..00 75,0(=0 60,600 71.300 71.90!!
1.5 1.4 1... 1.4 1.6 1.8 1.7 1.5 1.3 1.4 1.4 1.6
....... _ .. __ 	 . 	 " 	 — •••-'•
 *   I upJ/ft" = 0.041/m /Jay/itT

 "   1 Ib/day/l't" = 4.88 kg/day/m*
 ••  I j!p
-------
          TABLE  13.    POWER  CONSUMPTION  FOR  AERATION  AT  NEWTOWN   CREEK  AIR  PLANT         	


i,7~   ~	               i        2     ~~~34        5       6        7        8        9       10       11        12
I,.,'                         09/17-   12/10/72- 02/25-    04/06-   06/01-    07/08-    08/12-   09/16-    10/14-    02/06-   05/01-    12/13/74-
                           11/25/72  02/01/73  04/05/73  05/31/73  06/30/73  08/11/73  09/01/73  10/08/75  10/25/73  04/30/74__Og/05/_7j_03/n,/7S___
	                                                 '          85i       8fl5      87,      898       791      644
hp-hr/mil  sal sewage"             898       Sal      Bil


                                               0.94      0.83      0.48     0.55     0.64      0.07     0.83     0.97      0.83     0.71
hp-hr/lh BOO removed**
   1  hp-hr/mil sal  = 0.197  kWh/HlOO in3

   1  hp-hr/lli = i.M kWh/kg
                       TABLE  14.     NEWTOWN  CREEK  AIR  PLANT  SLUDGE  PRODUCTION
Tota I iirodtK-i-d/day/bay


W;isted/lh DOU removed

Wasted/mil jjal sew.-ijse*'

I'roduced/ Ih lull, removed

I'roJu-'e.l/mi 1 gal si-wage"*

3
" w/rT/73
16,500

20,200
1 . t>2
1 . .UK)
1.98
1 ,SJO
_ 	 . .

4
OS/31/73
15,400

1 9 , 300
1.35
1 ,-lSll
1.70
1.850
	 -. .—

S
06/30/73 Of
14.400

19,400
0.74
1 , -Mill
1 . OU
1 ,620
	 : 	

6 7
i/11/73 09/01/73 1
12,600 12,100
4 500 4 100
17,101) 16,200
0.71. 0.76
1 ,1150 1 ,001)
0.95 1.03
1,45(1 1,340
	 „ • -

8
0/08/73 10
1 3 , 300
5,100
18,400
0.87
1 ,070
1.20
1.480


9
/2S/73
1 2 . 300
4 .600
16.900
0.99
1 ,1.30
1.55
1,410


02/06- 05;
04/30/74 OSj
12,900
2,800
15.700
1 .41
1,331.
J.72
1 ,620


11 12
'01- 12/13/7--
'05/74 03/11/75
14.200 11,200
S.faP:1 4. OHO
17,800 15.200
1.31 1-05
1.240 9~0
1 ,c>4 I ..13
! , 560 ! , 32(1

   1  Ih - O.-IS kg

   1  Hi/mil sal * 0.12 kg/1000 m*

-------
   TABLE  15.   POWER CONSUMPTION FOR AERATION  AT JAMAICA STEP AERATION  AIR  PLANT
Month
Flow (mgd)*
BOD Removed in
Secondary System (mg/1)
hp-hr/mil gal sewage*
hp-hr/lb BOD removed**
03/72
95
82
619
0.90
04/72
95
83
577
0.83
05/72
93
79
619
0.90
06/72
97
70
577
0.97
07/72
89
61
619
1.19
08/72
91
72
577
0.97
09/72
92
98
619
0.74
10/72
92
66
644
1.19
11/72
99
80
619
0.94
12/72
94
92
SSO
0.74
01/73
92
99
619
0.74
02/73
88
97
619
0.74
   1 mgd = 0.044 m3/sec = 3785 m3/day
   1 hp-hr/mil gal = 0.197 kWh/1000 m3
   1 hp-hr/lb = 1.64 kKh/kj
   TABLE 16.   POWER  CONSUMPTION  FOR  AERATION  AT  26th  WARD STEP AERATION  AIR  PLANT
Month
Flow (mgd)*
BOD Removed in
Secondary System (mg/1)
hp-hr/mil gal sewage*
hp-hr/lb BOD removed**
06/75
79

86
349
0.48
07/75
88

75
295
0.47
08/75
90

43
215
0.60
09/75
89

52
201
0.47
10/75
82

54
215
0.47
11/75
82

66
241
0.43
12/75
78

58
255
0.54
01/76
85

48
228
0.56
02/76
81

54
228
0.51
03/76
80

S3
201
0.47
04/76
81

61
241
0.47
OS/ 76
87

47
2S5
0.64
06/76
8*

48
21S
O.S2
07/76
85

47
228
O.S6
08/76
87

•SO
201
0.59
09/76
SI

56
201
0.43
10/76
S3

47
201
O.S1
  1 mgd = 0.044 m/sec = 3785 m/day
*  1 hp-hr/mil gal • 0.197 kWh/1000 m3
** 1 hp-hr/lb =1.64 kWh/kg

-------
                    TABLE  17.   SLUDGE  PRODUCTION AT  JAMAICA  STEP  AERATION  AIR  PLANT
U1
Month
Row (mgd)*
BOD Removed (mg/1)
(Pri. * Sec.)
Effluent SS (mg/1)
MLSS (mg/1)
Sludge Age'* ((Jays)
Total SS (dry lb)*
Wasted/day (x 1000)
In effluent/day (x 1000)
Total produced/day
(x 1000)
Wasted/ lb
BOD removed
Wasted/mil gal sewage
Produced/ lb
BOD removed
I'nnluccd/rai 1 gal sewage
03/72
95
124
16
2900
4.8
118.6
12.7
131.3
1.21
1250
1.34
1380
04/72
95
122
17
2600
4.9
103.5
13.5
117.0
1 .07
1100
1.21
1230
05/72
93
120
15
2250
3.y
104.4
11.6
116.0
1.12
1120
1.25
125U
06/72
97
115
19
1800
3.1
98.8
15.4
114.2
1.06
1020
1.23
1180
07/72
89
103
22
1750
4.7
81.4
16.3
97.8
1.07
920
1.28
1100
08/72
91
115
22
3000
5.9
74.9
16.7
91.6
0.86
820
1.05
1010
09/72
92
109
29
2100
2.2
69.1
22.3
91.4
0.83
750
1.09
990
10/72
92
112
26
1700
3.8
65.0
20.0
85.0
0.76
710
0.99
920
11/72
99
102
26
2000
3.5
85.0
21. S
106. S
1. 01
860
1.26
1020
12/72
94
121
34
2400
3.7
78. *
26.7
105.3
0.83
S30
1.11
1120
01/73
92
125
22
1800
3.2
91.7
16.9
108.6
0.96
1000
1.13
11SO
02/73
88
138
25
1600
2.3
77.7
18.4
96.0
0.77
sso
0.9S
1090
        *  I mgd = 0.044 inVsec -- 3785 m /day
        *• He fined as kg Ml.SS in reactor/kg SS in reactor influent/day.
        '  1 lb = 0.454 kg
        " 1 Hi/mil gal = 0.12 kg/1000 m3

-------
                 TABLE   18.    SLUDGE   PRODUCTION  AT   26th   WARD  STEP
MI.SS (mg/l)
.,  r.                              n(,/7s  u///b  «»//3" 09/75  10/75   11/75  12/75  01/76  02/76   O.V76  (14/76  05/76  06/76  07/76
Motirn                               '                                	„„_  j.-^...	-i--.--.	•	—— —"••"— *	~	'	—      '


|:~o"w"'hlig~d)~™"«8     ^)0     M     82      *2     ?R     8S     R'      R"     S'     ^     M     RS      S?     ^     "5


BOP RemoveiUmg/1)                    ^     ^     5p     5f)     ^      M     ^     6S     „      M     M     ss     S8     (-:
Km-cm ss (»g/i)                    21      >o     ^     -"     lft     1S      I6     22     1S     1?      "     2'     1S     '7
                                   2700   2100   2200   2300   2300    1800   1900   25(10   230O    2100   2000   1900   1900   1700    19"C>   170n   2SOO


          ..  ,,    ,                  ,  j    , -,    3 1    •> Q    ,  8    -1.0    3.9    5.3    5.1     5.0    3.7    S.R    3.6    3.5     4.6    3.S    4.7
Sludge Age*'  (days)                  3-''    -1-'    J-'    - •s
                                   13.8   11.7   15.0    14.8   10.9   12.3   10.4   15.6    12.2   11.S    9.5   15.2    9.1   12.1    S.7   TO.!    13.S


 Total  produccd/dny „ ,000,         69.3   67.3   75.8    ,6.5   64.4   54.4   ,9.3   55.2    66.,   64.8   69.4   70.3    6R.0   64.3   5S.9   «..'    ,S.l



 WastcU/lb BOO removed              0.92   1.20   1.37


 Wasted/mil pal sewage



 Produced/Ih                                        ^                   q_   \ n\   1  ^0    1  >4   1  S9   1 .-19   1.67    1.67
 BOH removed                        1.14   1.46   1./1    1.-^_^^_^__n^
                                                       1.24   1.26   0.73   0.80   0.86   1.09   1.31   1.29    1.31   l.-tS   1.10   1.06   0.99    1.2S


                                   0.70   0.63   0.68   0.58   0.65   0.51   0.50   0.47   0.67   0.67   0.74    O.,o   0.70   0.6,   O.S8   O.M    0.65
 *  1  ingil =  0.014 m'Vscc = 3785 m' /day

 *• Defined  as kg MISS in reactor/kg SS  in renctor influent/day.

 *  1  Ih = 0.45.1 kg

 ** 1  Ib/mil gal = 0.12 kg/1000 mj

-------
                            SECTION 6

       EQUIPMENT AND INSTRUMENTATION OPERATING EXPERIENCES

     A multitude of equipment failures and inadequacies were
experienced during the course of the test.  Unless specifically
noted in the operational narrative, Section 5, these difficulties
did not significantly affect the overall performance of the pro-
cess.  However, the great number of problems did require a large
cv.nount of attention by the technical and operating staffs.  This
information is provided, not as a criticism of the original de-
sign and selection of particular products, but as a matter of
record.

PSA OXYGEN GENERATOR

     This unit was rehabilitated in late summer 1974 after 27
mo of rather unreliable service.  It operated practically flaw-
lessly after the overhaul, in contrast to its first 2 yr.

     Most of the problems were associated with malfunctioning
valves beginning early in the program, which resulted in moisture
contamination of two of the four adsorption beds.  Prom that
time forward, the maximum output of the unit was 10.4 metric
tons/day (11.5 tons/day) of 90 percent pure oxygen, instead of
the design rate of 15.2 metric tons/day (16.7 tons/day).  To
protect the adsorption beds from further moisture contamination
from stuck valves, an oxygen purity analyzer was later installed
to continually monitor the PSA product purity.  The analyzer
sounded an alarm when the purity fell to  85 percent and shut
down the PSA unit at 80 percent.

     Continued valve problems required the replacement during
the course of the test of all valves, valve actuators, and
solenoids, and some pressure switches.  The replacements, of
a different design, performed considerably better than the ori-
ginals, but they too failed to function properly from time-to-
time .

