ORP-81-1
      ADVANCED
              FOR
       RADIUM REMOVAL
        ^    FROM
       DRJNKING WATER:

THE FLATOMINEATER TREATENT PROJECT
       Division of Occupational Health
          cifid Radiation Control
        Texas Deportment of Health
             Austin, Texas

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Page Intentionally Blank

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THE FLATONIA WATER TREATMENT PROJECT


                          for
  U,S»
         Division of Occupotlonoi Health
             end Radiation Control
          Texas Deportment of Health
                Austin, Texas
                      i-c

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Page Intentionally Blank

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                     Advanced Technology for Radium Removal from




                                  Drinking Water:




                       The Platonia Water Treatment Project




                                   Lewis M. Cook




                            Texas Department of Health






                                I,  Introduction






In late 1977, the Texas Department of Health received a grant from the U.S.




Environmental Protection Agency (EPA) to conduct a study to determine the




applicability of using manganese-coated acrylic fibers (Mn-fibers)  to remove




radium from drinking water.  The project also had as its goals the reduction of the




levels of radium-226 in the municipal water system of Platonia, Texas.  Platonia




(Figure 1), a small (population 1,108) town on Interstate 10 approximately mid-way




between Houston and San Antonio in southeast Texas, depends entirely on ground water




(well water) for the municipal supply.  Three of the four wells in the water system




exceeded EPA's limit of 5 picoCuries total radium per liter (pCi/1) for drinking




water and two of those exceeded it substantially.  About the time the project was




begun, the city drilled another well to augment the system because the well having




the lowest level of radium had failed.







During the course of the project, some of the objectives had to be changed, due to




changes in water useage, philosophy, and waste-generating and disposal requirements.







One of the goals was to remove the radium from the filters so that the filters




could be re-used.  This was not attempted for several reasons.  The removal of radium




requires that the filters be immersed in Nitric acid, and the acid, containing fairly




high dissolved and suspended radium  concentrations,would require disposal in liquid




form.  Since waste disposal facilities no longer accept liquids for disposal, and

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Figure 1.  Business district. North Main Street, (U.S.  90), Flatonia,
           located in Fayette County, Texas.

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the fact that it was thought that the handling of large volumes of liquid radio-




active waste was not a task compatible with the operations of a municipal utility




crew, this part of the proposed project was not attempted.






Despite the many problems encountered, problems which ranged from tangled red tape




and logistics to bad luck that could only be termed bizarre, and despite the numerous




delays and modified objectives, a great deal of information about the process was




gained and the project was technologically successful.  The water supply in Flatonia




met the drinking water standards for radium for almost all of 1979 for the first time




in several years.







From the knowledge gained performing this work, we have concluded the technique of




using Mn-fibers to remove radium from drinking water appears to be a relatively




simple, effective procedure which can be compatible with the operations of a




municipal utility crew and probably will operate at an economic advantage over




other methods.

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                                  II.  History







The Texas Department of Health began routine sampling of water near uranium




deposits in 1970.  Private wells near these deposits have been found to deliver




water containing over 100 pCi/1 of radium-226 to the families using this water.




The work was first reported at the Natural Radiation Environment II Symposium




{Wukasch and Cook, 1972), and was further discussed at an International Radia-




tion Protection Association Symposium in Washington, D.C. (Wukasch and Cook,




1973).






A W_ashi_ngtpri Post story summarizing the paper came to the attention of W.S.




Moore, Ph.D., who  contacted  us.







Moore, at the time, was working with the U.S. Navy Oceanographic Office, and




was examining the ratios of radium-226 to radium-228 in the oceans to determine




oceanic vertical mixing rates.  Because the concentration of radium in ocean




waters is quite low (on the order of 0.05 pCi/1) it was necessary to concentrate




the radium from large volumes of sea water in order to have sufficient quantities




of radium to determine this ratio.  The removal was done with acrylic fiber




filters which had been treated with manganese solutions.  Radium removal effi-




ciencies were on the order of 90% (Moore and Reid, 1973).  Within a month, Moore




had brought an  experimental apparatus to Texas at our request, to determine if the




process would reduce the high levels of radium being found in some well water.




It did (Moore and Cook, 1975).






About the same time, we were notified that gamma ray well logs of wells in

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Flatonia showed extremely high levels of gamma ray intensity in the (Miocene




or Oligocene Series) Catahoula tuff (Hill, 1973).






The Catahoula tuff is a host rock for uranium deposits in other parts of South




Texas (Cook, in press), and uranium exploration in the near vicinity of the town




had been conducted.  No plans for commercial operation had been announced,




however.






Water sampling showed that all of the wells in the Flatonia municipal water




supply contained detectable levels of radium and radon (Table I).   Well locations




are shown on the map of the town in Figure 2.







In August of 1974, Moore and the writer performed tests using the process on




water from well #6 in Flatonia, similar to those done in South Texas in 1973




(Figure 3).  In February 1975, other variations of the process were also tested




with encouraging results.






In order for the city water supply to meet the drinking water standard, it




would be necessary for the city to either abandon the present wells and drill




new wells, gambling that those wells would have acceptable radium levels,




or the city could treat the water from the wells to reduce the radium content.






when the costs of drilling new wells were compared to the projected costs of




treating the water by passing it through Mn-fibers, it was decided that  a potential




for substantial savings lay in using the fibers.







The process was an experimental one, and if it could successfully be scaled




up to water-treatment plant size, then other communities which have problems

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                                 HIGHWAYS REVISED TO  JANUARY 1, 1976
Figure  2.   well locations  in  Flatonia,

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                         Y*#

Figure 3.  Bench scale tests of the process were conducted in Platonia
          using 10 inch length filter cartridges.  30 inch length filter
          cartridges are used in the housing in Flatonia,

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                        Table 1




Radium and Radon in the Flatonia Municipal Water System
Radium-226
(pCi/1)
Well
Well
Well
Well
5
6
7
8
3.4
16
14
6.4
( 3)
(13)
( 4)
( 3)
Radon -2 2 2
(PCi/1)
1300
10700
7400
1400
(1)
(15
(1)
(1)
   Numbers in parentheses are number of samples.

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with high radium levels in their drinking water would berefit from this new




technology.






It was thought that development of such a process would logically be of interest




to the EPA, so contacts with EPA were made and in September of 1977 a proposal




for the Flatonia Water Treatment Project was submitted.  A cost-reimbursement




contract was subsequently issued.






The proposal entailed participation of three governmental entities:  EPA, the




Texas Department of Health, and the City of Flatonia,  The EPA provided money




for the purchase of equipment and suppliess consultation fees and interstate




travel.  The Health Department paid the salaries of the principle investigator,




his assistant, and paid for laboratory services and intra-state travel.  The city




of Flatonia furnished the work space, people and equipment for installation of




process equipment and sample collection as well as work space in Flatonia,  W.S,




Moore, who holds U.S. patent numbers 3,965., 283  and 4,087,, 583  on the fibers




and their preparation, allowed this technology to be utilized on a royalty-




free basis.

