EPA/600/R-18/078 | April 2018
www.epa.gov/homeland-security-research
United States
Environmental Protection
Agency
&EPA
Decontamination of	Spores
from Drinking Water Infrastructure
with Physical Removal (Pigging)
Office of Research arid Development
Homeland Security Research Program

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EPA/600/R-18/078
April 2018
Decontamination of Bacillus Spores
from Drinking Water Infrastructure with
Physical Removal (Pigging)
by
Jeffrey Szabo and John Hall
U.S. Environmental Protection Agency
Cincinnati, OH 45268
Greg Meiners, Sue Witt and Sri Panguluri
Aptim
Cincinnati, OH 45204
Interagency Agreement DW-89-92381801
Office of Research and Development
Homeland Security Research Program
Cincinnati, OH 45268
Contract EP-C-12-014
Office of Research and Development
Homeland Security Research Program
Cincinnati, OH 45268

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Disclaimer
The U.S. Environmental Protection Agency (EPA) through its Office of Research and
Development funded and managed the research described herein under contract EP-C-12-014
with Aptim and Interagency Agreement DW-89-92381801 with the Department of Energy. It
has been subjected to the Agency's review and has been approved for publication. Note that
approval does not signify that the contents necessarily reflect the views of the Agency. Any
mention of trade names, products, or services does not imply an endorsement by the U.S.
Government or EPA. The EPA does not endorse any commercial products, services, or
enterprises.
The contractor role did not include establishing Agency policy.
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Table of Contents
Disclaimer	ii
List of Figures	iii
Abbreviations	iv
Acknowledgements	v
Executive Summary	vi
1.0 Introduction	1
1.1	Background	1
1.2	Proj ect Obj ecti ve	1
1.3	WSTB System Description	1
2.0 Description of Pigging Techniques and Experimental Design	6
2.1	Ice Pigging	6
2.2	Chain Cutter Pigging	10
2.3	Contamination and Decontamination Experiments	18
2.4	Experimental Methods	19
3.0 Experimental Results	21
3.1	Ice Pigging	21
3.2	Chain Cutter Pigging	22
4.0 Conclusions	27
5.0 References	29
List of Figures
Figure 1: Schematic overview of Water Security Test Bed (WSTB)	2
Figure 2: Aerial view of the Water Security Test Bed (WSTB)	3
Figure 3: Water Security Test Bed system flow regulator	3
Figure 4: Water Security Test Bed discharge lagoon	4
Figure 5: Removable 15-ft PVC coupon section	4
Figure 6: Extracted pipe coupon	5
Figure 7: 450-ft Water Security Test Bed pipe interior	5
Figure 8: Ice slurry transfer to a mobile truck	7
Figure 9: Ice slurry injection into the upstream fire hydrant	8
Figure 10: Ice slurry retrieval from the downstream fire hydrant	9
Figure 11: Slurry water downstream discharge	10
Figure 12: KEG chain cutter nozzle	11
Figure 13: Combination (Vactor) truck	12
Figure 14: Chain cutter nozzle attached to the combination truck high pressure hose	13
Figure 15: Chain cutter nozzle inserted into the 450 ft	14
in

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Figure 16: Chain cutter nozzle after traversing the 450 ft	15
Figure 17: Individual pipe sections next to the Water Security Test Bed lagoon	16
Figure 18: Chain cutter nozzle operating in the individual pipe sections	17
Figure 19: Inside of the cement-mortar lined pipe section after pigging with the chain cutter.... 17
Figure 20: Decontamination of Bacillus globigii (BG) from the 450 ft Water Security Test Bed
pipe with ice pigging	21
Figure 21: Decontamination of Bacillus globigii (BG) from the 450 ft Water Security Test Bed
pipe with chain cutter pigging	23
Figure 22: Decontamination of Bacillus globigii (BG) from an individual cement-mortar lined
iron pipe with chain cutter pigging	25
Figure 23: Decontamination of Bacillus globigii (BG) from an individual corroded iron pipe with
chain cutter pigging	25
Abbreviations
BWS	bulk water sample
cfu	colony forming units
CT	chlorine concentration, C, in mg/L and contact time, T, in minutes
ft	foot
hr	hour
gpm	gallons per minute
HPC	heterotrophic plate count
INL	Idaho National Laboratory
LOD	limit of detection
M	meter
min	minute
MPN	most probable number
HSRP	Homeland Security Research Program
USC	Utility Services Co., Inc.