     During checkout before the initial process startup,  a de-
fective bearing was discovered in the PSA compressor motor, re-
quiring its removal and repair by the manufacturer.

     In September 1973, the PSA oxygen generator was again shut
down for 10 days awaiting the return of the compressor motor,
which had been removed for repairs  to the same bearing, and the

                                47

-------
repair cf a scored shaft.

     After 2 mo of operation, the PSA cooling tower fan motor
burned out, requiring its replacement; 2 mo later, the replace-
ment motor was removed for repair of a defective bearing.

     In the 27 mo prior to its overhaul, the PSA generator was
out of service for 3054 hr of a possible 18,504 hr, or 16.5
percent of the time.  In the 7 mo following its rehabilitation,
there were only 57 hr of interrupted service, or 1 percent down-
time .

     It must be noted that this PSA unit was the first of its
size ever manufactured, and so some bugs were inevitable.

LIQUID OXYGEN FEED VALVE

     In September 1973, with the PSA generator shut down for the
second compressor bearing repair, the process was dependent en-
tirely on the liquid oxygen supply.  At this most inopportune
time, the motor operating the liquid oxygen feed valve burned
out and had to be shipped to the manufacturer in California for
repair.  Without the automatic valve, the oxygen feed rate could
no longer be controlled by the gas space pressure and only manual
control through the valve bypass was possible.  This crude manual
control could not be adjusted for variations in organic  loading
and resulted in less effective oxygen utilization.  Although the
PSA unit was returned to service a week after the valve  motor
failure, once again permitting PSA oxygen feed control,  liquid
oxygen feed control was not possible during the 1 mo required
for the motor repair.

STAGE COMPRESSORS

     During the first days of the test, bearing failures attri-
buted to improperly manufactured ball retainers required the re-
placement of both sets of shaft bearings on all five gas recir-
culating stage compressors and the substitution of a conventional
petroleum lubricant for the synthetic-based lubricant originally
supplied.  Even after the replacements were installed, additional
bearing failures were experienced.  It was then discovered that
rain was entering the bearing housings through the shafts, conta-
minating the lubricant and causing the failures.   In October
1972, weather-proof shields were installed around  the shafts
and some bearings were replaced for the second time.  Still
another bearing failure occurred in August 1973.

     In addition to the compressor shutdowns resulting from bear-
ing failures, there were nuisance shutdowns caused by excessive
vibration and low seal air pressure during the first 5 mo.  Oc-
casional failures of the couplings between the seal air  compres-
sors and their motors, as well as failures of the  seal air sys-

                               48

-------
terns themselves, developed aCter a year of operation.  Some of
these difficulties were repaired by plant personnel, while others
required the services of the manufacturer,

PROPELLER MIXERS

     Oil leaks plagued the operation of the propeller mixers  un-
til, after  2 mo of operation, gaskets were fabricated for  the
speed reducers.  Improperly sealed rotating unions  resulting  in
considerable oxygen leakage required replacement; some rotating
unions were still leaking at the end of the test  program.  On
one of the  two first-stage mixers, the drive motor  burned  out,
some gears  and bearings required replacement,  and the motor
bearings failed.  After 6 mo of operation, the mixer high-oil
temperature and vibration shutdown systems, which were causing
nuisance shutdowns, were doomed extraneous and were removed.

RETURN SLUDGE PUMP

     The return sludge pump was the single most troublesome piece
of equipment.  With no spare unit provided, bearing failures  in
November 1972 and again in November 1973  required complete pro-
cess shutdowns to accomplish the repairs.

     In addition to the bearing failures, another problem  was
evidenced by the pump going out on overload at less than half
its capacity.  The overload resulted from debris  accumulating
between the shaft sleeve and the packing  and between the wearing
rings, and  also because of a restricted suction.

     When the pump was taken out of service for the first  bearing
replacement, the factory-supplied grease  seal  system was replaced
-with a water-seal system.  The higher pressure water-seal  system
prevented the  further accumulation of foreign  material between
the  shaft sleeve and packing and also halted the  excessive leak-
age  that had been experienced  through the packing.  The  first
plant  shutdown provided the opportunity to modify the pump suc-
tion  line;  remove the accumulation of grit, rags  and other for-
eign material  from the sump, which had been responsible  in part
for  the reduced pump capacity; and install a water  jet to  pre-
vent  future accumulations.  With the  improved  seal  system  and
the  suction modification,  the  pump output increased significant-
ly  and overload shutdowns  became less  frequent.   During  the
second  shutdown,  it was discovered that the clearance between
the  wearing rings was excessive, allowing debris  to accumulate
and  restrict the  rotation  of the impeller.  The clearance  was
reduced by  building up the  impeller wearing ring  in the  factory
because a  new  set of wearing rings was not readily  available.

WASTE  SLUDGE PUMP

      The  major  difficulty  with the waste  sludge system was an

                                49

-------
improperly-designed pump suction.  Originally, the suction line
consisted of a 7.6-cm (3-in.) pipe teed from the 51-cm (^0-in.)
return sludge pump suction line and operation was frequently
interrupted when a vacuum formed in the line and halted the
waste sludge flow.  Wasting was then attempted by manipulation
of valves and the use of an alternate pipeline, but a constant
flow could not be maintained.  During one of the shutdowns, a
piping modification was made to allow the waste sludge pump to
take suction from the discharge of the return sludge pump.  This
also proved unsuccessful:  with the waste sludge pump in series
with the much larger return pump, the waste flow v/as dictated
by the return pump and operation of the waste sludge pump vari-
able-speed controller had very little effect on controlling the
flow rate.  Finally, during the third plant shutdown, a new 7.6-
cm (3-in.) sucti.cn line from the pump directly to the sump v/as in-
stalled.  From then on, operation of the waste sludge pump com-
pletely independent of the return system was possible.

     The only problem with the waste sludge pump itself was a
cracked casing, probably caused by water freezing in the casing.
During the second summer of operation, the plant force installed
a water seal system for the pump to replace the factory-supplied
grease seal system.

MAGNETIC DRIVES FOR VARIABLE-SPEED PUMP CONTROL

     Before the initial process startup, the influent pump vari-
able-speed magnetic drive had to be removed and returned to the
manufacturer for the replacement of a defective bearing.  During
the second summer of operation, the magnetic pick-up, which is
the mechanism that initiated the automatic control of the return
 ;ludqe pump, became inoperative, requiring manual control of the
pump for a short time until the pick-up was replaced by the man-
ufacturer.  Two mo later, a faulty signal converter was discovered
in the return sludge pump variable-speed drive.  Following a
flooding of the pump pit, the waste sludge pump lost its speed
control and the pump could not be used for the weeks until the
manufacturer replaced the tachometer generator and the defective
drive bearings.

WASTE SLUDGE MAGNETIC FLOW METER

     In January 1973, after 8 mo of operation, a volumetric test
of the waste sludge magnetic meter showed that the meter v/as
reading low by almost 40 percent.  The manufacturer's explanation
was that the indicated calibration voltage may have been incor-
rect.  This error, coupled with additional problems encountered
with the power supply boards, required a non-linear correction
to the acquired data.  Consequently, the first 8 mo of waste
sludge data were inaccurate and had to be discarded.  The defec-
tive meter was replaced in February 1973 by one borrowed from


                                50

-------
another manufacturer, and in late March, the second mete:  w<   re-
placed by a third meter from a third manufacturer.  The .second
meter was satisfactory, but it was only a loan and had to be
returned.  By this time, the staff had become wary of magnetic
flow meters and weekly volumetric tests of the waste sludge meter
were begun.  Therefore, the waste sludge data acquired from March
1973 until the end of the test are reliable.  Although the per
manent replacement meter proved adequate, volumetric checks show-
ed that on two occasions it too required service.

RETURN SLUDGE MAGNETIC FLOW METER

     In September 1972, the first routine service check of this
meter revealed an improper electrical connection and an incor-
rect calibration voltage.  The return sludge flow data for the
first 4 mo of the project, before the meter was recalibrated,
were therefore dismissed.  Because of the large volume of return
sludge, a volumetric check could not be performed in place, as
was possible with the much smaller waste sludge meter.  The meter
was, therefore, removed for a factory bench flow test after al-
most a year-and-a-half of operation.  Accuracy within 1 percent
was ascertained.  Malfunctions of the electrical circuitry were
experienced on two occasions after September 1972 and were cor-
rected by the manufacturer.

     In November 1974, after the conclusion of 11 phases of the
test program, it was discovered that the return sludge piping
had been installed in a manner which permitted the entrainment
of air in the meter.  Since proper operation of a magnetic flow
meter requires full liquid flow, all return sludge data for the
first 11 phases before the condition was rectified must be viewed
with caution.  If anything, recorded return sludge flow data dur-
ing this period were higher than actual.

INFLUENT MAGNETIC FLOW METER

     The first routine service check in September 1972 also re-
vealed an incorrect   calibration voltage in the influent magne-
tic flow meter.  The resulting incorrect flow data collected
from May through September 1972 were, therefore, abandoned.
After recalibration, a volumetric check of the meter indicated
acceptable accuracy.  No electrical problems due to circuitry
were experienced with the meter.

OXYGEN FEED FLOW METER

     Difficulties were experienced with the flow totalizer
counter, the integrator, the square foot extractor, and the
multiplier-divider, all of which required service by the vendor.
Although the design combined oxygen supply capacity of the PSA
generator and liquid supply system was 30 metric tons/day  (33
tons/day), the upper limit of the oxygen feed flow meter was only

                               51

-------
23 metric tons/day (25 tons/day).  In the summer of 1973, when
system influent flow was increased to 1.31 m3/sec  (30 mgd), the
resulting increased oxygen flow exceeded, the capacity of the
meter.  During this period, oxygen feed was measured by adding
to the PSA generator output the amount of liquid oxygen trucked
in.  in September 1973, the capacity of the meter was increased
to 36 metric tons/day  (40 tons/day); however, incorrect calibra-
tion data were used to increase the range of the meter, and an
incorrect procedure was used during subsequent routine calibra-
tions.  The extent of  the resulting error was finally determined,
and all oxygen feed data acquired from September 1973 to April
1974 were corrected.

HYDROCARBON ANALYZERS

     For the  first 8 mo of the project, frequent failures  of  the
diffusion heads,  as well as large span errors and  drifts from
zero, were responsible for unreliable analyzer readings.   Accord-
ing  to the manufacturer, the poor performance resulted  from ac-
celerated oxidation of the heads  in  the moisture-laden,  oxygen-
rich  environment.  Performance improved after the  heads  were  re-
placed with others of  a design more  compatible with  an  oxygen
environment,  but  for  the remainder  of the  program,  the  zero and
spin  Required weekly  adjustments  and  the  diffusion heads required
replacements,  although infrequently.

OXYGEN PURITY ANALYZER

      Although this  unit performed satisfactorily,  slight drifts
 from zero  and span  errors  required  weekly calibrations.

 DISSOLVED  OXYGEN  METERS

      After 5  mo of  troublesome operation, automatic DO measure-
 ment was abandoned.   It was impossible  to keep  the meters  cali-
 brated.   Not only were the high DO levels accelerating the wear
 of the probes, but with the probes located in the sparger  bubble
 stream,  they were continually battered by turbulence, even after
 deflectors were installed.  The end of automatic DO measurement
 also halted automatic control of the first-stage DO level.
 Thereafter, the DO was determined manually with a portable analy-
 zer at infrequent intervals since that measurement was not con-
 sidered to be necessary for successful operation.

