EP A/600/A-98/008
POLLUTION PREVENTION FACILITY DEMONSTRATION OF
N-METHYL PYRROLIDONE AS A PAINT STRIPPING ALTERNATIVE
Jeiini M. Elion. Research Triangle Institute, Research Triangle Park, NC
J. Kaye Whitfield, Air Pollution Prevention and Control Division, US EPA, Research Triangle Park, NC
Dan Gillum, Marine Corps Logistics Base, Albany, GA
INTRODUCTION
This paper describes the demonstration of n-methyl pyrrolidone (NMP) as an alternative to methylene
chloride for stripping cured coatings from metal parts. It contains descriptions of both the old and new
processes, a summary of the equipment retrofit, and the results of the operational evaluation conducted at the
Marine Corps Logistics Base (MCLB) in Albany, GA, from November 1 to December 21,1995. RTI
coordinated this demonstration with personnel at the MCLB and die EPA Air Pollution Prevention and Control
Division. The project was funded by EPA under contract 68-D4-0120.
OBJECTIVE
The MCLB carries out maintenance activities on a wide variety of equipment from small arms to tanks,
trucks, and other vehicles. Much of the maintenance on the vehicles requires removing existing paint prior to the
repair procedures and applying new paint once the maintenance has been performed. The processes for paint
stripping, repainting, and cleaning of paint equipment release significant amounts of hazardous air pollutants
(HAPs). By Executive Order 12856, the MCLB is required to reduce these air emissions by 50% by 1999 from
1992 levels. The objective of this task was to demonstrate pollution prevention technologies or processes to
reduce the emissions of HAPs resulting from paint stripping via immersion in methylene chloride. This process
was chosen because methylene chloride is a HAP, a suspected carcinogen, and one of 17 chemicals on the EPA
33/50 list of priority pollutants. This objective was achieved by replacing methylene chloride with NMP, a non-
HAP and less volatile solvent. This process has been implemented and is in use at the Base.
PAINT STRIPPING WITH METHYLENE CHLORIDE
The first step in the paint stripping process was immersing a metal basket of coated metal parts in room
temperature methylene chloride for 1-2 hours (depending on the soil loading in the tank). This was followed by
three rinses with tap water: 1) an initial rinse to remove most of the methylene chloride residue, 2) a pressure
wash and pressure rinse to remove any remaining paint chips, and 3) a final hand rinse. The MCLB estimated
that the rinsing operations took 10-15 minutes per load. The basket was set aside to allow the parts to air dry.
At least two baskets of parts were stripped per day with this process.
The methylene chloride tank had an approximate surface area of 143 ft2 (13.3 m2) and was capable of
holding two 48 by 48 in. (122 by 122 cm) baskets side by side. The depth of methylene chloride in the tank was
approximately 30 in. (76 cm). A layer of water floated on the methylene chloride, serving as a seal to reduce
methylene chloride emissions due to evaporation. The water seal was approximately 2-3 in. (5.0 to 7.6 cm)
thick, but was not monitored to maintain a constant thickness. Water from the first rinse was used to replenish
the water seal on the methylene chloride tank; water from the second rinse was used to replenish the first rinse.
Water from the third rinse contained very little methylene chloride residue and was treated on site at the facility's
Industrial Wastewater Treatment Plant (IWTP).
About every 18 months, the tank was shut down and cleaned. Most of the paint chips would settle to the
bottom of the tank. MCLB personnel would pump most of the methylene chloride into 55-gal. (208 L) barrels.
Then the rest of the sludge would be scooped out into hazardous waste disposal containers, and the methylene
chloride from the barrels would be pumped back into the tank.
This tank was shut down and drained in May 1995, because the methylene chloride failed to meet
chemical specifications. When the tank was drained, severe damage to the tank walls was discovered. The
MCLB decided not to repair the tank but, instead, to switch to the NMP process as soon as it was operational.
In the meantime, those parts that would have been stripped in the methylene chloride were stripped with abrasive
blasting. This was a labor-intensive alternative because these parts required extensive masking to prevent media
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from becoming trapped, and usually required multiple passes to remove paint satisfactorily. Other parts, such as
the battery tie-down brackets coated with plastic coating Plastisol®, were soaked in hot alkaline solution
followed by scraping and blasting, also very time consuming.