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                         III.  Operations Conducted.






The Mn-fliter preparation area was constructed in the fall of 1977 in anticipation




of using the area as a filter regeneration facility.  Accordingly, an emergency




shower was also installed, as was an extra large capacity (about 2,000 liters)




spill absorption and containment "tray" in the bottom of the work area.   Vermi-




culite was used as the absorber,  (Figure 4)







The filter housing foundation for the south plant area was placed near the buried




water lines leading to the elevated ground storage tank on the south edge of




town,  (Figure 5).  The lines from well 6 and well 7 connect just to the west




of this area.







Well 9 was drilled and developed and was connected into the vertical riser pipe




at the tank.  This routing was chosen so that the water from wells 6 and 7 could




be routed through the filter and the water from well 9 could be put into the




system without being sent through the filter.  The pipe from well 9 to the tank




crosses the feed pipe from well 6 near well 9, and had the radium removal equip-




ment not been in the system, there would have been a connection at the point where




the well 9 output pipe crosses the well 6 pipe.  The length of pipe necessary




to extend the well 9 connection to the tank was supplied to the city under




this project.






The filter housing was installed in the Flatonia system about one year after




the foundation was prepared, due to difficulties discussed elsewhere in  this




report.

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Figure 4,  The filter preparation area was to be used for filter prepa-
           ration and regeneration.  The use of 2 x 8 lumber provided
           a sturdy platform for the drums, which weigh about 500 pounds
           each when full.

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Figure 5.   Location for the South Water Treatment Plant,
                               14

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The foundation (6' x 6' x 9") was constructed in December 1977 of reinforced




concrete (Figures 6 and 7).   This proved to be larger than strictly necessary but




provided a comfortable work area.






After the filter housing arrived, the plumbing was connected.  Difficulty in




cutting cast iron pipe was encountered.  Since the mechanical joint pipe fittings




required nipples between adjacent fittings, small pieces of the pipe were needed.




A hydraulic pipe cutter (Figure 8} was used, but failed to cut the pipe.  The




pipe, instead of fracturing like case iron does, merely deformed under the pressure.




The pipe was supposed to have been cast iron but a well-intentioned contractor




had substituted a stronger, less brittle pipe.






The city crew supplied a small piece of cast iron pipe for some of the needed




fittings and the mild steel pipe was used for the rest.  The city crew took the




pipe to Prototype Machine Shop, where it was cut into lengths using a band saw




(several bands were used in the attempt).  No charge was levied for this service.






The city crew also dug up the buried water line and made the hook-up.






In the meantime, filters had been treated.  Figure 9 shows the beginning steps




and Figure 10 shows 60 treated filters.  The surgical gloves used to protect




hands proved to be not sufficiently durable.  Stains from the permanganate last




a few days to a week before they wear off.  The solutions, when spilled on the




skin, do not cause pain (Figure 11).






The filter housing hardware was installed  (Figure 12), the filters inserted,




and the spring and cap assemblies were joined and pushed onto the filter tops




(Figure 13).  Next the hold-down plate was installed, the head bolted down,

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                                                  If
Figure 6.   Constructing the form for the foundation of the  South Water
           Treatment Plant.
                                16-

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Figure 7.  The finished form.

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Figure 8.  Problems were encountered in cutting pipe supplied under
           contract.  The supplied pipe was not cast iron but a more
           durable and stronger, mild steel.  The hydraulic pipe cutter
           operates only on brittle pipe.

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Figure 9.  Filters at initial chemical addition step.

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Figure 10,  Filters at end of treatment.

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Figure 11,  Manganese stains result when holes develop in gloves.  The
            stains cause a short-term discoloration, are painless and
            should remove radium from water.

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                                                                    . *«i*s;
Figure 12.  Installation of "V"  shaped filter  guide bars.  Note circular
            hold-down plate which is used to compress  filter springs.
                                 22'

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and  testing was begun  (Figure 14).







Tests for chemical changes in the water before and after it passed through




the  filters included radium removal, presence of acrylonitrile and/or other organic




chemicals as well as routine chemical analyses and taste and odor  (Table II & Figure




15).  The treated water was dumped on the ground during this early data gathering




period between the Initial installation and receipt of laboratory results indicating




acceptable quality water was delivered.







Prior to the beginning of the tests, cards were mailed to the customers of the




utility, briefly describing the project and requesting notification of any com-




plaints.  A few complaints were received concerning aestnetic quality of the




water prior to the time that any water was treated by the filtering system.




After the system was connected, no complaints related to the operation were




received.  The card is shown in Figure 16.







The radium removal efficiency was substantial, but less than expected.  As a




result, the treated water was added to the system only when needed after the




initial trial run.







In June 1979, the filters were exchanged with a new "batch to test several




theories about the process, which will be discussed in detail later in this




report.  At that time, most of the interior of the filter housing were painted




with epoxy paint.






The second filter housing is to be installed at the downtown water plant




(Figure 17).  The city warehouse just to the west of this plant is shown in




Figure 18.   It is in this building that our filter preparation area is housed.

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                                     Table II

                           Chemical  Tests  - well  6  water
Test
Calcium
Magnesium
Sodium
Carbonate
Bicarbonate
Sulphate
Chloride
Fluoride
Nitrate
Potassium
Dissolved Solids
Phenolphthalein
Alkalinity as CaCO
Total Alkalinity as CaCO-,
Total Hardness as CaCO3
Diluted Conductance
(ymhos/cm)
pH
Before
Filter
108
4
67
0
346
24
81
0.4
< 0.02
NA
454

0
284
285
870
7.6
After
1000 gal.
88
4
61
0
336
23
79
0,4
< 0.02
29
449

0
275
233
B64
7.5
After
4000 gal.
92
3
60
0
337
23
80
0.4
< 0,02
24
448

0
276
243
864
7.6
After
8000 gal.
101
4
59
0
341
24
73
0.4
< 0.02
NA
429

0
280
271
852
7.7
Gas Chromatography + Mass spectroscopy test for acrylonitrile and related chemicals
negative.

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Figure 14.  The assembled filter mechanism at the early testing stage.

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Figure 15.   Tests for chemical,  radiological, and aesthetic quality
            were conducted prior to adding water to the municipal water
            system.
                                    27

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                           &OTXCE

The Texas Departmer.t of Health, working ±n cooperation with
the City of Flatonia -with financial assistance from the O. S.
Environmental Protection Agsncy, will bsgla a as** water treat-
ment process in & few tweaks.  After preliminary testing, the
water from some of the City's wells will be passed through
specially treated' filters before being added to the distribu-
tion system.  The filters are spra froa acrylic yarn and
treated with oxides of aoanganese.  They will remove radium,
naturally present in sosas of the well waters, without changing
the appearance or taste of the water.