WSTB	Water Security Test Bed
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Acknowledgements
Contributions from the following individuals to the field work described in this report are
acknowledged: Stephen Reese, Trent Armstrong, and Michael Carpenter of the Idaho National
Laboratory; Steve Packer of Big Sky Industrial; John Kitchen of Utility Services Group; and Jim
Goodrich of the U.S. Environmental Protection Agency, who is the Water Security Test Bed
program manager.
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Executive Summary
The U.S. Environmental Protection Agency's (EPA) National Homeland Security Research
Center partnered with the Idaho National Laboratory (INL) to build the Water Security Test Bed
(WSTB) at the INL test site outside of Idaho Falls, Idaho. The WSTB was built using an 8-inch
diameter cement-mortar lined drinking water pipe that had been previously taken out of service.
The pipe was exhumed from the INL grounds and oriented in the shape of a small drinking water
distribution system that is 450 feet (ft) long. The WSTB can support drinking water distribution
system research on a variety of topics including biofilms, water quality, sensors, and homeland
security related contaminants. Since the WSTB is constructed of real drinking water distribution
system pipes, research can be conducted under conditions similar to those in a real drinking
water system (USEPA, 2016).
This report summarizes the results of biological decontamination experiments performed at the
WSTB focused on removing Bacillus globigii spores adhered to the inner surface of the 8-inch
water pipe. B. globigii spores are a non-pathogenic surrogate for B. anthracis, which is the
causative agent of anthrax. Decontamination was undertaken with a technique known as
pigging, or physical scouring of the inner pipe surface, followed by disinfection with free
chlorine. Two pigging techniques were evaluated in separate experiments. First, ice pigging
technology was used via a proprietary truck mounted mobile technology developed by the Utility
Services Co., Inc. (USC). Ice pigging works by pumping a slurry of ice and water down the pipe.
The ice in the slurry was expected to scour the inner pipe surface. The second pigging technique
used a KEG® chain cutter. In this technique, water was pumped from a combination (Vactor®)
truck at high flow and pressure and through a nozzle with a chain attached to it. The water flow
caused the chains to spin and scour the pipe interior. Both pigging techniques were used to
decontamination the 450 ft long pipe, as well as individual sections of cement-mortar lined iron
pipe, and unlined iron pipe with corrosion. The results of this study indicate that the chain cutter
followed by chlorination was more effective at reducing B. globigii spores than ice pigging
followed by chlorination.
The following is a summary of the results that came from the pigging experiments performed at
the INL WSTB:
•	No change in the number of spores adhered to the inner pipe surface was observed after
ice-pigging was conducted in the 450 ft pipe. After pigging, chlorination of the water in
the pipe at an initial concentration of 52 mg/L for 24 hours (55 mg/L after 24 hours)
resulted in a 1.0-log inactivation of the spores adhered to the pipe inner surface.
•	Pigging with chain cutting (2,300 psi, 70 gpm) resulted in a 3.3-log reduction of the
number of spores adhered to the inner surface of the 450 ft pipe. After pigging,
chlorination of the water in the pipe at an initial concentration of 82 mg/L for 24 hours
(31 mg/L after 24 hours) resulted in an additional 1.0-log inactivation of the spores
adhered to the pipe inner surface, for a total reduction of 4.3-log.
•	Chain cutter pigging (1,200 psi, 25 gpm) of an individual cement-mortar lined iron pipe
section resulted in a 1.5-log reduction of the number of spores adhered to the inner pipe
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surface. After pigging, chlorination of the water in the pipe at an initial concentration of
201 mg/L for 24 hours (154 mg/L after 24 hours) resulted in an additional 2.3-log
inactivation of the spores adhered to the pipe inner surface, for a total reduction of 3.8-
log.