 SAMPLE COMPOSITORS

      The effluent automatic sampler operated successfully
 throughout the project, but the influent unit was not as  for-
 tunate .  The sampling line clogged so frequently  that after  a
 little more than a year of operation, it was retired and  grab
 sample compositing was substituted.
                                 52

-------
SERVICE CONTRACT

     In order bo ensure data accuracy, as we.1.1 as  to attend  to
the frequent instrumentation problems, a service contract was
entered into between the City and an instrumentation company.
This contract called J:or the services of a technician  1 full day
each week, in addition to emergency calls.
                               53

-------
                            SECTION 7

                      DISCUSSION OF RESULTS

     EPA's purpose in sponsoring the test was to obtain, evalu-
ate, and disseminate operating and performance data for us-* in
the design or upgrading of plants throughout the country.  Eqr; il-
ly important to EPA were sludge production, power and oxyjem /  -
quirements, and equipment performance.  In the vJew of the C;^.
of New York, the prime requisite for success and r ; joptance  f
the process was 90 percent removal of BOD and SS al; '.83 m-^, ; .-;„
(20 mgd) .   A large body of data was obtained even ^i'cer siz.ible
portions had to be discarded because of defective flow meters.
However, although effluent quality can be readily assessed, only
qualified conclusions can be offered regarding sludge production,
power requirements, and oxygen consumption.

OXYGEN SYSTEM PROCESS PERFORMANCE

     Effluent quality during the 12 phases averaged 19 mg/1 each
of BOD and SS and ranged from 9 to 26 mg/1 of BOD and 12 to 27
mg/1 of SS.  The averages for the eight non-filamentous phases
were the same--19 mg/1 for BOD and SS—and for the  four fila-
mentous periods, 21 and 20 mg/1, respectively.   Thus, although
the fungi, were responsible for some operating difficulties and
for increased sludge volumes, they had no significant effect on
process efficiency.

     No supportable relationship between sewage  flow and effluent
quality could be discerned.  During Phases 5, 6,  and 7, when  in-
fluent  flow rates were 120 to 177 percent of  the design  flow  and
the BOD loading rates were 123 to  140 percent of the design load-
ing, the effluent quality was only slightly below those  at lower
flows,  and, indeed, improved as the rate was  increased.

     Removals during Phase.1  (at constant  ilow,  not diurnal)  were
higher  than during  any other period—94 percent  of  BOD  and 92
percent of SS.  Removals during Phases  8 and  9,  at  flows only  49
and 7C  percent of Phase 1's  0.91 m^/sec  (20.8 mgd), and  during
the same season of  the year, were  3-5 percent less.  The reason
is  not  known.

     Also  unknown  is the reason  for  the  failure  of  the  activated
sludge  culture re  return to  its normal  diversity in Phase  11
following  the  severely  filamentous Phase  10.  Effluent  BOD and


                                54

-------
 SS  averaged  24  and  26  mg/1,  respectively,  just  about the  same as
 they  ware  during  Phase 10.

      There was  a  sharp drop  in  the  COD/BOD ratio  during Phases 5
 and 6 (June  and July  1973) and  a  gradual  return to  normal in
 later periods.  Compared  to  the four  earlier  phases,  influent:
 COD strength was  16 percent  lower during  Phases 5 and 6 but  the
 BOD was  38 percent  greater.

      Average influent  TOG ranged  from 90  to  11C mg/1 and  effluent
 TOG from 21  to  54 mg/1.   The 54 mg/1  occurred in  Phase 4  and  was
 far greater  than  the  usual average  effluent  range of 21 to 35
 mg/l.  Except for Phase 4, the  fungus periods were  highest in
 effluent TOG.

      There is strong  but  circumstantial evidence  that restarts
 of  the Newtown  Creek  oxygen  system  during  the first  two winters
 were  responsible  for  the  greater  growth of the  fungus experienced
 in  those winters  as contrasted  to the third winter.   However,
 complete shutdowns would  not occur  in a permanent plant system
 equipped with the usual assortment  of backup  equipment.

 CONSULTANT OBSERVATIONS AND  PILOT PLANT STUDIES

      The following conclusions  are  based on the fungus consult-
 ant's observations  (10) and  the 1974-1975  winter  oxygen pilot
 plant studies at Newtown  Creek  and  Wards Island:

 1.    The same fungus present in Newtown Creek wastewater  was  also
 present  in the  four other wastewaters sampled,  and,  thus,  it  is
 highly likely that it  exists at all other  City  plants.

 2.    The fungus organisms did not significantly concentrate in
 the mixed  liquor of the three other plants examined  nor in the
 Wards Island oxygen pilot plant.

 3.    Newtown Creek's wastewater Js  conducive  to the  growth and
 proliferation of the fungus  in  activated sludge mixed  liquor
 during cold weather (wastewater temperatures  below approximately
 60 F)  , more  so itnder oxygen.

 4.   No  fungicide or operating  strategy was found which could
 satisfactorily control growth of  the  undesirable  organisms during
winter operation at Newtown  Creek.

COMPARISON OF OXYGEN SYSTEM  AND AIR PLANT  PROCESS PERFORMANCE

     It was expected that the UNOX process would  provide  removal
efficiencies greater than those of the Newtown  Creek  air  plant,
for the air plant was being  operated  as a  high-rate  conventional
regime and the UNOX process  was considered a  substitute for step
aeration.  Excepting the severe fungal Phase  10,  the  UNOX  effln-

                                55

-------
ent averaged 15 mg/1 of BOD and 25 mg/1 of SS lower than the air
plant's, which operated at a flow of only 11.3 mgd.  In Phase 10,
the air plant effluent BOD was 3 mg/1 higher but the effluent
SS was 1 mg/1 lower.  However, during Phase 12 (the third win-
ter) ,  the UNOX effluent was better than the air plant's by 15
ivg/1 of BOD and 28 mg/1 of 3S.

     In terms of percent removal, the oxygen system averaged
88 percent for DOD and 86 percent for SS:  xor the air plant,
the averages were 81 and 68 percent, respectively.  Oxygen sys-
tem flow ranged from 0.44 to 1.55 m3/sec  (10.1 to 35.4 mgd) with
an average of 0.91 m3/sec  (20.7 mgd), while the air plant single
module average was 0.50 m3/sec  (11.3 mgd) with a range of 0.42
to 0.54 m3/sec  (9.7 tc 12.4 mgd).  Thus,  the oxygen system_per-
formed considerably better than the air plant en nearly twice
the flow.  In terms of filtrate BOD removal, the oxygen system
averaged 87 percent compared to 77 percent for the air plant.
Flow and process performance  (both concentration and percent re-
moval) data were presented previously  in  Tables 2 and 10  for,
respectively, the Newtown Creek oxygen demonstration and  full-
scale air systems.  BOD and SS  removals for the two systems  are
compared graphically in Figures 6 and  7,  respectively.

     The two  systems reacted differently  during the three win-
ters.  Oxygen system effluent  quality  was mildly affected during
Phase 3  (the  first winter) , but BOD removal by the air plant fell.
to  73 percent,  the  lowest of all  12 phases.  During Phase  10_(the
second winter), it was oxygen  process  performance  that deterior-
ated; the air plant was not affected.  During  Phase 12  (the  third
winter), however, the  air  plant was greatly affected  and  the
oxygen  system only  slightly.

      Separate  influent samples were collected  and  analyzed  for
the air  plant  and the  UNOX  system,  but the  UNOX  influent  data
have  been used  for  the air  plant  also  because  they  are  consider-
ed  more  reliable.   The air  plant  samples  were  composites  taken
at  the  entrances  to  the aerated  grit  chambers  of  two  of  the
14  tanks; the UNOX  samples  were taken  at  the  end  of  the  non-aer-
ated  qrit chamber where,  despite  some  settling of  SS,  the BOD
was only slightly reduced.  There was  a  more  serious  hazard  at
the air  plant sampling location,  where a  tendency  existed for
drawing  a stream  of  return sludge into the  aerated grit  chambers
and contaminating the  samples.

AERATION TANK PERFORMANCE

      The oxygen diffusion equipment at first was designed for a
BOD loading  of  15,150  kg/day   (33,400  Ib/day),  but was enlarged
before  construction to 18,915 kg/day (41,700 Ib/day)  because
the latest  analytical  data at the time showed the BOD influent
strength to  be ubout  250  mg/1.  Thus,  the design volumetric or-
ganic loading '.or the 4656-iP3 (1.23-m.il  gal)  aeration tank was

                                 56

-------
                  FLOW (MGD)" - OXYGEN SYSTEM vs. A!H PLANT
  FLOW
  (MGD)'
40-


30-


20-


10-


 0
               1 MGD = 0.011 M3/SEC
                             OXYGEN

                                PI AN I  DESIGN FLOW PER BAY
NAIR (FLOW PER BAY)
   -1—-—I—:—I—~—T
               1  '  2  '  3  '  4
                       5  '  6    7
                          PHASE
                                                   9 '  10 '  11 '  12
               EFFLUtNT BOD (MG/L) - OXYGEN SYSTEM vs. AIR PLANT
                                                              MINIMUM
                                                         FEDERAL STANDARD
EFFLUENT
  BOD     20 -
  (MG/L)
                    23    4    5    6    /
                                                   9    10   1'    12
                 BOD REMOVAL (%) - OXYGEN SYSTEM vs. AIR PLANT
           90-
   30D
 r.bMOVAL
                                                     MINIMUM
                                                FEDERAL STANDARD
                  '2'3'4'5'6'7 '   8  '  9   10 '  11   12

                                     PHASE
  Figure 6.   Comparison of  Newtown Creek oxygen system and  air
               plant  BOD removal  performance.

-------
                 FLOW (MOD)* - OXYGEN SYSTEM vi. AIR PLANT
 FLOW
 (MGD)'
         40 1
         30-
20
                                    OXYGEN

                                          .ANT DESIGN PLOW PER BAY
             ' 1 MGD = 0,044 M3/SEC
                  AIR (FLOW PER BAY)
              1  '  2    3  '  1   '  5    6  '  7  '  8  '  9  '  10  ' 11  '  12
         10-
              EFFLUENT SS (MG/L) - OXYGEN SYSTEM vs. AIR PLANT
EFFLUENT
   SS
  (MG/L)
         50


         40


         3° ^
         10-
                   MINIMUM FEDERAL STANDARD
          0   1  '  2  '  3 '  4  '  5  '  6  '  7 '  8  '  9 '  10  '  11 '  12  '
                                  PHASE


                SS REMOVAL (%) - OXYGEN SYSTEM vs. AIR PLANT
         90-i
                                                    MINIMUM
                                               FEDERAL STANDARD
   SS
 REMOVAL
              l'2345678'9   10  '11
         60
                                   PHASE
 Figure 7.   Comparison of  Newtown Creek oxygen system and  air
              plant  suspended solids removal performance.
                                   58

-------
4.05 kg BOD/day/m  (253 lb/day/1000 ft ).  The volumetric or-
ganic loadings encountered during most of the test were consid-
erably lower than the design loading, but during the high-flow,
high-BOD Phases 5, 6, and 7, they averaged 4.95 to 5.64 kg BOD/
day/m3 (309 to 352 lb/day/1000 ft3), 123 to 140 percent of de-
sign.  This was during the periods of 1.10-to 1.53-rn3/sec (25-
to 35-mgd) flows and BOD removal efficiencies of 90 percent.  It
can be said, then, that the process performed exceptionally v/ell
during 3 mo of flow and BOD overloading at high sewage temper-
atures and in the absence of filamentous organisms.