No problems with the delivered water are expected, however, if
you should have a complaint, please save a sample of the
water and call the City Office at 885-3337.
 Figure 16.

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Figure 1"? .   Downtown water  treatment area  where second filter unit is
             to be installed.
                                  29-

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Figure 18.   The  City Warehouse is shown to the  left of the base of the
            elevated water storage tank.  It  is the location of the
            filter preparation area.
                             30<

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Forms for this second unit foundation have been made, and this will be smaller




than the foundation for the first unit.  The city will conduct the operation of




this second installation and filter operation under guidance and consultation




with the Health Department.

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                     IV.  Logistic Problems Encountered




                                A, Delays




The project was designed to last one year, based upon expected paperwork


delays, manufacturing schedules, available travel money, and manpower.




Belays far exceeding reasonable expectations were encountered.  Reviews of


purchase orders for the filter housings by the Fiscal Division of the Health


Department, followed by a review and bid requests issued by the Texas Board


of Control, bid opening , and the award of contracts required from 8-11 weeks,




Construction of the first filter housing took 22 weeks, although 6-8 weeks


had been the estimate given by the supplier.




That first filter housing actually never made it to Flatonia.  It was destroyed


in shipment when vandals burned the shipping warehouse in Austin on July 27,


1978, as the housing was awaiting forwarding to Flatonia.  In the meantime,


we had ordered the second housing.  We planned to substitute it for the first


housing.  This replacement for the first filter housing didn't arrive in


Flatonia until December 1978.  In early February 1979, the paperwork for the


purchase of the second filter housing was begun.  The delivery of this second
                                                     e

housing occurred on November 16, 1979.  Installation of this second unit is


planned by the Flatonia crew in the spring of  1980.
                                 32'

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                                  B. Materials








Several problems related to materials were encountered during the project.




The treatment of the first set of filters proceeded slowly, much more slowly




than expected.  Two 55-gallon drums were filled with 60 filters for the




treatment procedure.  The drums were lined with polyethylene bags of 6 mil thickness,




which proved to be insufficiently strong to prevent leaks and subsequent corrosive




attack of the steel drum.  Next, for protection of the drums they were coated with an




epoxy paint used for water tanks.  The paint, after drying more than the recommended




curing time, was also attacked by the potassium permanganate.  Finally, drum liners
                   i



made of 1/8 inch thick .polyethylene were lent to us by W.S. Moore, Ph.D., the




consultant, in order that they could be obtained without significant delay.






The filter treatment consists of soaking the filters in a potassium permanganate




solution for lengths of time which depend upon the strength of the solution and




temperature  (U.S. Patents 3,965,283 and 4,087,583).  This reouires about 7-10




minutes at 175°F and a concentration at 60 grams of potassium permanganate per liter




of water.  At 86 F, the processing requires 3 to 4 days, at the same solution strength,






The fibers, in becoming coated with oxides of manganese, turn from pure white




through tati to a chocolate color (at about 4% manganese by weight) and finally




to jet black (at around 10% manganese by weight).  The desired degree of treat-




ment is about 7-8% manganese by weight, resulting in a very dark drown fiber.






On or about March 7, 1978, before the filters were delivered, a phone conver-




sation was held with the contractor, • who was informed of the need for acrylic

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fiber filters, and that any other substance would not work.  The contractor




stated that he had acrylic fiber filters and another type, a polyurethane,




in stock, that the polyurethane was slightly more expensive and it would be




supplied at the same price, if desired.  This suggestion was rejected, again




with the admonition given that only acrylic fibers were acceptable.









On March 29, 1978, 42 boxes of 12 filters each were delivered to Flatonia.




The filters were inspected and appeared acceptable, being the correct length




and diameter, being made of white fibers spun onto 1" plastic centers.









Immediately, 60 filters were placed in a drum containing a solution of potassium




permanganate (40 g/1).









On March 31, a check on progress of the filter treatment was conducted.  The




temperature of the unheated drum was 72°F and the degree of manganese loading




on the fibers was estimated to be less than 1%.  On April 5, a drum heater was




connected to a second drum filled with water and another 60 filters to determine




heater settings.









On April 6, heaters were connected to both drums and chemicals were mixed for




treatment of all the 120 filters, enough for one filling of the filter housing




plus five for testing.









On April 7, the manganese level of the filter was checked.  Again less than 1%




manganese by weight was deposited on the filter.  Because of possible inter-




ference caused by the epoxy coating on the drums by the chemicals, processing




was suspended by draining the chemical solution and leaving the filters to stand




in water,

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Upon receipt of loaned polyethylene drum liners, processing was resumed on




May 2, 1978.
Then, 60 of the filters were placed in a drum with about 20 grams of




per liter, heated to 83°F.  On May 4, the temperature was increased to 93°P by




Flatonia City workers.  On May 5 the fibers had 1-2% manganese by weight,




estimating from the color.  The solution strength was increased to 40 grams




per liter and the temperature increased to 98°F to speed the seemingly slow




uptake of manganese .









By May 8, the fibers still had not absorbed more than 2% manganese by weight,




so the solution strength was increased to 60 grams per liter, the "reference"




strength, and the temperature was kept at 98°F.









On May 9, the city recorded the temperature as being 103 F, and it was left at




that warm temperature until May 12, by which time it was anticipated they would




have been treated to 7 - 10% manganese by weight.









The fibers actually contained less than 3% manganese.  The drum heater was




disconnected.  A sample of 100% orlon acrylic  (white) yarn was obtained to




compare it with those being used in Flatonia.  Part of one of the unused Flatonia




filters was unwound and 3.8 gram bundled sample of each type of yarn was taken,




They were dropped simultaneously in a heated solution of potassium permanganate




solution at approximately 50 grams per liter at 180 F.  They were stirred inter-




mittently and removed together after 7 minutes in the hot potassium permanganate




solution.  They were then placed in a beaker and washed until no trace of the




purple solution remained.





                                    35 <:

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Because of the differing winding of the yarns, there was no possibility of con-




fusing the two samples.






The orlon acrylic yarn reacted exactly as expected, turning jet black.  The




sample from the filter delivered to Flatonia reacted differently,







The degree of darkening on it was very much less than the orlon acrylic.   The




final color on this sample was beige, representing much less than 1% manganese




by weight.







The consultant for the project, Willard S. Moore, Ph.D., the developer of the




treatment process, was called and he- reported having tested numerous acrylic




fibers manufactured under differing processes and had never found an acrylic




fiber which failed to take up manganese oxides.







As a final test, the vendor's filter material was heated to between 170 ^ a°d




190° F in the same solution used for the simultaneous test for over one hcur




and did not darken significantly more.






It was therefore concluded that the filters delivered to Flatonia were something




other than the spun acrylic fiber filters specified.   Laboratory tests for infra-




red reflectance spectrometry confirmed the discrepancy.