• Chain cutter pigging (1,200 psi, 25 gpm) of an individual corroded iron pipe section
resulted in a 3.2-log reduction of the number of spores adhered to the inner pipe surface.
Chlorination of the water in the pipe at an initial concentration of 201 mg/L for 24 hours
(154 mg/L after 24 hours) resulted in an additional 0.6-log inactivation of the spores
adhered to the pipe inner surface, for a total reduction of 3.8-log. However, it should be
noted that the initial number of adhered spores were one log higher on the iron pipe
compared to the cement mortar pipe, likely due to the presence of tuberculation in the
iron pipe.
In summary, the best spore removal, a 4.3 log reduction, was achieved with the combination of
chain cutter pigging and chlorine treatment. However, this combination of decontamination
techniques was not enough to remove all detectable spores from the pipe surface. Should this
situation occur in reality, a technique like pipe lining or infrastructure replacement may need to
be implemented to ensure that human exposure to spores via drinking water does not occur.
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1.0 Introduction
1.1	Background
The U.S. Environmental Protection Agency's (EPA) Homeland Security Research Program
(HSRP) has partnered with Idaho National Laboratory (INL) to build the Water Security Test
Bed (WSTB) at INL in Idaho Falls, Idaho. The centerpiece of the WSTB is an 8-inch diameter
drinking water pipe that had been taken out of service. The pipe was exhumed from the INL
grounds and oriented in the shape of a small drinking water distribution system. The WSTB has
been fitted with service connections, fire hydrants, and removable coupons to collect samples
from the pipe interiors (USEPA, 2016).
Experiments focused on decontamination of Bacillus globigii spores adhered to the inner surface
of the 8-inch water pipe have been conducted at the WSTB in recent years. B. globigii spores are
a non-pathogenic surrogate for B. anthracis, which is the causative agent of anthrax. In one
experiment using the full-scale WSTB, chlorine dioxide was used to decontaminate adhered
spores. Two-log removal of B. globigii spores was observed with chlorine dioxide
decontamination, which was less effective than anticipated based on previous pilot-scale
experiments (Szabo et al, 2017; USEPA, 2016). Chlorine dioxide is a powerful disinfectant, and
it was not anticipated that other common drinking water disinfectants such as free chlorine or
monochloramine would be more effective. Therefore, subsequent efforts at removing adhered
B. globigii spores were focused on physical removal, or scouring of the inner pipe surface,
hereafter referred to as pigging. Two technologies were selected: ice pigging and chain cutter
Pigging.
1.2	Project Objective
The objective of the project was to conduct decontamination experiments at the WSTB with two
pigging technologies following intentional contamination of the WSTB with B. globigii spores.
The effectiveness of the pigging technologies at removing B. globigii from the inner pipe surface
was evaluated.
1.3	WS TB System Description
The primarily feature of the WSTB is an 8-inch (20 cm) diameter drinking water pipe oriented in
the shape of a small drinking water distribution system. The WSTB contains ports for service
connections and a 15-foot (5 m) removable coupon section designed to sample the pipe interior
to examine the results from contamination/decontamination experiments on the pipe wall. Figure
1 schematically depicts the main features of the WSTB.
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Figure 1: Schematic overview of Water Security Test Bed (WSTB).
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Figure 2 shows the aerial view of the WSTB. The lower right corner shows the upstream and
system inlet; the upper left corner shows the lagoon. The upstream fire hydrant was used for
injecting the ice slurry and the downstream fire hydrant was used to retrieve the injected
material.
Lagoon
Downstream fire hydrant
WSTB end
WSTB start
Upstream fire hydrant and injection port
Figure 2: Aerial view of the Water Security Test Bed (WSTB).
Drinking water supplied to WSTB is chlorinated ground water that also supplied the surrounding
INL facilities. The WSTB incorporates approximately 450 feet (137 m) of 8 inch (20 cm)
diameter cement-lined pipe. The 8 inch (20 cm) pipe system is constructed directly over the lined
drainage ditch for spill/ leak containment (as shown in Figure 2). The total volume of the WSTB
was estimated to be around 1,150 gallons (4,353 L). The valve near the end of WSTB along with
the flow meter (shown in Figure 3) was used to regulate and maintain flow.