     The oxygenation tank detention time, which was 1.1 hr at
0.88-m3/sec (20-mgd)  influent flow and 25-percent return sludge
flow, decreased to 48, 44, and 40 min, respectively, during
Phases 5, 6, and 7.  These and other aeration tank data for the
oxygen system and air plant were shown previously in Tables 3
and 11, respectively.

FINAL TANK PERFORMANCE

     Oxygenated return sludge was expected to average 3 percent
solids, but the highest phase average actually obtained was only
18,600 mg/1 in Phase 9.  Excluding Phase 10, the average through-
out the test was 14,300 mg/1 compared to 10,500 mg/1 for the air
plant.  The reduced compaction of the sludge in the settling
tank, chiefly during Phase 10, required  the use of high return
sludge rates to maintain MLSS  (which averaged 3930 mg/1 for the
entire test program)  at desired levels.

     The oxygen system final tank overflow rate ranged from 19
m3/day/m2  (460 gpd/ft2) at a flow of 0.44 m3/sec  (10.1 mgd) to
66 m3/day/m2  (1610 gpd/ft2) at 1.55 m3/sec  (35.4 mgd).  The data
do not show any impairment of effluent quality due to increasing
overflow rate.  The adjacent Tank No. 10, which was kept empty
as a standby if more settling area was needed, was not required.

     The solids loading on  the oxygen settling tank ranged  from
.1.37  to 313 kg/day/m2  (28  to 64 Ib/day/ft ) , from  two to seven
times  the  loading on the  air plant  settling tanks.  Weir load-
ings reached a high of 2749 m3/day/m  (221,300 gpd/ft), compared
to the maximum of 963 m3/day/m  (77,500 gpd/ft) for the air  plant.
The  "Ten State Standards"  (7)  recommend  a maximum  overflow  rate
of 33  m3/day/m2  (800 gpd/ft2)  and a maximum weir  loading of  186
m3/day/m  (15,000 gpd/ft).   Fo*- solids  loadings,  the normal  prac-
tice is  59-88 kg/day/m2  (12-id Ib/day/ft2), with  a maximum  of
146  kg/day/m2  (30 Ib/day/ft2)  (8).

     Final  tank performance data  for  the two Newtown Creek  pro-
cesses were previously summarized  in  Tables  4  (oxygen) and
12  (air) .
                                59

-------
 SLUDGE SETTLING CHARACTERISTICS

      During non-fungus periods, the unstirred UNOX SDI averaged
 t.t g/100 ml, and seldom fell below 2.0.  During Phases 3 and
 10, and less so in Phases 2 and 12, the Index slid severely to
 averages of 1.2, 1.8, and 1.5 g/100 ml.  In addition, there were
 extended periods during Phase 10 when the SDI bottomed as low as
 0.4 g/100 ml.  A full plant-scale test under such circumstances
 would have been afflicted with a formidable sludge disposal pro-
 blem.  In contrast, the Newtown Creek air plant Index was not
 measurably affected by the fungus, averaging 1.5 g/100 ml
 throughout the project and on a monthly averaae basis varvinq
 only from 1.3-1.8 g/100 ml.   Sludge settling data for the oxygen
 ana air systems are included in Tables 4 and 12, respectively!

 OXYGEN SYSTEM OXYGEN REQUIREMENTS

      Throughout the test program,  an unknown volume of oxygen
 leaked through the oxygenation tank cover and through the mixer
 unions.   The vent gas was metered, but since the quantity lost
 through the leaks could not  be measured,  the amount of oxygen
 actually used could not be calculated.  It is for this reason
 that only oxygen supplied was  listed in Table 5.

      In  order to minimize the  leaks,  the  gas pressure under the
 cover was reduced to 2.5-5.1 mm (0.1-0.2-in.)  of water.   This was
 rar less  than the design pressure  of 25-76  mm (1 to 3-in.),  but it
 did not  affect the process.

      The  amount  of oxygen supplied averaged  173  g/m3  (1440  lb/
 mil gal)  and was somewhat proportional to  the  MLVSS and  the
 sludge age.   Based  on  BOD removal,  the oxygen  requirements  varied
 from 0.8  to  1.6  kg  supplied/kg BOD removed.   At  or  above  the de-
 sign flow,  the amount  of  oxygen  supplied  averaged 1.1 kg/kq  BOD
 removed;  at  flows  below  design,  it ranged  from 1.2  to 1.6 kq/kq
 During the  1973  summer high-loading  phases  (Phases  5,  6 and  7)
 the requirement  was  only  0.8 kg  supplied/kg  BOD  removed.       '

     There is much  less variation  among the  phase averages when
 the oxygen requirement is calculated on a COD  removal  basis    In
 the 11 phases  in which oxygen  supply was monitored, the require-
 ment was either  0.6 or 0.7 kg  supplied/kg COD  removed  in eiqht
 phases, and either 0.8 or 0.9  in the other three.   In  view of
 the  industrial nature  of  the Newtown Creek wastewater, COD re-
moval probably is the  better parameter.

POWER REQUIREMENTS

     The oxygen-generating and dissolution equipment, which  in-
cluded the PSA unit and its compressor, the  gas  recirculating
stage compressors, the stage  mixer spargers, and the liquid  oxy-
gen vaporizer, was sized for  a BOD loading of 18,915 kg/day
                               60

-------
(41,700 Ib/day),   Unfortunately, however, it was not equipped
with turn-down capability to accommodate lower loadings; about
all that could be done was to throttle the suction !ine of the
PS?, compressor, which reduced the power only slightly.  The re-
sult was that essentially the entire 746 kW (1001 hp*) of the
equipment was used at all times, regardless of the loading.  The
power requirements at BOD loading rates below design  (during all
phases except 5,  6, and 7), therefore, are not fairly repre-
sentative of the process.  It was only during those three 1973
summer phases when the equipment was fully loaded the>t the power
required can be equitably compared with the work performed.

     Tables 6, 13, 15, and 16 contain data on th
-------
     For Jamaica,  the  power  required  by  the air blowers during
the reporting period of March  1972"Febt:uary 1973 averaged 1./18
kWh/kg BOD removed  (0.90  hp-hr/.lb)  with  the lowest rate of 1.21
(0.7<1) achieved dnriny four  of  the  12 mo.   For 2Gth Ward, (;ho
average fj-om June  l97D~October  1976 was  Q.H4  kWh/kg BOD re-
moved  (0.51 hp~hr/lb)  with a j arnje  of 0.71  to 1.0'3 "(0.13 to
O.G-1).  Caution should be used  when eonsi derimj these power data
relative to tlic Newtown Crock  oxygena tion system data since the
parameter used here  (kWh/kg  BOD removed)  does not account for
differences in the  rate of oxygen consumption per unit BOD re-
moved or for differences  in  the plant loading relative to the
design point.  Therefore, direct comparison of the.se data to
data from the Newtown  Crook  oxygenation  system may not be valid.

SOLIDS PRODUCTION

     As a practical operating  consideration,  more important than
the dry weight of  sludge  produced is  its  volume,  for it is sludge
in its liquid form which  must  be processed.   When sludge is dig-
ested, as at Newtown Creek,  the volume can  best be measured when
pumped from a thickening  tank.   Waste oxygen  sludge was added to
the air plant's return sludge  system  because  piping the waste
oxygen sludge and/or oxygenated mixed liquor  to one of the
plant's eight thickeners  would  have been  too  expensive for what
was, after all, to have been only a 1-yr  test.   Thus, no informa-
tion was obtained on the  gravity thickening characteristics of
UNOX Sludge.

     Therefore, the only  estimation that  can  be made of excess
sludge production with oxygen  at Newtown  Creek is on the basis
of the dry solids  in the  waste  sludge and the final effluent.
Figure 8 compares UNOX sludge  production  at Newtown Creek with
that observed for the  air and  oxygen  trains at Batavia, New York
(9), and relates kg volatile solids produced/day/kg MLVSS to  kg
BOD removed/clay/kg MLVSS.

     Four Newtown Creek points  agree  very closely with the P.ata-
via oxygen distribution,  while  three  fungus points and one
transition point fall  in  the neighborhood of  the  Batavia air
distribution.  Sludge  production data for Phases  1 and 2 could
not be used because of the i.mccurately calibrated waste sludge
r.,eter in use at that time; Phase 9  data were  om.i tied because  the
mixed liquor samples were contaminated by the froth during that
period; and insufficient  solids  analysis were performed in Phase
11 to plot data from that phase.  In  comparing sludge production
data for Newtown Creek and Batavia, it should be  remembered  that
both plants operate wxthout  primary sedimentation.

     Newtown Creek oxygen system sludge production during normal
and fungus periods can also  be  compared with  sludge production
during the same periods for  the  Newtown Creek air plant.   As  pre-
viously summarised in  Table  6,  during non-fungus  operation, ex-

                                62

-------
         1.2
      CO
          1.0

         0.8
LLI
O
D
Q
O
QC  n G
Q.  0.6

CO
Q
_J
O
CO

3  0.4
      O
         0.2
          0
                                                           PHASE No. 7
                                 PHASE No, 12
                                    O
                   BATAVIA
                AIR AERATION
                                          BATAVIA
                                      OXYGEN AERATION
                     PHASE No. 8
                                     NEWTOWN CREEK

                                   O FILAMENTOUS PERIODS

                                   « NON-FILAMENTOUS PERIODS
                     0.4         0.8        1.2        1.6

                         KG BOD REMOVED/DAY/KG MLVSS
                                                        2.0
      *  INCLUDES BOTH WASTE SLUDGE AND FINAL EFFLUENT VOLATILE SOLIDS
Figure 8.  Excess solids produced by  Newtown  Creek oxygen system
            superimposed on Batavia, New York  sludge  production
            graph.
                                  63

-------
 cess solids generated by the oxygen system averaged 0.93 kg/kg
 BOD removed but rose to an average of" 1.27 kg/kg BOD removed,
 37 percent higher,  during Phases 3, 10,  and 12 (the three fungus
 phases).   For the air plant, the comparable figures were 1.27
 and 1.71  kg/kg BOD removed, respectively,  as documented pre-
 viously in Table 14.  Oxygen,  there tore,  produced on a BOD re-
 moval basis 27 percent less solids than  the air plant during
 normal periods and  26 percent less during  fungus periods.

      Data from the  Jamaica step aeration  air plant, which was
 not troubled by filamentous organisms, were confined to a nar-
 rower range, averaging 1.1.6 kg/kg BOD removed and varying from
 0.95-1.34 during the 12-mo period of March 1972-February 1973
 (see Table 17).  Using these bases, Newtown Creek oxygen system
 solids production when unaffected by the  fungus was 23 percent
 less than Jamaica's and during the fungus  phases, 6 percent
 more.

      A comparison can also be  made with the excess solids pro-
 duced at  New York City's 26th  Ward step aeration air plant (also
 not infected by filamentous growths)  during the first 17 mo fol-
 lowing its upgrading (Table 18).   At an average sludge age of
 4,0 days,  twice that of the Newtown Creek  oxygen system, solids
 production averaged 1.39 kg/kg BOD removed.   Oxygen system pro-
 duction wr.s 9  percent less solids during filamentous periods and
 33  percent less during non-filamentous periods.