EQUIPMENT RETROFIT
The first step in preparing for the demonstration was to retrofit an existing tank at the MCLB. The tank
designated by the MCLB was a large stainless steel tank, about 16 ft (4.9 m) long by 8.75 ft (2.7 m) wide by 8 ft
(2.4 m) deep. It was located in a pit in the concrete floor with the top edge even with the surface of the floor and
about 1 ft (0.3 m) of space between all sides of the tank and the concrete walls. The tank was divided by a steel
wall into two areas, each about 8 ft long by 8.75 ft wide by 8 ft deep. Lip vent exhausts were located along the
front and rear edges of the tank. It was insulated, but not heated. For successful stripping with NMP, the
existing tank required plumbing to heat the bath with steam available from MCLB, and a recirculating pump to
provide enough agitation to ensure uniform temperature throughout the bath. The adjacent tank required a pump
to draw recycled NMP for rinsing stripped parts. Finally, a vacuum distillation unit was installed to reclaim
used solvent from the stripping bath and provide recycled NMP for rinsing. After the tank retrofit was
completed, the heating and recirculating systems were tested using water in the tank. The stripping tank was
then emptied and filled with an initial charge of 38 55-gal. barrels of technical grade NMP. In parallel, the
operators were trained on operating the new process and equipment, and maintaining the system. For the rest of
the demonstration period, the operators used the NMP tank for normal stripping operations.
PAINT STRIPPING WITH NMP
The first step in the NMP chemical paint stripping process was immersing a metal basket of painted
metal parts in the heated NMP for 2-3 hours. The operating temperature range of the NMP was 150 ±10°F (66
±6°C). After the basket was raised over the stripping tank, the parts were pressure rinsed with recycled NMP.
The pressure rinse removed NMP residue and paint chips, and allowed the NMP to drain into the stripping tank.
The parts were blown with an air gun to remove additional NMP before the final rinse. The basket was then
moved away from the stripping tank and rinsed with tap water to displace the NMP. This rinse drained to the
IWTP. The MCLB estimates that the rinsing operations took 15 minutes per load. The basket was set aside to
allow the parts to air dry. At least two baskets of parts were stripped per day with this new process.
DEMONSTRATION RESULTS
The first basket stripped with the new process was loaded with battery tie-down brackets and
disconnects. The tie-down brackets were coated with black Plastisol®, a plastic coating that is very difficult to
remove. The disconnects were coated with several layers of Chemical Agent Resistant Coatings (CARC). The
basket was observed after 1 hour immersion at 140°F (60QC). The Plastisol® was peeling off the batteiy tie-
down brackets, but was not completely removed. Also, the CARC was softening on the disconnects but was not
sloughing off. The basket was left in the bath for an additional hour. While the basket was over the NMP bath,
the parts were blown with an air gun to force excess NMP back into the tank. The basket was moved away from
the tank, and the parts were then rinsed with water. The parts were examined: it was noted that NMP removed
nearly all of the Plastisol® from the tie-down brackets and the CARC from the disconnects. Some of the
remaining coating sloughed off when the parts were handled. On some parts, the coating had softened but still
adhered to the parts; in these instances, the coating had been veiy thick. Since NMP is absorbed through
multiple layers down to the base metal and then lifts the entire coating, parts with very thick coatings or multiple
layers would probably need to be left in the stripping tank overnight.
Of an estimated 20 baskets consisting mostly of batteiy tie-down brackets, disconnects, and filter
housings stripped over the course of the demonstration, MCLB reported problems with only two baskets. All the
remaining baskets of parts were stripped well enough for the parts to continue through production.
In the first case, the temperature control valve on the steam line stuck, so the NMP was not hot enough
to be effective. The second occurred when the steam supply valve was closed instead of the steam bypass valve.
(The bypass valve allowed rapid heatup of the tank.) The steam supply, steam bypass, and temperature control
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valves were labeled and an alarm has been added to alert the operators if the temperature drops below 140°F, the
minimum operating temperature.
During the demonstration, a white vapor sometimes appeared over die stripping tank. It would usually
appear when the recirculating pump was on and disappear when the pump was turned off, even at operating
temperatures. This suggests that the agitation of the pump is increasing air emissions. Research is planned that
will investigate the exact cause of vapor formation. The vapor is believed to be primarily NMP, with some
water present. Larger eductors may help reduce turbulence in the bath and still maintain an even temperature
throughout the bath. Also, the ventilation and exhaust system is to remain on at all times, as it is with other
tanks at the MCLB containing caustic or other hazardous compounds.
Currently, the operators are stripping one basket in the morning, one in the afternoon, and occasionally
leaving some parts in overnight. MCLB noted that some parts have corrosion on them that must be removed by
abrasive blasting and that loose coatings or small amounts of coatings remaining on these parts after chemical
stripping would be easily removed in a single pass. For example, filter housings not chemically stripped required
20-30 minutes abrasive blasting. The NMP-stripped parts need only 1-2 minutes blasting to remove corrosion, a
good improvement in time and personnel effort.