Figure 3: Water Security Test Bed system flow regulator.
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The effluent water and ice slurry from the WSTB system was discharged to a lagoon (Figure 4)
which has a total water storage capacity of 28,000 gallons (105,980 L).
North
Figure 4: Water Security Test Bed discharge lagoon.
Bulk water samples (BWSs) and coupon samples were taken from the 15-foot (5 m) polyvinyl
chloride (PVC) pipe-segment designed and fabricated to contain 10 sets of duplicate removable
coupons (totaling 20 coupons). The coupons were made from cement-lined pipe used to
construct the rest of the WSTB. The coupons were installed such that they were flush with the
interior pipe surface. The coupons allow for the measurement of contaminant persistence on pipe
material, and the determination of the effectiveness of decontamination . Figure 5 shows a portion
of the 15-foot (5 m) PVC coupon section.
Coupons
Figure 5: Removable 15-ft PVC coupon section.
The 20 small coupons (22/32 of an inch [1.8 cm] in diameter and 0.371 square inches [2.4 square
centimeters] in area) were cut from the cement mortar-lined iron pipe obtained from INL and set
into threaded plugs that were inserted into the PVC-coupon section of the pipe. Figure 6 shows a
picture of the threaded coupon that was inserted into the pipe main. Furthermore, as seen in
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Figure 7, sampling could also be performed by removing pipe caps and directly sampling the
pipe interior.
Figure 6: Extracted pipe coupon.
Area sampled (scraped) for
Bacillus globigii spores
Figure 7: 450-ft Water Security Test Bed pipe interior.
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2.0	Description of Pigging Techniques and Experimental Design
Historically, the term "pigging," in the context of pipeline cleanup operations, refers to the
practice of using mechanical devices known as "pigs" to perform cleanup activities. The original
mechanical pigs used for cleaning pipes were made from straw wrapped in wire. This device
would make a squealing noise when scraping the pipe walls and traveling through the pipe,
which led to the process being called pigging. In general, pipeline cleaning operations using
pigs are accomplished by launching the "pig" at an upstream location and pushing the pig down
the pipe until it reaches a downstream receiving station for retrieval.
In industrial applications, soft "foam" pigs are most commonly used for pipe cleaning
applications. The soft pigs are constructed using flexible open cell polyurethane foam materials
(or other materials with similar properties) topped with select external wrapping that is suited for
individual application. The soft pigs are slightly oversized and designed to form a "sliding seal"
in the pipe. When pushed through the pipe, the soft pig is able to mechanically scrape and
remove product buildup, foreign matter and loose sediment from the pipe walls.
In 2011, Utility Services Co. (USC) launched ice pigging services (USC was subsequently
acquired by Suez North America and renamed Utility Services Group). Ice pigging combines
the operational advantages of flushing with the cleaning impact of soft pigging. The ice pig is a
semisolid ice slurry that is pumped like a liquid and flows through pipe bends and fittings
without blockage. Ice pigging has a minimum impact on operations. The ice pig is simply
pumped into and recovered from a hydrant at each end of the pipe section without excavation of
pipe or modification to the hydrant. According to the vendor, the benefits of ice pigging (in
comparison to other forms of pigging) to clean pipes include (USC, 2016):
•	Requires only 1/2 the time of other mechanical techniques
•	No requirement to disinfect post cleaning
•	Less disruptive/expensive than foam pigging
•	Combines operational advantages of flushing with cleaning impact of soft pigging
•	Pig behaves like a liquid, flows through changes in diameter, through bends, and through
butterfly valves without blockage
Physical scouring of the pipe interior can be performed using a variety of nozzles, or metal tips
that are attached to a high pressure hose. These pigs are activated by pumping water at high
pressure and flow through the nozzles. Some nozzles scour, or pig, the pipe using high pressure
water jet (or spray) that comes out of the nozzle at an angle. Other pigs use metal hooks, screws
or other metal protrusions to scour the pipe interior. The chain cutter described later in this
report falls into the category of physical scouring nozzles. Water pumped at high flow and
pressure through the nozzle causes the chains to spin and scour the pipe interior. Detailed
descriptions of the ice pigging and chain cutter pigging are provided in the following sections.