 OXYGEN SYSTEM  NUTRIENT REMOVALS

      One  mo of  the  program had been set aside  for a test of
 phosphate  removal by alum addition.   However,  in  June 1973,  a
 state-wide ban  on the use of high-phosphate  detergents went into
 effect, reducing the already low  influent  phosphorus concentra-
 tion which had  averaged 3.9 mg/1  for  the previous 8% mo to 2.8
 mg/1 for  the month  of June.  Probably the  ban  had an effect be-
 fore June  because all high-phosphorus products  had to be removed
 from store shelves  before that date.  During  the  eight phases
 following  the  initiation of the ban,  the oxygen  system without
 alum addition achieved  59 percent total phosphorus removal  from
 2.P  mg/1 down to 1.2  mg/1.   The alum addition  test,  therefore,
 was  considered  unnecessary.

     Table 8 lists  by phase  the average concentrations  of influ-
 ent  and effluent  total  phosphorus,  soluble orthophosphate,  and
 the  major  nitrogen  components.  Influent soluble  orthophosphate
 was  similarly reduced by  the effects of the ban  from 2.2  mg/1  to
 1.7 mg/1  (both  as P).   The  average  effluent concentration from
 June 1973  on was  only 0.7 mg/1,

Ammonia nitrogen  averaged  9.5 mg/1  in the  influent  and  8.2  mg/1
 in the effluent.  Removals were erratic,  varying  from 0  to  39
percent.   The TKN content was relatively steady,  averaging  21.0

                               64

-------
mg/1 in the influent sewage and 12.8 mg/1 in the effluent.

OTHER OXYGEN SYSTEM SEWAGE CHARACTERISTICS

     Averages for alkalinity, dissolved solids, turbidity, and
pH were previously given in Table 9.  The principal item of in-
terest here was the drop in the pH of the wastewater in its trav-
el through the covered oxygen aeration tank and its recovery in
the settling tank.  This decrease in pH may have played some
part in the proliferation of the fungi.

     Analyses for dissolved solids and turbidity were discontinu-
ed after Phase 5 to reduce the workload on the laboratory.
                                65

-------
                           REFERENCES

 1.  Albertsson, J.G., McWhirter, J.R., Robinson, E.K., and
    Vahldieck, N.P.,  "Investigation of the Use of High Purity
    Oxygen Aeration in  the Conventional Activated Sludge Pro-
    cess," Water Pollution Control Research Series Report No.
    17050 DNW  05/70,  U.S.  Department of the Interior, Federal
    Water Quality  Administration, Washington, D.C., May  .1.970.

 2.  "Standard  Methods for  the  Examination of Water and Waste-
    water,"  13th ed., American Public Health Association,
    Washington, D.C., 1971.

 3.  Streeter,  H.W. and  Phelps,  E.B.,  "A Study of the  Pollution
    and  Natural Purification of the Ohio River," Public  Health
    Bulletin 146,  U.S.  Public  Health  Service, Washington, D.C.,
    1925.

 4.  "Methods for Chemical  Analysis of Water and Wastes," U.S.
    Environmental  Protection Agency,  Cincinnati, Ohio,  1971.

 5.  Private  communication  with R.F. Lewis, U.S. Environmental
    Protection Agency,  Cincinnati, Ohio, March  1973.

    Private  communication  with R.F. Lewis, U.S. Environmental
    Protection Agency,  Cincinnati, Ohio, November  1973.

 7.   "Recommended  Standards for Sewage Works," Great  Lakes  -
    Upper Mississippi River  Board  of  State Sanitary  Engineers,
    1971.

 8.  Dick,  R.I.,  "Role of Activated Sludge Final  Settling Tanks,"
    Journal  Sanitary  Engineering Division, American  Society of
    Civil  Engineers,  96, No.  2, pp.  423-436,  April  1970.

 9.  Brenner, R.C., "EPA Experiences  in  Oxygen-Activated Sludge,"
    Prepared for  the  U.S.  Environmental  Protection  Agency
    Technology Transfer Design Seminar  Program,  Cincinnati,
    Ohio,  October  1974.

10.  Private  communications (Progress  reports  to  New York City
    Department of  Water Resources)  with  W.O.  Pipes,  Department
    of Biological  Sciences,  Drexel University,  Philadelphia,
    Pennsylvania,  February and March  1975.
                                 66

-------
                           APPENDIX A

                DETAILED DESCRIPTION OF EQUIPMENT

MECHANICAL EQUIPMENT

PS7. Oxygen Generation System

     Oxygen gas was produced on-site by a Union Carbide pressure
swing adsorption (PSA) unit and its associated equipment, which
included an air compressor, cooling tower and pump, and instru-
ment air booster and dryer.  Air at rates up to 4050 std mj/hr
(143,000 scfh) and pressures up to 28,125 kgf/nr  (40 psig) was
fed to the PSA unit from a Clark Isopac-3 two-stage centrifugal
compressor, driven by a Louis Allis Co. 336-kW (450-hp) motor.
The PSA unit was designed to produce 473 std mj/hr  (16,700 scfh)
equivalent to 15.2 metric tons/day (16.7 tons/day) of  90 percent
pure oxygen, or 13.6 metric tons/day (15 tons/day) of  100 per-
cent pure oxygen.

Liquid Oxygen Tank and Vaporizer

     These units consisted of a Union Carbide liquid oxygen
storage tank with an equivalent gas capacity of 35,853 m
(1,266,000 ft ) and an electrically-heated, water-bath vaporizer
with a capacity of 510 std m3/hr  (18,000 scfh) of  gas.  The  tank
was a double-walled, vacuum-power-insulated unit  with  a liquid
capacity of 42 m3  (11,000 gal) and a working pressure  of  45,700
kgf/m2  (55 psig).  The vaporizer consisted of a l.Q-nH  (500-gal)
water ballast tank including a vaporizer coil for the  product
stream, smaller pressure-building coil  for pressure maintenance,
and an electric immersion heater.  The  heater, rated at  72 kW,
maintained a  temperature of 130 F.  A  sensor in the water bath
signaled an alarm  if  the temperature fell below 90 F,  and another
sensor in  the oxygen  piping downstream  of the vaporizer  sounded
an alarm if the temperature of the oxygen fell below 0 F.

Mixers

     The characteristics of the eight  Philadelphia Gear  mixers
were slightly different  from  stage  to  stage.  The Stage  1 mixers
were driven by  37-kW  (50-hp),  1750-rpm motoio, with 183-cm  (72-
in.) propellers at a  267-cm  (105-in.)  pitch  rotating at 77  rpm.

     The mixers in Stages  2,  3, and  4  were  driven by  22-kW  (30-
hp), 1750-rpm motors.   The  propellers  in  Stage  2  were  183-cm

                                67

-------
 (72-in.) diameter, 224-cm  (88-,in.)  pitch,  and 70 rpm;  .in Stage 3,
 they were  183~cm  (72~.in.)  diameter,  183-cm (72-in.)  pitch, and
 74 rpm; and  in Stage  4,  .188-cm  (74-in.)  diameter,  188-crn  (74-in.)
 pitch, and 71 rpm.  Eight-arm oxygen  .spargers were rnountod to the
 bottom of  the hollow, stainless  steel mixer  .shafts 46-cm  (18-in.)
 beneath the  propellers.  Johnson  rotary  joints were  used at the
 tops of the  .shafts as oxygen lead-ins to the rotating  shafts.

 Mo t or_Cp n t rp l_Center

     The 460-volt motor  control  center  (by General Electric Co.)
 was located  in the control building  and  contained  motor  controls
 for all major system  equipment,  including  the PSA  air  compressor,
 cooling tower pump and fan, instrument air compressor, mixers,
 oxygen recirculation  compressors,  influent pumps,  return sludge
 pump, and waste sludge pump.

 Main Instrument Panel

     The main instrument panel  (MIP),  located in the control
 building, contained all  the major  instruments,  controls,  and
 recorders, in addition to  the annunciator  system for signaling
 abnormal operating conditions and  alarms.  The  controls  and
 instruments  on the MIP are described  individually  later  in this
 appendix.

 Oxygen Recirculation Compressors

     Five compressors (Hoffman Division  of Clarkson Industries)
 were provided, two for the first  stage,  and  one each for  Stages
 2, 3, and  4.  The Stage-2 unit was rated at  21  s td rn3/min (750
 scfm), the other four at 18 std m3/min (650  scfm).  Each  was
 driven by a  30-kW (40-hp), 3550-rpm motor  and provided with an
 integral seal air supply and necessary instrumentation for surge
 prevention and vibration protection.  The  suction  line leading
 to each compressor was equipped with  a V.D.  Anderson Co.  "Hi-eF"
 separator to remove liquid entrained  in  the  recirculated  gas.

 Influent Pumps

     These units were Worthington  61-cm  (24-in.) "Mixflo"  horizon-
 tal volute pumps.   The variable-speed pump was  driven by  an
Electric Machinery Arnpli-Speed magnetic drive from a Westinghouse
 119-kW (150-hp),  585-rpm motor.   A Regutron  II  control and  F.IS
 signal transmitter were used to regulate the  magnetic drive.
The constant-spaed pump was driven directly  Ly  a Westinghouse
 119-kW (150-hp),  585-rpm motor.

R^oturn Sludge Pump

     This variable-speed pump was a Worthington 51-cm (20-in.),
0.66-m3/sec  (15-mgd)  "Mixflo"  vertical volute pump, driven  by

                               68

-------
an Electric Machinery Ampii-Speed magnetic drive  From a Westing-
house 75-kW (100-hp), 705-rpm motor.  A Regutron  II control and
an RIS signal transmitter regulated  the drive.

Waste Sludge Pump

     The waste sludge pump was a variable-speed,  ITT Mar.Low,
vertical "Vane-Flow" solids-handling unit with a  0-1135-1/min
(0-300-gpm) range, driven by an Electric Machinery .\rnpli-Speed
magnetic drive from a 5.6 kW (7'-2-hp), 880-rpm motor.  The Arnpli-
Speed drive was controlled by a Regutron II control, and speed
was manually regulated from the control building.

AUTOMATIC VALVES

Liquid Oxygen Feed Valve

     The Driox feed valve was a 5-cm (2-in.) Masoneilan electron-
ically-controlled automatic globe valve with cast bronze body,
percent-contoured bronze trim, and Teflon seat.   It was operated
by a General Controls hydromotor actuator in response to a 12-
to 20-ma increase-to-open input signal.  The valve was set to
fail closed upon loss of power.

Oxygen Feed Valve

     The PSA oxygen valve was a 5-cm (2-in.) Masoneilan auto-
matic bronze globe valve with a 3.8-cm  (1^-in.) percent-contoured
trim.  It was pneumatically-controlled, diaphragm-operated,
2100-6300 kgf/rn^ (3-9 psig)  air-to-open, and equipped with a
positioner.  An adjustable limit stop permitted presetting the
maximum open position of the valve.  A solenoid valve in the
diaphragm supply normally was energized to allow  the valve to
respond to its positioner signal.  The solenoid valve war, de-
energized automatically in the event of a lower explosive level
(LEL) alarm, or manually by operation of a switch which inter-
rupted the signal, thereby closing the oxygen feed valve.