                        C.  State Budgetary Process




It should be briefly mentioned that these were significant delays due to  the




somewhat complex purchasing system the State of Texas uses.  No "petty cash"




system existed, so for relatively small items which were needed quickly (in a few




minutes rather than several days or weeks) the investigators purchased these with




personal funds.  Examples include extension cords, small springs, and bleach




(for disinfecting).

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                              V, Water Treatment






                      A.   Radium Concentration Variations






Earlier testing of the activity of well 6 gave consistent results of around




14 pci/l.  During this earlier period, well 6 provided most of the water used by




the town.  At that time the town used wells, 6, 8, 5, and 7 for their supply,




approximately in that order when volume is considered.  Well 5 failed in 1977




and another well was drilled, well 9A.  This new well did not produce the quan-




tity that the driller had guaranteed, and another well, numbered 9B, was drilled




by off-setting well 9A.  This offset produced over 250 gallons per minute, a




greater production rate than any other well in the system.  It plus well 8




is sufficient to provide most of the water needed by Flatonia all during the




fall, winter, and early spring, but demand during the summer requires all of the




wells in the system.






When well 6 was turned on at the beginning of the project in December of




1978, the concentration of radium in the water was 38 pCi/1.  Heavy pumping




caused the concentration to drop to 20 pCi the next day,  A similar pattern




of activity was seen in June of 1979 after the second set of filters was installed




and was used for treating the town's water in the summer.






Apparently, the most highly contaminated water is drawn  from near the




well, and water more distant from the well has less activity.  After the




well is shut down, the radium levels climb once again to around 35 -
                                      37 <

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40 pCi/1.  After continued heavy use, the radium levels decreased to around




the levels originally measured, around 14 pCi/1.






Well 7 showed a little variation also.  The levels of radium in well 7 seemed to




increase slightly with pumping.






                      B.  Description of Filter Housing




The filter housing used in this project is a Facet Model 115R3, a cylindrical




steel pressure vessel-  about 36 inches in diameter and standing about seven




feet tall.  The filters are 30 inches tall, and are arranged in a concentric




circular pattern, with a "wedge" of filters missing on the outer rows to accom-




modate the inlet.  The filters fit over "cups" with steel "V" channel guide bars




inserted to hold the filters upright.  The guide bars are removable and fit very




loosely into the cups.  The filters are held upright and vertical by a spring




and cap assembly fitted into the top of the filters.  A \ inch thick circular




steel plate, about 2 inches in diameter less than the inside diameter of the




vessel, is bolted down over the springs, the springs being compressed, thereby




holding the filters in place.  This hold-down plate has a circular hole which




is aligned above the intake.  The doomed top of the housing is held on with




swing belts and sealed by a rubber "0" ring.  The vessel is rated for 150 psig,




with a maximum differential of 75 psig between the inlet and output.







The water flows into the housing at a level below the bottom of the filters,




and rises in the empty "V" space above the inlet.  From this point, it can




pass among the filters and be filtered, or can rise and flow through the springs




and down between the filters.  Alternatively, the incoming water could flow up




through the hole in the hold-down plate, then around the edge of the hold-down




plate to the area between the tops of the filters and the plate, in the space where

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the compressed springs stand.









The water passes through the filter, from the outside into the center hole of




the filter and then down through the tube and through the 115 holes in the




bottom of the filter chamber.  The outlet for the housing is opposite the intake.




The housing has a drain pipe on the bottom, which can be used for sampling, as




a "bleed" or as an alternate output at relatively low flow rates (less than




150 gallons per minute), permitting dumping of the filtered water.









                          C.  Results and Problems






The initial filter loading and tests in early December 1978, achieved a large




reduction in the levels of radium in the water passed through the filter.




Treated water was dumped on the ground until analysis results were received




from the Health Department laboratory which showed an absence of any organic




chemicals from the filtered water which could have come either from the manu-




facturer of the acrylic fiber of the chemical treatment in Flatonia.  Even




after heavily concentrating the sample, no traces of any chemicals attributable




to the filter could be detected using gas chromatography and mass spectroscopy.









After the negative report on the presence of organics was received, and analyses




for radium showed that radium levels were below 5 pCi/1 for the commingled




water, the filter output was put into the system.









Apart from this early work to prove that the process worked, the filtered water




was added to the system only when it was needed to keep up with demand.









Well 9 was out of service for a few weeks in January 1979 and wells 6 and 7




were needed.  During this period the 250,000 gallon elevated ground storage

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tank needed cleaning of the sand and iron sulfide precipitate in it and well 6

was used to flush and fill this tank.



The reason for using well 6 as little as feasible was the fact that the efficiency

of the filter system was not as great as had been expected, and adding the water

that passed through the filter system to the municipal water supply when it

wasn't strictly necessary would be contrary to the ALARA* principle.



Simply dumping the filtered water on the ground was also viewed as wasteful

and was not done except for flushing loose manganese oxides from the filter

system and for the initial testing phases.



The results of the water treatment project with respect to the removal of

radium from the drinking water in Flatonia are shown in Table III.



The initial removal efficiency with the first set of filters was less than

expected.  Earlier work with smaller filters (although with larger flow per

filter) had led to the expectation that initial removal efficiencies approaching

99% could be expected.  The initial radium removal efficiencies were actually

around 80%.  The cause of this low efficiency was speculated to be due to one

of several factors;

                    1.  Possibly uneven manganese uptake by fibers in the
                        middle of the winding of the cartridge's core.

                    2.  "Channeling" through the filter housing.

                    3.  Chemical Interference caused by Iron oxides (rust)
                        in the filter housing.

                    4.  An empty filter space in the housing.

                    5.  Insufficient amount of manganese treatment of the fiber.

*As low as reasonably achievable.
                                  40<

-------
                                       Table III

                               Water Processing Results
                                                           Radium  Concentration
                      Volume
Date
12/05/78
12/06/78
12/11/78
12/13/78
12/14/78
12/18/78
12/19/78
12/20/78
12/21/78
1/18/79
1/19/79
2/06/79
Time (Gal. x 1000)
1500
1000
1230
1330
1530
1205
1305
1405
1505
1406
1416
1446
0880
0950
0950
unk
0745
0845
0935
1300
1340
1050
1230
1330
1320
1335
1350
1
4
8
16
114
123
129
141
255
261
267
273
333
334
337
405
535
535
(877)
991
1123
1249
1252
1256
1278
1290
1304
1962
1964
1965
2/13/79

6/22/79
1055
1120
1140
1300
1966

   3
   6
  • 8
  17
                       Well

                        6
                        6
                        6
                        6

                        6
                        6
                        6
                        6

                        6
                        6
                        6
                        6

                        6
                        6
                        6

                        6
                        6
                        b

                        6

                        6

                        6
 6
 6

6+7
6+7
6+7

 6
6+7
 7

 7

6+7
 6
 7
6+7
Before Filters
pCi/1
38


28
24
19
20
20
26
22
22
23
27
33
25
(27)
(27)
(27)
(27)
(27)
(27)
29
32
40
17
19
20
37
32
17
9.5
27
27
10
22
After Filters
PCi/1
6.7
6.6
3.6
4.0
4.8
7.0
5.9
5.9
7.1
6.3
7.1
7.2
8.7
7.6
6.8
8.2
4.6
4.6
4.4
5.8
9.4
7.0
10.9
10.8
7.5
6.1
5.7
8.1
6.9
0.2
2.0
7,9
4.2
2.1
3.2
                                                                   Radium Remov.
                                                                                      83
86