ESTIMATE OF NMP EMISSIONS/LOSSES
Over the course of the 6 week demonstration, approximately 3,640 lb (1651 kg) ~ about 8 barrels ~
were lost to emissions, dragout, and recycling. This is a significant reduction over the previous process, which
required the addition of approximately 10 barrels of methylene chloride each month. At this point, over 95% of
these losses may be attributed to NMP emissions and dragout because only six distillation cycles were run
during the demonstration period. Over time, as the paint sludge accumulates in the still, the MCLB will be able
to determine how much NMP is lost in the still bottoms. At least 25% of the loss over the demonstration period
may be attributed to tank overheating. Based on these losses, the MCLB will need to add 3-4 barrels of NMP
each month to the stripping tank. This amount may vary as the operators become more experienced with
controlling the bath temperature. MCLB is considering adding a cover to the tank to further reduce air
emissions.
ECONOMIC COMPARISON
A summary comparison of the capital and annualized costs is presented in the following table.
Assuming that an existing tank system is either to be cleaned and filled with methylene chloride or to be
refurbished for use with NMP, capital costs are significantly lower for the methylene chloride system (about
11% of the NMP system). The high capital costs for NMP reflect the significant investment required for the
retrofit. Capital items include the distillation unit (the largest single cost), recirculation pump, rinse pump,
heater platecoil, thermocouples, level sensors, recorders and displays, and the initial charge of NMP. Estimated
annualized costs for methylene chloride are $86,888, or about 108% that for NMP. The major cost is for the
methylene chloride, which is used in much larger quantities than estimated for NMP (almost ten times as much).
Labor costs are expected to be similar; although the basket of parts soaks longer in NMP, the operator does not
spend significantly more time with the new process. Because NMP is not regulated under the Resource
Conservation and Recovery Act (RCRA), a lower disposal charge applies to paint waste sludge containing NMP
as compared to paint waste sludge containing methylene chloride.
PROCESS
CAPITAL COSTS
ANNUALIZED COSTS
Methylene Chloride Stripping
$19,683
$86,888
NMP Stripping
$166,260
$80,580
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SAFETY CONSIDERATIONS
NMP has a flashpoint of 195°F (91°C); it is classified as a combustible and must be stored in
accordance with applicablelregulations. NMP is highly biodegradable, and NMP waste may be effectively
treated in a IWTP using activated sludge technology. NMP will be classified as hazardous waste only if it
contains hazardous components from the stripped parts.
NMP is a skin and eye irritant. NMP will not burn skin on contact but, because of its low vapor
pressure, it will not quickly evaporate either. Personnel are required to wear splash goggles, butyl rubber gloves,
and butyl rubber aprons when working with NMP. This personal protection equipment (PPE) designed to
protect the eyes and skin from direct contact is similar to that now required at the MCLB when working with
methylene chloride and MEK. Areas must be properly ventilated to prevent vapor buildup to levels above the
Threshold Limit Value of 100 ppm.
ENVIRONMENTAL CONSIDERATIONS
Under Executive Order 12856, the MCLB is required to file an annual Toxics Release Inventory (TRI)
of chemicals listed under section 313 of the Superfimd Amendments and Reauthorization Act (SARA) Title III.
The TRI includes emissions, transfers, and waste management data as part of the community right-to-know
provisions of SARA Title III. Methylene chloride is classified as a toxic chemical and is included on the TRI.
NMP was added to SARA Title III, section 313, for chronic health effects and became subject to reporting on
January 1,1995. As a result, the MCLB will be required to include NMP on the annual TRI report. However,
unlike methylene chloride, NMP is not classified as a Comprehensive Environmental Response, Compensation,
and Liability Act (CERCLA) hazardous substance, or a RCRA hazardous waste.
CONCLUSIONS	^
The NMP, when heated ^150 ±10^F\66 ±6°C), was able to remove multiple layers of CARC and strip
parts to the base metal within 3-4 hours. The heated NMP was able to successfully remove Plastisol®, a plastic
coating, from battery tie-down brackets. These parts were previously stripped in a hot alkaline bath, followed by
scraping and blasting to remove the coating. The NMP was able to soften epoxy-based topcoats, but removal
usually required overnight soaking. Annualized cost of NMP stripping is comparable to stripping with
methylene chloride, although the start-up cost is higher.
The distillation unit may provide a convenient method of removing paint sludge. It is expected that
pump agitation combined with the solvency of the NMP will dissolve paint chips in the tank; the paint will be
separated from the NMP during distillation. It is hoped that this will eliminate the past practice of draining the
tank for paint sludge removal as required with the methylene chloride.