Stage 1 Mixer Bypass Valve

     The bypass valve was a 10-cm  (4-in.) Masoneilan electronic-
ally-controlled automatic globe valve with cast bronze body,
percent-contoured bronze trim, and Teflon seat.   It was operated
by a General Controls hydromotor actuator in response to a 4-tc
20-ma increase-to-open input signal.

Air Bypass Valve

     This was a 10-cm (4-in.)  Norriseal automatic butterfly valve,
with case iron body, neoprene seat, Buna-N seals, and aluminum-
bronze disk.  The valve was pneumatically-controlled, diaphragm-
operated, 2100-10,500 kgf/m^ (3-15 psig) air-to-open, with its

                               69

-------
air line interrupted by a solenoid valve.  The solenoid was
normally energized, keeping the valve closed.  The solenoid was
deenergized either manually by operating a sv/itch or automatic-
ally in the event of an LEL alarm.
Relief Valves

     These valves were 30-cm  (12-in.) Oceco regulators with
Pluorel  (Viton) diaphragms designed to provide both pressure and
vacuum relief.  Those for the first three stages were set to open
at 15 cm  (6 in.) of water, the fourth-stage valve at 13 cm  (5 in.)
of water.  All were set to open at 10 cm  (4 in.) of vacuum.

INSTRUMENTS

Stage 1  Pressure Controller

     The  Stage  1 pressure controller, located on the MIP. was a
Honeywell electronic deviation-indicating controller with a  4-
20-ma input signal and a 4-20-ma output signal.  The controller
was  reverse acting, that is,  a decreasing input signal caused
the  output to  increase.  The  controller had both manual and
automatic control selection;  the output signal was  continously
displayed.

Stage 1  Pressure Recorder/Oxygen Feed Signal  Recorder

     A two-pen Honeywell strip chart recorder on the MIP  recorded
Stage 1  reactor pressure and  the oxygen feed  signal on a  single
0-100 chart.

Oxygen Feed Flow Totalizer

     This instrument  consisted of  a  Honeywell linear  integrator
and  a Honeywell totalizing  counter with mechanical  reset,  both
located  on  the MIP.   The  integrator  accepted  a  1-5-volt-dc input
signal  linearly proportional  to  the  oxygen  flow and produced
25-volt  pulses to  drive  the totalizing  counter.

Oxygen  Feed Flow Recorder/Vent  Gas Pressure Recorder

      A  two-pen Honeywell  strip  chart recorder on the  MIP recorded
on a single chart the oxygen flow to the  aerator and  the vent
gas  pressure  at Stage 4.

Oxygen  Purity Analyzer

      This instrument, a Servomex Controls Ltd.  (Adam David Co.)
oxygen  analyzer,  was also mounted on the MIP.  It had two scales,
 0-25 percent and 0-100 percent,  and provided an output signal of
 0-10 mv dc proportional to the  scale,  which was converted to a
 4-20-ma signal.  The analyzer normally monitored the purity of

                                   70

-------
the vent gas stream from Stage 4, but connections permitted sam-
pling the PSA stream or the oxygen content of any of the other
stages.

Oxygen Purity Recorder

     An instrument on the MIP recorded the oxygen purity on a
single 0 to 100 chart.

Stages 1 and 4 Combustible Gas Detection Systems

     Two identical combustible gas detection system were pro-
vided to monitor Stage 1 and Stage 4 gas.  Each system, by Mine
Safety Appliances, consisted of flow control components and the
MlP-mounted analyzer unit.

     The flow control components consisted of the diffusion head
for detecting combustible gas concentrations and a flow meter
and necessary filters to protect the devices.  A pressurized
stream from the recirculation compressor normally v/as sensed;
however, the low-pressure reactor gas space could be sampled
by the use of a pump and appropriate valves on the sample rack.
The analyzer contained a power supply, readout circuitry, alarm
circuits, and operating controls.  Dual set points were provided
to signal the detection of combustible gas when it reached 25
percent of the LEL, and again when 50 percent of the LEL was de-
tected.

     Alarm switches announced alarm levels of combustible gases in
the stages and triggered automatic responses in the control cir-
cuits .

Stages 1 and 4 LEL Recorders

     A two-pen Honeywell strip chart recorder on the MIP recorded
LEL levels for Stages 1 and 4 on a single 0-100 linear chart, re-
presenting percent of LEL for hexane, the hydrocarbon for which
the analyzer was calibrated.

Vent Gas Flow Meter and Totalizer

     An Eastech, Inc. 8-cm  (3-in.) vortex shedding flow meter was
provided with an Eastech signal conditioner and totalizer to
measure vent gas flow from Stage 4.  The meter body and bluff
body were of 316 stainless steel, and the 0-rings of Viton.

Influent Flow Meter and Transmitter

     This instrument was a Brooks Inscruments electromagnetic
flow-sensing device with an integral signal converter and located
in the influent line leading to the aeration tank.  The flow tube
was neoprene-lined stainless steel, and the 316 stainless steel

                               71

-------
electrodes were equipped with automatic mechanical electrode
cleaners.  The converter produced a linear output signal of 4-20
ma.  The meter had a flow measuring capacity of 94.6 mVmin
(25,000 gpm).
Influent Flow Controller

     This controller was a Research, Inc. "Data-Trak" programmer
which could provide a 24-hr cycle by varying the output signal
according to the time of the day.  It was equipped with a Re-
search, Inc. Model 607-R1000 "Match-Pack" signal transducer
which converted the 0-1000-ohm output to a 4-20-ma output signal.

Influent Flow Totalizer

     This influent flow totalizer consisted of: a Honeywell linear
integrator and a Honeywell totalizing counter with mechanical
reset, both located on the MIP.  The integrator accepted a 1-5-
volt-dc input signal linearly  proportional to the influent flow
and  produced 25-volt output pulses  to drive the totalizing
counter.

Influent Flow, Return Sludge Flow,  and Waste Sludge  Flow Recorders

     A  three-pen Honeywell strip chai t recorder on the MIP re-
corded  the  flow rates of  the three  system  streams on a single
chart.

Return  Sludge Flow Meter  and Transmitter

     A  57-m3/min  (15,000-gpm)  Brooks  Instruments  electromagnetic
meter with  integral  signal converter  was provided  to monitor re-
 turn sludge flow.  The  tube was  neoprene-lined  304  stainless
 steel  and  the  electrodes  316  stainless?  steel  equipped with  auto-
matic mechanical  electrode cleaners.

 Re turn  Sludge  Flow Controller

      This  unit was a Honeywell electronic deviation-indicating
 cascade controller which accepted both a 1-5-volt-dc signal in-
 put proportional to the return sludge flow and a 1-5-volt-dc,
 remote, set-point input from a ratio controller for cascade
 operation.   The controller could be operated in manual,  auto-
 matic,  or cascade modes.

 Return Sludge Flow Ratio Controller

      A Honeywell electronic ratio/bias device receiving a 1-5-
 volt-dc input signal and producing a 4-20-ma output signal was
 included with the return sludge flow control package.
                                72

-------
W=aste Sludge Flow Meter and Transmitter

     The waste sludge flow meter was a 1.1-m /min  (300-gpm) Honey-
well electromagnetic flowhead with integral signal converter and
a neoprene-lined 304 stainless steel tube and 316 stainless steel
electrodes equipped with ultrasonic cleaners.

Waste Sludge Flow Totalizer

     The waste sludge flow totalizer consisted of a Honeyv/ell
linear integrator and a Honeywell totalizing counter with me-
chanical reset, both located on the MIP.  The integrator accepted
1-5-volt-dc input signal linearly proportional to the waste
sludge flow and produced 25-volt output pulses to drive the
totalizing counter.

Sample Compositor System

     Two Union Carbide flow-proportional samplers, one for the
influent from the grit chamber and the other for the settling
tank effluent, were used for collecting system influent and
effluent samples.  During each sampling action, a  3-m.l portion
was taken from the respective stream and deposited into a  re-
frigerated jug.  The device varied the rate at which the portions
were taken in accordance with an internal rate control adjust-
ment and an external flow ratio control signal.  The external
signal required was 5-20 ma with the 5-ma signal producing high
sampling rates  (6 ml/min maximum).

Sample Compositor Flow Ratio Controller

     This segment of the sample compositor  system  was  composed of
a  Honeyv/ell electronic ratio-bias  station that received a  1-5-
volt-dc input signal and produced  a  4-20-ma output signal.   The
ratio of the output signal  to the  input signal was set by  the
vertical thumbwheel and could be varied from 0.3 to  3.0.
                                 73

-------
                           APPENDIX B
          ESTIMATED CAPITAL COST FOR CONVERSION OF THE
         NEWTOWN CREEK PLANT TO OXYGEN ACTIVATED SLUDGE

     ThP EPA Project Officer requested that an estimate be  _
added to this report of the capital cost that would be required
if the entire Newtown Creek plant were converted to oxygen
activate^ sludge.  Design and estimated cost data are based on
?,he UNOX system and were provided by Union Carbide Corporation.

DESIGN BASIS

     Since the termination of data collection on the UNOX
system demonstration module, the Manhattan pumping sta ion  has
been completed, bringing an approximate 5.3 mVsec  (120 mgd)  of
very dilute wastewater to the Newtown Creek plant via a force
main under the East River.  The net effect of this additional
contribution  to  the plant's influent has been a  significant
reduction in  wastewater  strength.  Raw wastewater character-
istics  during the  project and  after addition of  the  Manhattan
sewage  are compared in Table 19.

         'TABLE 19.   COMPARISON  OF NEWTOWN  CREEK WASTEWATER
                    CHARACTERISTICS BEFORE AND AFTER
                    INTRODUCTION OF MANHATTAN FLOW
                      Characteristics During
                      the Project:
                      Brooklyn and Queens
                      Flows Only  (range of
                      monthly averages)
                     Current  Character-
                     istics:  Brooklyn,
                     Queens,  and Manhat-
                     tan Flows (typical
                     values)
 BOD (mg/1)
 COD (mg/1)
 Suspended Solids
    (mg/1)
150 - 240
290 - 365

100 - 160
130
260

100
      The current flow of 5.3 m3/sec  (120 mgd) from Mannattan is
 far less than the original estimate of 7.4 m3/sec  (170 mgd)   For
 thi- design exercise, the average dry-weather hydraulic loading
 selected fSr the full-plant conversion to oxygen at Newtown Creek
                                74

-------
is 13 4 mVsec (307 mgd).   This allows for a modest increase in
the Manhattan flow to about 5.9 n^/sec (135 mcj«3) .  Combined
with an average BOD of 130 mg/1,the design average BOD  loading
is, therefore, 150,980 kg/day  (332,850 Ib/day).

OXYGEN SYSTEM DESCRIPTION AND  DISCUSSION

     Since the original design  and construction  of the  UNOX
System demonstration plant at  Newtown Creek,  the technology
base for oxygenation system process and equipment design  hao
been greatly  expanded through  extensive research and  development
programs, equipment testing and vendor development programs,
and  design and operating  experiences on the more than 100
oxvqenation  systems currently  in  operation around the world.
in fact, the  previously-cited  problems experienced with equipment
and  instrumentation during the Newtown Creek  demonstration
project  initiated  many  of the  programs mentioned above.  As  a
result of these  efforts,  many  improvements have been  made in
equipment reliability  and performance  as  well as in  operating
cower  efficiency of  oxygenation systems  over  the last 6 yr.  The
Sygenation  system described  below,  which is  proposed today  for
upgrading of the entire Newtown Creek  facility, bears little
resemblance  to the original  demonstration system in  terms of
the specific mass  transfer,  oxygen generation, and  control
 instrumentation equipment included in  the system.  However  the
 functional  definition of  the oxygenation system and  the process
 parameLrs  used to design the system remain  entirely consistent
with the system tested and performance results obtained during
 the Newtown Creek demonstration project.