80
63
70
70

73
71
67
68

68
77
73

70
83
83

84

V8

65

80

66
72

56
68
72

78
79
98

79

71
84
79
85

-------
                                                        Radium Concentration

                      Volume                Before Filters   After Filters    Radium  Removal
 Date     Time     (Gal, x 1000)    Well        pCi/1   	      pCi/jl         	%

7/11/79   1300                       6           19               5.1               73
          1305                       7           18               7.0               61
          1310                      6+7          25               1.1               95

8/09/79   1255        2468           6           16               6.5               59
          1320        2470           6           13               8.3               36

-------
                                      _ 1 —






To test the first possibility, one of the unused filter cartridges was sacrificed




to examine the interior windings of the fiber.  The center tube, a one-inch




diameter perforated tube, allows the solutions access to the interior windings,




while access to the outside windings is obtained from being in contact with




the solution in the drum, but the chemical solution can reach the windings in




the middle of the filter only by diffusion from the center tube and from the




outside.






There was no apparent difference in the manganese content of the fibers in the




middle of the cartridge compared to the inside windings or the outside windings.









                                      -2-




Based upon data gathered from radiation surveys, channeling was suspected.  A




method to test this supposition was devised.  Channeling of the water through the




filter housing, causing some filters to filter more water than others, would mean




that the water would move more quickly through some of the filters.  This, in turn,




would mean that the water would spend less time in the filter medium and a smaller




percentage of radium would be removed.







The filter housing is designed so that it is  likely that some of the filters




would have less flow through them than others.  The incoming water is routed




up the side of the housing in a "V" shaped space devoid of filters, which is




bordered by filters.  It first passes the filters next to the opening and




can reach the filters diametrically opposite  the inlet by passing around




all of the filters in the middle of the housing.






Evidence that this channeling was occurring was obtained during leach tests of  two  filti




which were removed for testing purposes  (Table IV).  The leaching solution in
                                          43-

-------
                                   TABLE IV

                 Concentration of Radium-226 in Leach Solutions
         Description
    226 Ra
    (pCi/1)
Cartridge No. 1 - Filter Batch

3rd Circle of filters from outside,
  Mid-way from water input

       15 min. Leaches

       Leach 1 - pH 3.0 at start
       Leach 2 - pH 2.0 at start
       Leach 3 - pH 1.0 at start
       Leach     1M  HNCU
  16 +_ 10
 122 + 20
 625 +_ 44
4150 + 100
Cartridge No. 2 - Filter Batch 1

1st (outside) Circle, 7/8 from input

       Leach - 24 hours @ 0.5M   HNO-
                                                              395 + 9
Cartridge No. 3 - Filter Batch 2

3rd Circle from outside, at input

   Not Leached

Cartridge No. 4 - Filter Batch 2

4th Circle, Mid-way from input

   Leach - 15 min. @ 0.5M HNO.
                                                             2480 +  80
                                        44 <

-------
each case was 0.5 M HNO , while the amounts of dissolved radium obtained from




leaching differed by a factor of 6,  The filter from which the higher amount




of radium was removed came from near the middle of the housing, while the other




filter came from diametrically opposite the input of the filter,









To re-route the flow of the incoming water, a baffle of corrugated iron sheet




was cut to fit into the "V" shaped inlet slot and to act as a riser to allow




water to flow up through the circular hole in the filter hold-down plate,




around the edges of the plate and into the filter spring area, thence to the




filters.  The baffle was installed on January 18, 1979 but test results  (See




Table III) did not show any significant improvement.  Whatever channeling or




other preferential flow existed, there was no significant improvement over the




radium removal rate before the baffle was installed.









Consideration was given to using a. plugging medium to partially block some of




the filters.  This would tend to distribute water more evenly throughout the




filter housing.  However, this was not attempted due to perceived difficulties




in operations.









At times it is desirable to backflush the filter housing, and some slight back




flushing would occur with the well cycling on and off automatically during




operations.  This would dislodge any filter plugging medium.  Suggested items




to attempt the plugging were polyethylene sheet chips, sand/ and diatomaceous




earth.









During the project, a special apparatus for testing a single filter was developed,




These tests were designed to determine the effect of varying the flow rate




through the filters.  Two separate tests were conducted.  The second test was




necessary due to the large variation in the radium content of the input water

-------
which put the accuracy of the results of the first test in question.






With well 6 in operation, approximately 3 liters of water per minute are passed




per filter.  With well 7 added to the flow of well 6, this increases to around




3.5 liters per minute.  With well 7 alone, the flow is about C.5 liter per




minute.






The results obtained are shown in Table V.  At relatively low flow rates, the




radium removal efficiency is somewhat greater than at higher flow rates ; the




same effect is also seen when Table III is examined.  Since well 7, when used




alone, produces water at a significantly slower rate than well 6, one would




expect that the radium removal rates would be higher than when well 6 was used.




This is observed.  There is one apparent exception.  In August of 1979, samples




were collected of well 6, well 7 and well 6 plus well 7, both before and after the




filter.  Because insufficient time elapsed between well switch manipulations




to allow the system to be purged of water from the previous arrangement, samples




labeled well 7, and well 6 and 7, actually were of water which was at least




partly of well 6, well 7 and/or wells 6 and 7.  The volume of the housing was




calculated to be about 250 gallons, and inasmuch as well 7 pumped only about




25 - 30 gallons per minute, about 10 minutes of operation would have been




necessary for one filter housing volume to be processed (disregarding the




volume of water in the lines).  Since this was on the order of the length of




time between samples in this particular series of samples, the obviously anoma-




lous results were obtained.






There may well have been some preferential flow through the housing even with




the baffle inserted in the housing, as the filters offered little resistance




to the flow of water at the processing rate used  (up to 120 gallons per minute).

-------
 Differential pressure across the housing was less  than two pounds  per square




 inch.   It is thought that a higher differential  pressure across the filters




 would  lead to less uneven flow through the housing,









 Based  upon the data and experiments,  it still cannot be discounted that signi-




 ficant preferential flow through the  housing exists,









                                      -3-




 The first filter housing was not epoxy coated at the factory.   It  was thought




 that rust in the housing would not be significant, since some  pipes in the city




 system had been in use nearly 50 years .  Substantial amounts of rust were




 encountered, however.  The chlorination step used  for sterilizing  the filters




 before filtered water could be added  to the system produced water  discolored




 with iron, and rusting was evident on the interior of the vessel and especially




 on the hardware (springs, "v"-bar guides, cups) .  The possibility  that the iron




 from the vessel in the chlorine solution could somehow interfere with the ability




 of the manganese fibers to remove radium could not be discounted ,  so the interior




 of the vessel, the springs, cups, and "V" bars were wire brushed and painted




 with epoxy paint designed for painting the interior of water supply tanks.  The




 filters from this first part of the test were removed and the  second batch of




 filters were used for the second part of the test.