The implementation of NMP eliminates a major source of HAP emissions at the MCLB. By eliminating
the methylene chloride for immersion stripping, the MCLB can reduce emissions 11%. The MCLB has already
replaced 1,1,1-trichloroethane vapor degreasers with aqueous parts washers. This change alone will further
reduce emissions from HAPs by another 16%. The MCLB has also replaced methyl ethyl ketone with a
propylene carbonate/benzyl alcohol blend for cleaning paint application equipment, reducing emissions from
HAPs an additional 21%. These three changes combined result in a reduction of emissions of 48%. The
remaining HAPs used at the MCLB are components in paints and coatings. The MCLB plans to replace solvent-
borne CARCs with waterborne CARCs in 1996 to achieve over 50% reduction in emissions from HAPs.
NOTICE
Although the information described in this article has been funded in part by the Environmental
Protection Agency under contract 68-D4-0120 to Research Triangle Institute, it does not necessarily reflect the
views of the Agency and no official endorsement should be inferred.
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"ntoh/tdt dtti td ir»c TECHNICAL REPORT DATA III llll II llll
JN JbvMrL L" K I P- J. IU 0 (Please read Instructions on the reverse before complet || | |||| || ||||
lllllllllllllll
1. REPORT NO ,
EPA/600/A-98/008
3 iii mi ii iiaa
PB98
III III 1 llll 1 III
-137441
4. TITLE AND ; _ . . , ^
Pollution Prevention Facility Demonstration of N-
Methyl Pyrrolidone as a Paint Stripping Alterna-
tive
5. REPORT DATE
6. PERFORMING ORGANIZATION CODE
7.author(s) Jm M.Elion (RXI), J.K.Whitfield (EPA), and
D.Gillum (Marine Corps)
8. PERFORMING ORGANIZATION REPORT NO.
9. performing organization name and address
Research Triangle Institute
P. 0. Box 12194
Research Triangle Park, North Carolina 27709
10. PROGRAM ELEMENT NO.
11. CONTRACT/GRANT NO.
68-D4-0120
12. SPONSORING AGENCY NAME AND ADDRESS
EPA, Office of Research and Development
Air Pollution Prevention and Control Division
Research Triangle Park, NC 27711
13. TYPE OF REPORT AND PERIOD COVERED
Published paper; 11/95— 3/96
14. SPONSORING AGENCY CODE
EPA/600/13
15.supplementary notes APPCD project officer is J. Kaye Whitfield, Mail Drop 61, 919/
541-2509. Presented at National Pollution Prevention Roundtable, 1996 Spring
Conference, Washington, DC, 4/10-12/96.
i6. abstract The paper describes a demonstration of n-methyl pyrrolidone (NMP) as
an alternative to methylene chloride for stripping cured coatings from metal parts.
It describes both the old and the new processes, summarizes the equipment retrofit,
and gives results of an operational evaluation conducted at the Marine Corps Logis-
tics Base (MCLB) in Albany, GA, from November 1 to December 21, 1995. The NMP,
when heated to 66 +/- 6 C, removed multiple layers of Chemical Agent Resistant
Coatings (CARCs) and stripped parts to the base metal within 3-4 hours. The heated
NMP successfully removed Plastisol, a plastic coating, from battery tie-down brac-
kets. The NMP softened epoxy-based topcoats, but removal usually required over-
night soaking. The annual cost of NMP stripping is comparable to stripping with
methylene chloride, although the start-up cost is higher. The implementation of NMP
eliminates a major source of hazardous air poilutant (HAP) emissions at the MCLB.
By eliminating the methylene chloride for immersion stripping, the MCLB can re-
duce emissions by 11%. The MCLB has already replaced 1, L 1-trichloroethane vapor
degreasers with aqueous parts washers: this change alone will further reduce emis-
sions from HAPs by another 16%. The MCLB has also replaced methyl ethyl ketone
with a propylene carbonate/benzyl alcohol blend, reducing HAP emissions by 21%.
17. KEY WORDS AND DOCUMENT ANALYSIS
a. DESCRIPTORS
b.IDENTIFIERS/OPEN ENDED TERMS
c. COSATI Field/Group
Pollution
Paint Removers
Metal Products
T oxicity
Solvents
Pollution Prevention
Stationary Sources
N-Methyl Pyrrolidone
Metal Parts
Hazardous Air Pollutants
13 B
11K
11F
06T
18. DISTRIBUTION STATEMENT
Reproduced from
Release to Public best available copy.
19. SECURITY CLASS (This Report)
Unclassified
21. NO. OF PAGES
20. SECURITY CLASS (This page)
Unclassified
22. PRICE
EPA Form 2220-1 (9-73)

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