      Based  on the organic loading defined above  and  the Process
 performance data gathered during the testing program,  a UNOX
 svstem to treat the Newtown Creek wastewater would require
 conversion of 14 of  the  16 existing aeration tanks to  oxygen
 Service   Each  tank would be modified to contain four  equal-
 volume stages operating  in series   Each .^age  would be  15.2 m
 lona x 16.8 m wide x 4.6 m liquid depth  (50  ft  x 5^  ft x  15 It)
 and contain  1168 m3  (308,590  gal) of mixed Ixquor.   The  total
 oxyqenation  volume would be 65,410 m3 (17.28 mil gal).   One
 surface aerator would be provided in each stage for  mixing  and
 mass  transfer.  Each first stage would have  an aerator with an
 installed nameplate rating of  44.7 kW  (60 nameplate  hp (nnp)).
 The second  staqes would  be equipped with aerators having name-
 plate Stings of  29.8  kW (40  nhp).  The  third  and fourth stages
 would be equipped with aerators  having nameplate ratings of
  22  \  kW  (30  nhp).  Thus, each aeration  tank  would contain four
  surface aerators  with  a  total nameplate  power  of 119.3 kW (160
  n"Pf  and the  total  system  installed  power  for oxygen dissolution
 would be 1670  kW  (2240 nhp)  at 480  volts.
                                 75

-------
     The surface aeration mass transfer equipment proposed here
for upgrading the Newtown Creek facility is substantially
simpler and in much broader use for similar applications than
the submerged turbine system originally tested during the
Newtown Creek demonstration project.  Employing surface aerators
would eliminate many of the pieces of equipment which were sources
of mechanical problems during the testing program, such as the
gas recirculation compressors and the rotary unions connecting the
oxygen gas piping to the mixer sparger unit.  A substantial
amount of oxygen piping would also be eliminated.  Furthermore,
use of surface aeration equipment would eliminate or minimize
the problems caused during the testing program due to foaming
since the high level of surface turbulence and mechanical
agitation would disperse the foam if it tended to form.

     The existing UNOX system demonstration module (Aeration
Tank No. 9), which utilized the submerged turbine equipment,
would either be dismantled or "mothballed".  This tank along
with one other aeration tank (not specified for this exercise)
would not be incorporated in the upgraded oxygen system design,
but their companion final tanks would be used to keep secondary
clarifier overflow rates as low as possible.  The aerated grit
chambers mated with the two aeration tanks to be removed from
service would also be retained to maximize grit removal.
Figure 1 presented previously in Section 1 illustrates the
plant layout and the interrelationship of the various tank
complexes.

     Modifications to the existing tankage would include:  (1)
removal of all air diffusers and associated piping from the
aeration tanks, (2)  installation of three interstage partitions
per aeration tank with openings to permit flow of mixed liquor
and gas from stage-to-stage, (3)  installation of gas-tight
covers for the aeration tanks to retain the oxygen rich gas,
(4) installation of a new sludge recycle pump station, and (5)
improvements to the 16 aerated grit chambers and 16 final settling
tanks.  The 0.9-m (3-ft)  freeboard available in the 5.5-m (18-
ft) deep aeration tanks would provide sufficient gas space for
the surface aerators employed in UNOX designs.

     A cryogenic oxygen generation plant having a production
capacity of 171 metric tons/day (188 tons/day) of 95-99 percent
pure oxygen would be the recommended unit to supply oxygen feed
gas to the oxygenation system.   Two 189-m3  (50,000-gal) DRIOX
storage tanks with 434 metric tons (478 tons) of oxygen capacity
would be recommended for back-up liquid oxygen supply, which  is
sufficient for 2.5 days of operation at design average-load
conditions when the cryogenic oxygen generation plant required
maintenance or repairs.  At the design operating point, the
above cryogenic unit would be capable of supplying 1.10 kg
                               76

-------
 oxygen/kg BOD removed at the design oxygen utilization rate of
 90 percent and an effluent soluble BOD concentration of 10 mg/1.
 This value is entirely consistent with the experience during the
 demonstration project.  The back-up liquid oxygen supply would
 be used to meet diurnal oxygen demand peaks above 171 metric
 tons/day (188 tons/day).

      Although years of testing and design improvements have
 corrected the ti>s-chanical problems and significantly improved the
 performance efficiency of the Pressure Swing Adsorption (PSA)
 oxygen generation system relative to the experiences with the
 early version of this unit tested in the Newtown Creek demon-
 stration,  the magnitude of the oxygen requirements  for a full-
 scale upgrading at Newtown Creek  make use of today's version of
 the PSA system economically impractical.   It is  for this reason
 that the larger capacity cryogenic oxygen generation system is
 included in this cost estimating  exercise.

      The installed power of the oxygen supply system,  including
 that for liquid oxygen vaporization,  would  be 2610  kW (3500 nhp)
 at 2300 volts.   Adding the above  specified  connected dissolution
 power plus  37 kW (50  nhp @ 480 volts)  for miscellaneous  power
 needs,  the  total installed power  is  estimated at 4317  kW (5790
 nhp) .

      By way of  comparison to  the  Newtown  Creek demonstration
 oxygen system which, produced  a power  efficiency  at  or  above
 design loadings of 0.95  kWh/kg BOD removed  (0.58  nhp/lb  BOD),
 the system  described  above for the proposed  upgrading  at Newtown
 Creek would have an overall power  efficiency on  the basis  of
 installed power and,  assuming  an  effluent total  BOD of  20  mg/1,
 of  0.81 kWh/kg  BOD removed (6.49  nhp/lb DOD).  This represents
 a  projected efficiency improvement over  the  demonstration
 system of approximately  15 percent at design loadings  and  is
 the result  of improvements in  oxygen  dissolution  technology
 over the last 7-8  yr  and  the  use of  the more efficient cryo-
 genic  oxygen generation  system.   It  should further  be  noted that
 the actual  line operating  power draw  at design conditions  for
 this  system would  be  approximately 4  to 5 percent less than the
 installed nameplate power  ratings  of  the  equipment  previously
 discussed.

     Based  on the  past oxygen  system  demonstration  experiences
 at  Newtown  Creek,  it  is anticipated that  the  return  sludge  sus-
 pended  solids concentration for the proposed  system would  average
 about  15,000 mg/1.  At an  assumed  return  sludge f.ow equal  to
 40  percent  of the  influent  flow, and  MLSS concentration  vould
 approximate  4285 mg/1.  During the demonstration project,  the
 volatile fraction of  the mixed liquor  suspended solids averaged
 81  percent.  Due to the decreased  strength of Newtown Creek's
wastewater  since addition of the Manhattan sewage,  it is possible


                               77

-------
^  ^          UNITED STATES ENVIRONMENTAL'PROTECTION AGENCY


    •*'•••-.      .    '       "        •• -         8EHQ-0483-Q475
 OATBi  ADD  O Q IQOO   .      .     '            ..         Page 1 of 4
      lU IV  £• J lijV^sJ
    status Report*  8EHQ-0483-0475              Approved .

                /"V,  I                          Revision
MOHt Justine L. We^c^f/Wsam Leader          .      Needed
    Chemical Selepfion and Profiles' Team/CHIB             ..
                                                                   t


                                                           /jflr   \
  TOi Frank  D.  KoveV,  Chief      •"'••'.'
     Chemical  Hazard  Identification Branch/AD


     Submission  Description

     The  Eastman Kodak  Company submitted a March 2, 1983, interim
     summary report entitled  "Inhalation Teratologies! Potential of
     Ethylene  Glycol  Monobutyl Ether  [EGBE; 2-butoxyethanol] in -the
     Rat."  Eastman Kodak reported that the stuuy is being conducted
     under  contract for the Chemical Manufactures Association (CMA)
     and .is being sponsored by the Glycol Ether Program•(GEP) of which
     the  Tennessee Eastman Company, (a division of the.Eastman Kodak
     Company)  is a member.  In its submission, Eastman Kodak noted
     that the  data contained  in the interim report "have not been
     subjected to .Quality Assurance and are incomplete since fetal
     skeletal  examination and statistics have not been finished."

    According to the submitted interim report, 4 groups  of 30 mated
     female Fischer 344 rats were exposed via inhalation to EGBE vapor
    concentrations of  0, 100, 200, or 300 ppm for 6 hours per day on  .
    gestation days (GD) 6 through 15.   In addition,  the interim
    report presented the following summarized clinical.observations
    and  results of examinations performed as of March 2, 1983:

       "Gestation Body Weight Changes;  Gestational body weight gains
        of animals exposed to 300 ppm were significantly depressed
         (compared to controls) from GD 6-21.   Significant reductions
         in body weight gains (compared to controls) were also present
         in the 200 ppm group from GD. 6-15 and in the 100 ppm qroup
         from GD 6-12.".

        Gestational Food Consumption;  Food consumption  was reduced
        during the dosing period in all groups exposed to EGBE.  Sig-
        nificant reductions in food consumption (compared to controls)
        were noted in the 300 ppm group from GD 6-15, in the 200 ppm
        group from GD 6-12, and in the 100 ppm group from GD 6-12'.
      .  "Animals in the 300 and 200 ppm groups had  a significant in-
        crease in' their food consumption (compared to controls) from
        the end of exposures (GD 15)  until sacrifce (GD  21).



      *NOTE:   This status  report is  the result of  a preliminary
      staff'evaluation of  information  submitted to EPA.   Statements
      irade  herein are  not  to be regarded as expressino final
      Agency policy  or intent with respect to this particular
      chemical.  Any review 6f the status report should  take into
      consideration  the  fact that it may be based on  incomOrete
      information.
                                  ,      ^                    000015

-------
^ • -  • •                              •              8EHQ-0483-0475         ^
* "  -      -                                        Page 2 of 4
•'• - >                       \.

    Gestational Water  Consumption;  Only  animals exposed  to  300
    and 200 ppm had significant reductions  in water consumption.
    Those exposed  to 300 ppra  consumed  less  water than controls
     from GD 6-12.  Animals in the  200  ppra group consumed  less
    water than controls in the periods GD 6-9 and GD 12-15.
    Water consumption  prior, to the  exposure segment of  the study
    and following  exposures were similar  in all groups.

    Maternal  Clinical  Observations;  Exposures to EGBE  resulted
     in a dose-related  increase in  the  frequency of signs  indica-
     tive of hematuria.  These signs included red fluid  on cage
     trays, and urogenital wetness,  discharges and encrustations
     of red and/or  black color. In addition, animals exposed to
     EGBE were hypoactive during the exposure segment of the  study
     when compared  with controls.
                                             *
     Maternal  Organ Weights;   The weight of  the uteri of animals
     exposed to 300 ppm was significantly  lower than those of con-
     trols.  This reduction in uterine  weight is associated with
     the high  degree, of embryo and  fetal lethality present at this
     exposure  level*

     Maternal  Uterine and Ovarian Examinations;  Exposures to
     EGBE, particularly at the 300  ppm  level, resulted  in a marked
     increase  in embryo and fetal lethality  manifested  by resorp-
     tions of  concepti.  Exposures  to 200  ppm produced  a^more
     moderate  increase  in resorption when  compared  to controls,

     Fetal Visceral Examinations;   Exposures to EGBE resulted in  a
     dose-related increase  in  fetal atelectasis  [the  incomplete
     expansion of the lung(s)  at birth].   In addition,  fetuses
     from groups exposed to EGBE had ventricular  septal defects,
     absent innominate  arteries, and severely shortened innominate
     arteries."