 No effect of the iron could be demonstrated,
 The fourth possibility,  that of a filter inadvertently left out or a cap



being knocked loose,  causing a substantial volume of water to flow through the



 housing unfiltered was proven impossible by a careful inspection  and count



 during the openings  of the vessel .



                                       47-c

-------
                                     -5-




The possibility that the first batch of filters,  which contained significantly




less manganese (about 6 - 7%)  than the second (7  - 8%)  was considered a likely




cause of the low efficiency of the filter.   The second batch did not perform




as well as was expected from our earlier tests either.









It is quite likely though,  that the effect  of preferential flow in the single




stage filter is a contributor to reducing the efficiency.







Our earlier bench-scale experiments used a two-stage filtration system.  It




was known that a higher filtration efficiency could be obtained at a lower




flow rate per filter cartridge, and it was thought that the simplest way to




apply the manganese fiber radium removal procedure would be to use a large




single filter housing having a low flow rate per filter.  In view of the low




efficiencies actually found, it would appear that the best method would be to




use at least two stages of filtration.  This would allow the use of  smaller




units, and may circumvent the problem of waiting for a factory to custom make




a larger unit, when the smaller ones may be more quickly obtained.







The use of smaller units would also result in a greater differential pressure




across the unit and probably a more uniform flow through it.
                                 48-

-------
                VI.  Recommendations for Use of Manganese Fibers to




                    Routinely Treat Water for Removal of Radium






                                    A. Planning




The process is at least 80% efficient in a single stage of filtration at first,




and with two or more filter housings in series, should exceed 95%,






The single filter tests at various flow rates from 2 to 16 liters per minute,




Table V, show a large filtering ability even at flow rates as high as 16 liters




per minute (over four times the flow ratein the filter housing).  Scaling down




the size of the filter housing by a factor of 4 could be done and, assuming 80%




radium removal each, for two housings in series the removal rate should be 96%.







PVC pipe fittings are less expensive and should be used.  The installation is




also simpler.  They were avoided to prevent "false positives" in our tests for




organic chemicals.







Treating used filters in potassium permanganate solutions after one use,




instead of disposing of them directly and testing for radium removal ability,




should also be tried.







Small filter housings are available and should be used.  This would -permit one




person to perform filter handling operations, which due to the weight of the filter




holddown plate, now requires two people to handle.  The small filter housings also




may be more readily available.

-------
                             Table  V


         Single Filter Tests at  about  3%  liters per Minute

             Tests were performed to determine the

         filter history on radium removal performance.


                                                    Output
      Cartridge Condition                            pCi/1

Cartridge No.  3, Used, Not Leached                 1.0 + 1.5

Unused Filters                                    0   +0.2

Leached Cartridge                                 1.2 + 1.6

Input water,  well 6                               29+2.6
                                 50<

-------
                               B.  Operations







Step-by-step instructions for treatment, filter loading and disposal are



included as Tables VI, VII, and VIII.







                                  C.  Costs







The costs of operation could not be determined as well as desired due in part



to a reduction of state travel funds and the absence of the second filter



housing.  More data should be available for the final version of this report.



The cost analyses shown below (Table IX) are therefore maximums.  The cost



total for expendable supplies and labor is $1,137.75 for one filter housing



change  (sufficient for at least 2.5 million gallons), or approximately 45 cents



per thousand gallons (maximum).  Laboratory analyses, overhead, amortization



and installation of equipment costs are not included, nor is modification of



the system to provide series filtration.  More data on filter exhaustion would



reduce costs for these items.







This analysis shows that this process can favorably compete with other water



treatment processes.  Any attempt to remove the radium and re-use the filters



should serve to greatly lower the cost of new filters, (the major expense),



but should only be undertaken by persons with a familiarity of health physics.



Means for neutralizing and solidifying wastes generated should also be included.







Reprocessing the filter should also include a bath in a potassium salt, KCl



for example, as it is suspected that the process operates as an ion exchange


         +       4-t-
between K  and Ra

-------
An efficient crew accustomed  to  installing equipment in water treatment plants




should be able to conduct  operations according to the schedule in Table X,
                                    52 <

-------
                                 TABLE VI


                          Step-by-Step Instructions

                            - Filter Treatment -

                               For 120 Filters



Minimum crew;  1 (2 desirable)

Materials needed:

                   Work area  (with water supply, drain, electricity)

                   2-55 gallon drums with lids

                   2-53 gallon 1/8" rigid polyethylene drum liners

                  *60 Ibs. reagent grade potassium permanganate (KMnO )
                             crystals

                  *120 - 30 inch spun acrylic filters

                   lh rail polyethylene sheet - two 3" diameter circles

                   2 polyethylene buckets - 2 to 5 gallon size with pouring
                       spout

                   Drum syphon pump

                 **Stirring stick

                  *70 gallons Hot (110 - 120°F) water

                 **2 — Drum heating strips,   rings and 20 gauge wire (15')

                   2 - Drum heater variable power supplies

                   Polyethylene scoop (for KMnO^}

                   50 foot garden hose connected to water supply

                 **Rubber gloves - dishwashing type

                   Rubber boots and rain suit  (plastic, water repellant)

                  *24 Plastic bags - leaf type, sturdy (1.5 mil) minimum 36"
                        depth

                   Paper towels

                   Goggles  (for splash protection)

                   *Consumed, not reuseable
                  **Subject to rapid wear/or chemical attack

                                      i—*~t
                                      53-c"

-------
                             Table VI   (Cont'd)

 Remember - these filters are to be installed in your drinking water supply.

 Keep them clean.

 1.  Head warning on chemical containers.  Potassium permanganate,  (KMnC>4}
     improperly handled, can cause fire and/or explosions.

 2.  Place drums in work area.

 3.  Put liners inside drums.

 4.  Put (clean) gloves on.

 5.  Place 60 filters in drum, arranging them vertically  (it may be helpful
     to tip drum to a 45° angle).

 6.  Put boots and rain suit on.

 7.  Connect hose and turn on x
-------
                             Table VI  (Cont'd)

19.  Repeat steps 16 - 18 until all crystals have dissolved.

20.  Add hot water to bring liquid level in liner up so that filters are covered
     by at least 2 cm (3/4 inch)  of solution.  Filters may float, and will need
     to be pushed down.

21.  By repeatedly filling and emptying bucket using syphon pump, cycle 50
     gallons of solution from the bottom of the drum to the top to mix solution
     well.