In addition to the March 2, 1983,  interim report,  the  Eastman
Kodak Company provided the  following background  information;

    "Nelson _et^.al. at  the National Institute  for Occupational
     Safety and Health  (NIOSH) studied  the teratogenic  potential
     of  three  glycol  ethers  in rats; 2-biitoxyethanol  (EB) , 2-meth-
     oxyethanol  (EM), and 2-ethoxyethyl acetate  (EEA).   They  found
     that EM and EEA  were teratogenic,  while 2-butoxyethanol  did
     not produce significant embryofetotoxicity.   The  exposure
     concentrations of  2-butoxyethanol  were  150  to 200  ppm and
     Nelson et^ al^ reported  that these  concentrations  were diffi-
     cult to generate  (vapor pressure  of EB = 0.6  mm Hg at 20°C).
     Maternal  toxicity  was  evident  at  both dose  levels  and consis-
     ted of hematuria onl;r  after the first exposure.   No other ad-
     verse effects' were seen  in the dams exposed  to either level.
     No major  skeletal  or  soft tissue  malformations were  seen at
     150 or 200 ppm of  2-butoxyethanol  and the  incidence of common
     skeletal  variants  and  minor soft  tissue anomalies seen  in the
     treated groups were comparable to the controls.   Potential


                                                              000016

-------
 •£/--"'.                      -       •            8HQ-0483-0475          /
»v  -                                                Page 3 of 4

     reproductive effects of 2-butoxyethanol and other glycol
     ethers were studied in male  rats in [the submitter's]  labora-
     tory and in male mice by Nagano jst^ al^ in Japan.   Administra-
     tion was by gavage five times per week.  In the  former, doses
     from 222 to 885 mg/kg/day,  and in the latter, doses  from  250
     to 1000 mg/kg/day, did not produce testicular effects."

 Finally, Eastman Kodak noted that the following factors  should be
 considered by EPA in assessing  the CMA/GEP-sponsored inhalation
 teratology study of 2-butoxyethanol in rats: "the severe maternal
 toxicity produced,  the lack of  a dose-related response and the
 low  incidence of effects seen in the [CMA/GEP]  study, as well as
 the  negative results from the NIOSH study, the  known toxicity of
 2-butoxyethanol in adult male and non-pregnant  female rats, and
 [the chemical's]  vapor pressure."

 Submission Evaluation

 Although the submitted findings  indicate that 2-butoxyethanol did
 produce some degree of maternal  tibxicity in the CMA/GEP-sponsored
 teratology study, EPA does not  be'lieve that 2-butoxyethanol pro-
 duced "severe" maternal toxicity in the study.   One  of the most
 common major manifestations of  severe maternal  toxicity  in this
 type of study is a significant  weight change (usually seen as a
 decrease) in exposed versus control dams.  The  summarized data-
 that are presented in Table 4 (which contains measured maternal
 organ weights and "corrected" maternal body weights  (i.e., the
 maternal body weight minus the  weight of ths uterus  and  its
 contents)), indicate that there  were no significant  changes in
 the  corrected body weights of exposed dams when compared to the
 corrected body weights of control dams.  There  was,  however,  a
 significant decrease found in the uterine weights of dams exposed
 to 300 ppm 2~butoxyethanol when  compared to controls.  Stated in
 another way, the apparent decreases in maternal body weights  of
 dams exposed to 300 ppm 2-butoxyethanol are due primarily to  the
 decrease in the weight of the uterus and its contents.

 In order for EPA ho more properly evaluate the  significance of
 the  embryo/fetotoxic effects (including abnormalities) observed
 .1-n the CMA/GEP-sponsored inhalation study of 2-butoxyethanol, a
 complete copy of the final report (including protocol(s), data
 and  the results of performed statistical analyses) should be  ob-
 tained.  It should be noted at  the present time, however, that
 the  embryo/fetotoxic effects observed in the CMA/GEP-sponsored
 study (although in apparent contrast to previous findings), are
 consistent with the adverse developmental effects found in labor-
 atory animals exposed to two structurally related chemicals:  2-
 methoxyethanol and 2-ethoxyethanol.

 Current Production and Use
 A  review of the production range (includes importation volumes)
 statistics for 2-butoxyethanol (CASJ No. 111-76-2), which is
 listed  in the initial TSCA Inventory, has shown that between 31
                                                               000017

-------
Jr .    " -                                           8EHQ-0483-0475
" "k                          '                      Page 4 of 4

 million and 161 million pounds of this chemical were reported as
 produced/imported in 1977.  This production range information
 does not include any production/importation data claimed  as con-
 fidential by the person(s) reporting for the TSCA Inventory, nor
 does it include any information which would compromise Confiden-
 tial Business Information (CBI).  The data submitted for  the TSCA
 Inventory, including production .range information, are subject to
 the limitations contained in the Inventory Reporting Regulations
 (40 CFR 710).

 2-Butoxyethanol is used as a solvent for nitrocellulose resins,
 spray and quick-drying lacquers, varnish and varnish removers,
 enamels, and drycleaning compounds.  The chemical is also used
 for preventing spotting during the printing and/or dyeing of
 textiles and as an ingredient in certain pesticides.

 Comments/Recommendations

 EPA's Office of Toxic Substances (OTS) has received and evaluated
 several Section 8(e) and "For Your Information (FYI)" submissions
 concerning various glycol ethers.  The Chemical Hazard Identifi-
 cation Branch (CHIB/AD/OTS) has prepared CHIPs (Chemical Hazard
 Information Profiles) on 2-methoxyethanol, 2-ethoxyethanol, and
 their acetates.  In addition, Priority Review Level-1  (PRL-1)
 documents on 2-methoxyethanol and 2-ethoxyethanol have been pre-
 pared by the Health and Environmental Review Division  (HERD/OTS).
 At present, the OTS "Existing Chemicals Task Force  (ECTF)"  is
 considering various EPA options with regard to chemicals within
 the class of .glycol ethers.

    a) The Chemical Hazard Identification Branch will request  the
       Eastman Kodak Company to submit, when available, a complete
       copy of the final report from the CMA/GEP-sponsored inhala-
       tion teratology study of 2-butoxyethanol in rats.  The  sub-
       mitter will also be requested to provide a complete copy of
       the final report (including test protocols and data)  from
       the Eastman Kodak study reportedly conducted  to determine
       potential reproductive system effects of 2-butoxyethanol
       administered to male rats by gavage five (5)  times por  week
       at doses ranging from 222 to 885 mg/kg/day.

    b) In view of EPA's general interest in company  actions  that
       are taken on a voluntary basis in response to chemical  tox-
       icity/exposure information, the Chemical Hazard Identifica-
       tion Branch will request the Eastman Kodak Company to des-
       cribe the actions it has taken to warn workers and others
       and to reduce and/or eliminate exposure to .2-butoxyethanol.

    c) The Chemical Hazard Identification Branch will transmit a
       copy of this status report to NIOSH, OSHA, CPSC, FDA, NTP,
       0/..NR/EPA, ORD/EPA, OSWER/EPA, OW/EPA, OPP/OPTS/EPA, and the
       OTS "Existing Chemicals Task Force  (ECTF)."   A copy of  this
       report will also lie provided to EPA's Industry Assistance
       Office (IAO/OTS) for further distribution.
                                                               000018

-------
that the volatile fraction might drop to as low as 75 percent
in a full-scale system.  The MLVSS concentration  for design
purposes is, therefore, assigned a value of 3215  mg/1  (75
percent of MLSS),  Using the above assumptions, expected oxygen
system operating conditions are summarized in Table 20  for a
design flow of  13.4 m3/sec  (307 mgd) and a design BOD loading
of 150,980 kg/day  (332,850 Ib/day).  All other process  design
parameters except as mentioned above are consistent with process
performance experiences during the Newtown Creek  demonstration
project.

        TABLE  20.  DESIGN OPERATING  CONDITIONS  FOR  FULL-
                   SCALE NEWTOWN  CREEK  OXYGEN  SYSTEM
Oxygenation Tank Detention Time
     Based on Q  (hr)                               1.35
     Based on Q + R  (hr)                           0.96

F/M Loading  (kg BOD/day/kg MLVSS)                  0.72

Volumetric Organic Loading
      (kg BOU/day/m3)                               2.31
      (Ib BOD/day/1000  ft3)                         144

Secondary Clarifier  Overflow  Rate
      (m3/day/m2}                                   36
      (gpd/ft2)                                     872

Sludge Wasted
     Based on Figure 8 (non-filamentous
     curve)  and assumed  effluent  sus-
     pended  solids of  20 mg/1
           (kg/day)                                 94,350
           (Ib/day)                                 208,000

Sludge Retention Time
     "Based on Figure 8 (days)                      2.4

Average  Mixed Liquor DO  (mg/1)                     6

Average  02 Utilization Efficiency (%)              90

Design Oxygen Supply  (metric  tons/day)             171
                       (US tons/day)                 188

Effluent BOD (mg/1)                                20

Effluent Soluble  BOD  (mg/1)                        10

Effluent Suspended  Solids (mg/1)                   20
                                 78

-------
ESTIMATED CONSTRUCTION AND CAPITAL COSTS

     The estimated construction cost of converting the Newtown
Creek plant to oxygen is $44,000,000.  Adding anticipated fees
for engineering, legal, fiscal, and administrative services and
interest over an assumed construction period of 2 yr, the
estimated capital (total project)  cost becomes $54,335,000.  At
a design flow of 13.4 m^/sec (307 mgd), this capital cost is
equivalent to $46.76/daily m^  ($0.10/daily gal) of upgraded plant
capacity.  The above estimate,  which is applicable to the fourth
quarter, 1977, and includes provisions for major site work and
improvements to existing plant grit removal, clarification, and
sludge recycle facilities in addition to oxygen system equipment,
installation, and retrofit costs,  is broken down by cost element
in Table 21.

          TABLE 21.   ESTIMATED CAPITAL COST FOR OXYGEN
                     SYSTEM RETROFIT AT NEWTOWN CREEK


Oxygen Dissolution Equipment                      $ 4,375,000
                   Installation                       485,000

Oxygen Supply Equipment                             3,225,000
              Installation                          1,025,000

Site Work (including pilings)                       3,000,000

Aeration System Retrofit Modifications             16,000,000

Secondary Clarifier Modifications                   6,000,000

Grit Chamber Modifications                          2,890,000

New Sludge Recycle Pump Station                     3,OOP , OOP

                    Subtotal                       40,000,000

Contingency @ 10%                                   4,000,000

     ESTIMATED CONSTRUCTION COST                  $44,000,000

Engineering, Legal,  Fiscal,
  Administrative 9 16.5%                            7,260,000

                    Subtotal                       51,260,000

Interest During Construction @ 6% for 2 yr          3,075,000

     ESTIMATED CAPITAL COST                       $54,335,000
                                79

-------