22.  Pill the small annular space between the drum and drum liner with water to
     within 3 inches of the top.   This "jacket" of water conducts the heat from
     the drum heater to the filters.

23.  Rinse off the drum and other equipment and dry drum with paper towels.

24.  Wrap the drum heater around the base of the drum.  Use the small spring
     and wire to keep it in good contact with the drum by wrapping the wire
     once around the drum.  Connect the spring to one end of the heater, the
     wire to the other end of the spring and also to the other end of the heater
     strip.  Spring should be stretched so that drum heater remains   in good
     contact with the drum.

25.  Place round polyethylene sheet cover on top of filters and cover with drum lid.

26.  Connect heater power supply, and test for operation.  Allow 8-16 hours
     for stable temperature to be reached.  Adjust the power supply to keep
     within the range 86°F (30°C) to 104°F (40°C) .

27.  Once each day or two, repeat Step 21.  Remove the heater before working
     with solutions.  Replace heater afterwards.

28.  After 2 or 3 days,  the transparency of the solution will begin to change
     from a dark, deep purple to a more transparent and lighter shade.  Some
     brown fine precipitate (manganese oxide) will also form.

     As soon as any noticeable lightening in color has occurred, add 5 pounds
     of KMnO^j to the solution in the drum by disconnecting the drum heater and
     removing the heater strip (to keep accidental spills off of it) and following
     these steps:

29.  Connect hose and turn on water and leave on.

30.  Put syphon pump in drum.

31.  Holding pump hose so that any pumped solution runs back into the drum,
     prime the pump.  Lift the chemical bucket up and hold it over the chemical
     solution in drum (to avoid spilling on the floor) put the hose in the
     bucket and lower the bucket so that the syphon brings solution from bottom
     of drum into bucket.  As the bucket fills to 2/3 full, stop the flow by
     opening the syphon relief valve.

32.  Add 5 Ibs. of crystal potassium permanganate to the bucket and stir.

33.  Stir solution and crystal mixture in bucket for several minutes.

-------
                              Table VI  (Cont'd)


34.  Pour solution into drum (same as step 12).

35.  Repeat steps 31, 33 and 34 until all 5 Ibs. have been dissolved.

36.  Reconnect heater, following steps 23, 24, 25 and 26.

37.  Twice more over the next few days, as the strength of the solution decreases,
     add more KMnO^ in 5 Ib. lots following steps 28 through 36.

After all these steps have been completed and the solutions kept warm, the purple

color will completely disappear, indicating that all 30 pounds of KMno. in each

drum has been converted to oxides of manganese and potassium.   Once the color

of the liquid has changed to clear, the heaters may be disconnected and removed.

The filter fibers should contain about 7.5% Manganese by weight.   When the brown

precipitate is washed off of the filters they will have a very dark chocolate

to black color.  Check one or two of the filters by removing and washing them.

The filters are ready for loading into the filter housing now.



Keep the filters in the solutions without rinsing, until they are ready for use.
                                      56 <

-------
                                   TABLE VII


                           Step-by-Step Instructions

                            Loading Filter Housing



Minimum Crew:  2

Materials;

            1 quart bottle 5% liquid chlorine bleach

            Boots, rain suits, gloves

            24 plastic garbage bags (needed only if transportation of filters
               is necessary)

            115 treated filters

            Wrenches and jack for filter housing opening

            Paper towels

            Hose connected to water system

            Filter housing internal parts
Procedure

1.  Open bypass valve and close inlet and outlet valves on housing

2.  Open drain valve.  Open filter housing and insert rods for filters in
      cups in bottom of housing.
                          £

3.  Put on gloves, boots and rain gear.

4.  Remove filters from lined drums  (place 5 in each bag if bagging).

5.  Slide filters over rods onto cups until all 115 filters are in place.
      Pill from the center outward.

6.  Count the number of filters installed.  (Every one of the 115 filter
      positions must be filled).

7,  Place cups with springs on the filters, beginning in the center and moving
      outward.

8.  Lift the cover plate over the springs, align holes and slide over vertical
      bolts.  (This must be done carefully to avoid dislodging springs).  If
      any springs fall into the housing, it will be necessary to retrieve and
      replace them.  A straightened wire from a coat hanger and a flashlight
      will be of great assistance.

-------
                            Table VII  (Cont'd)



 9.  Tighten bolts to hold filters in place.

10.  Supply water pressure to the filter inlet valve.

11.  Open filter inlet valve and allow water  to run into filter housing and
       overflow.  Water will also exit through the opened housing drain valve.

12.  close filter inlet, allow water level in housing  to drop to about 1/3 of
       the length of the filters and close the filter  drain.

13.  Put rubber gasket in place and prepare to lower filter housing head.

14.  Pour the entire bottle of bleach into filter housing through the hole in
       the hold-down plate over the inlet "V".

15.  Lower and bolt down the head of the housing.

16.  Open filter housing inlet valve slightly.  Air will be expelled through
       the air relief valve in the top of the housing  as the housing is filled.
       When the sound of the air flowing out  of the valve ceases, the housing
       is full.

17.  Open the filter housing drain valve fully for a few seconds, and close it
       when the smell of the bleach is detectable.

18.  Close the filter inlet valve tightly.  Pressure to the housing inlet  valve
       now may be removed if necessary.

19.  IMPORTANT:  The filter housing must remain undisturbed,  full of the chlorine
       solution for at least 24 hours for proper disinfection.

20.  After at least 24 hours, open the filter housing  drain valve and let  housing
       empty.  Smell the water to verify a strong chlorine bleach smell is still
       present.

21.  Apply water pressure to the filter input valve.

22.  Open the inlet valve on the filter housing, letting water flow from the main,
       through the filters and then waste the water out of the filter drain valve
       to purge the filter housing of chlorine and precipitated manganese.

23.  Purge the housing of this by occasionally shutting off and opening the
       drain valve.

24.  After no further brown precipitate is seen, leave the filter drain valve
       open and close the filter by-pass valve.   The water in the main will
       now flow through the filter and be dumped through the filter drain  valve.

25.  The filter output valve may now be opened to feed treated water into  the
       system.  Close filter drain valve.
                                     58<

-------
                             Table VII   (Cont'd)

26.  Close the filter drain valve and regulate filter pressure.   (30 psig  for
     well 6 and 7-25 psig for well 6 or 7 alone)

-------
                                 TABLE  VIII

                           Step-by-Step Instructions

                          Filter Removal and Disposal



Minimum Crew:  2

Materials:

            Hose connected to water system

            24 plastic garbage (leaf)  bags minimum height 36"

            2 drums for radioactive waste with absorbent material.

            Disposable gloves, booties, overalls (water repellant)

            Portable alpha survey meter

            Masking tape

            Paper towels

            Box (for springs) - 1 cubic foot size

            Wrenches and jack for opening housing

            Dishwashing detergent



Procedure

1,   Open bypass valve if water needed in system

2.   Drain filter housing by closing intake and outlet valves, and opening low
    point 1" valve on bottom of housing.  Allow at least 24 hours for filters
    to drain.

3.   Open drums, put plastic liner in,  drape excess over drum lip and side.  Put
    1" of absorbent  material on bottom of drum.  Tip drum to about 45° angle
    to facilitate loading.

4.   Put on disposable gloves, booties and rain suit.  Tape sleeves.

5.   Open housing,  remove spring cover plate, remove spring/cap assembly on filters.

6.   With a helper holding the plastic bag, remove 5 filters, one at a time, and
    put them in the plastic bag.   Tie bag.  Helper puts the bag in the drum.

7.   Repeat step 6 until 60 filters have been put in the first drum and 55 in the
    other,

8.   Put disposable gloves, shoes, towels and coveralls from the last job in the
    small empty space in the side of the second drum, add absorbent material on

-------
                             Table VIII   (Cont'd)


     top of the filters, tie drum lining bag and seal drums.  Wipe off drums
     with towels.   Remove protective clothing.  Put coveralls, gloves, booties,
     and towels in plastic bag to be stored for disposal at the next filter
     unloading.  Survey personnel for contamination (hands, face, clothes, feet)
     using alpha survey meter.

 9.   Survey drum for:

                       gamma ray radiation levels

                       ftlpha contamination

     Wipe drum with filter paper for contamination test.

     Count wipe (must  be less than 22,000 dpm) to meet U, S. Department of
     Transportation Regulations.  Should not exceed 500 dpm.

10.   Using damp paper  towels, wipe off any area of skin which shows any evidence
     of foreign material from the filters.  Using liquid dishwasing detergent,
     wash areas.  Discard towels in plastic bag to be saved for disposal at next
     replacement.

11.   Perform final decontamination survey on personnel.  Remove any residual con-
     tamination by washing.  Skin must be dry to detect alpha contamination.

12.   Call disposal company to pick up drum.

-------
                            Table IX
                       Costs of Operation
            Consumable Supplies per Filter Loading
Filters                    115 @ $7.05                 810.75










Potassium permanganate      60 Ibs.  @ $2.45            157.00









Miscellaneous                                           10.00









Sub Total                                             $977 .75









Labor                       16 hrs.  @ $10.00       __  160.00







Total                                               $1,137.75

-------
                               Table X
                            Time Analysis




                            (Person Hours)









Filter Housing Installation




     Foundation




     Plumbing









Filter Preparation




     Initial Loading Chemical Mixing    2 people




     Checking, Stirring, Mixing









Filter Installation




     Transportation




     Vessel Opening




     Installation




     Vessel Closing and Chlorination




     Flushing
2 people
3 people
2 people
1 person
1 person
2 people
2 people
2 people
1 person
Total
Hours
6 hours 12 hours
10 hours 30 hours
4 hours 8 hours
8 hours 8 hours
h hour h hour
h hour % hour
1 hour 2 hours
h hour 1 hour
\ hour Jj hour

-------
                          VII  Acknowledgements
The writer would like to thank W.S.  Moore,  Ph.D.,  for  his  invaluable
advice and assistance, Bradley Caskey  for  his  able help, and Daniel Janek
of the City of Flatonia and his crew.
                                     64

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                            VIII  References
Cook, L.M., in Press, the Uranium District of the Texas Gulf Coastal Plain,
     in The NaturalRadiation Environment III.,   Proceedings of the Third
     International Symposium on the Natural Radiation Environment,
     Houston, Texas.  April 23 - 28, 1978.

Hill, R.B., 1973   Private Communication

Moore, W.S., and D.R. Reid, 1973   Extraction of Radium from Natural Waters
     Using Manganese - Impregnated Acrylic Fibers, Jour. Geophys. Res. 1973.
     P. 8880-8886.

Moore/ W.S. and L.M. Cook, 1975, Radium Removal from Drinking Water
     Nature  253;  262-263

Wukasch, M.C. and L.M. Cook, 1972, Environmental Surveillance in South Texas,
     in The_Natural Radiation Environment_ II, Proceedings of the Second
     International Symposium on the Natural Radiation Environment, Houston,
     Texas, August 7-11, 1972, P. 845-862, U.S.  ERDA Conf.  720806-P2.

Wukasch, M.C. and L.M. Cook, 1973, High Radioactivity in Drinking Water
     and Ground Water in South Texas, in Proceedings of the International
     Radi_ation Protection Association, III International Congress, Washington,
     D.C., September 9-14, 1973, P. 272-278, U.S. AEC, Oak Ridge, Tennessee.

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                                    TECHNICAL REPORT DATA
                             (Please read Instructions on the reverse before completing}
1. REPORT NO.
  ORP Contract Report  81-1
                                                             3. RECIPIENT'S ACCESSION NO,
4. TITLE AND SUBTITLE
  Advanced  Technology  for Radium Removal  from Drinking
  Water:  The Flatonia Water Treatment Project
                                                             5. REPORT DATE
                                                                      1981
             6, PERFORMING ORGANIZATION CODE
7. AUTHOR(S)
  Lewis M,  Cook
                                                             8. PERFORMING ORGANIZATION REPORT NO.
9, PERFORMING ORGANIZATION NAME AND ADDRESS
  Division  of Occupational  Health and  Radiation  Control
  Texas  Department of  Health
  Austin,  Texas
                                                             10. PROGRAM ELEMENT NO.
             11. CONTRACT/GRANT NO.

               88-01-3985
12. SPONSORING AGENCY NAME AND ADDRESS
  U-S?} Environmental  Protection Agency
  Office  of Radiation  Programs
  ANR-458
  Washington,  D.C.  204SO
             13. TYPE, OF REPORT AND PERIOD COVERED
             _    '   Final _
             14. SPONSORING AGENCY CODE
                 200/03 "-•'
15. SUPPLEMENTARY NOTES
16. ABSTRACT
  A study  was conducted  to determine  the applicability of using manganese-coated
  acrylic  fibers to remove R.adium from drinking water.
  The technique of using Manganese-coated fibers  to  remove radium from drinking
  water  is a simple,  effective and  economical procedure which  is  compatible with
  the operations of.a municipal  utflfty  crew.-     -•-.,..
17.
                                 KEY WORDS AND DOCUMENT ANALYSIS
                   DESCRIPTORS
                                                b.lDENTIFlERS/OPEN ENDED TERMS  C.  COSATI FieW/GlOUp
  Radium
  Drinking  Water
  Filters
18. DISTRIBUTION STATEMENT
  Release  unlimited
19. SECURITY CLASS 'This Reportt
 unclassified
                                                                            21. NO. OF PAGES
66
                                                20. SECURITY CLASS (This pagei
                                                 unclassified
                                                                            22, PRICE
 EP& form 2220-1 (R«s», 4-77}   PREVIOUS EDITION is OBSOLETE
                                               1<

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