2.1	ice Pigging
Prior to coming to the site to perform decontamination activities, the USC team prepared the ice
slurry using their mobile trailer mounted equipment at a parking lot in Idaho Falls, Idaho
(approximately 50 miles from the test site). When the USC team arrived on-site, they transferred
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the slurry to a tanker truck in preparation for the decontamination event (Figure 8).
Transfer to truck
Figure 8: Ice slurry transfer to a mobile truck.
Before decontamination took place, the flow to main WSTB pipe was shut off, and the pipe
depressurized. The ice pigging crew then connected hose to deliver slurry mix to upstream
hydrant (Figure 9).
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Ice slurry mix connection to upstream fire hydrant
Figure 9: Ice slurry injection into the upstream fire hydrant.
The ice pigging decontamination event involved injecting one 600 gallon (2,271 L) slug of the
blended ice slurry into the upstream fire hydrant, and letting it scour the inner pipe wall as it
traveled down the pipe. The slurry was drained from the downstream fire hydrant (Figure 10)
into the lagoon (Figure 11). Once the 600 gallons (2,271 L) of ice slurry was injected into the
pipe, the upstream hydrant was closed and the downstream hydrant steam port was connected to
a discharge hose which routed the ice slurry to the lagoon. Flow and pressure were re-established
into the main water line, which pushed the ice slurry slug through the pipe and out through the
downstream hydrant discharge. After the ice slurry had cleared the pipeline, the downstream
hydrant was closed and the post pigging coupon samples were collected. This process took
approximately one hour.
The ice pigging crew described the consistency of the ice slurry as being similar to a slushie
beverage or frozen margarita. It was observed during the test that the ice slurry came out as a
semi-solid slurry in the lagoon. However, it was difficult to determine how much of the ice slurry
melted as it travelled down the pipe. It was possible that some melting took place since the sun
was shining directly onto the black pipe exterior, which is above ground.
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	;	:			i	
Downstream hydrant
connection
Figure 10: Ice slurry retrieval from the downstream fire hydrant.
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Slurry water discharge
Figure 11: Slurry water downstream discharge.
2.2 Chain Cutter Pigging
The nozzle shown in Figure 12 is the KEG* mini chain cutter (KEG Technologies, Inc.,
Spartanburg, SC) was used for scouring the internal surface of the pipe. INL contracted Big Sky
Industrial (Big Sky) to perform the chain cutting service for the Water Security Test Bed. This
chain cutter is capable of being inserted into pipes from 4 to 8 inches in diameter, and was
designed to remove obstructions and blockages in pipes such as roots and tuberculation (like iron
corrosion). This type of chain cutter is primarily used to clear wastewater piping clogged with
persistent tree roots, however the field operation of the device was the same for drinking water
pipe decontamination. When water flows into the rear end of the chain cutter (at the left of
Figure 12), the front end (right end of Figure 12) rotates, and the chains scour the pipe wall.
Water flows out in a high pressure jet through openings in the middle of the nozzle. This high
pressure jet flows toward the rear end of the nozzle and helps propel the nozzle forward. The
lengths of chain can be adjusted by adding or subtracting links. The chain length was set to allow
the chains to just touch the interior pipe walls.
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Chains
Pressurized water entry
Figure 12: KEG chain cutter nozzle.
In order to achieve the appropriate amount of chain rotation and scouring action, water must be
supplied from a combination truck, which is shown in Figure 13. Big Sky provided the Vactor®
truck and the operator for this chain cutting experiment. In the wastewater industry, combination
trucks are commonly referred to as "Vactor trucks" after one of the manufacturers of these
vehicles. Combination trucks have a dual function. The hose on the front can vacuum solids out
of a sewer and pump them into the tank on the back. The truck can also store approximately
1,300 gallons (4,921 L) of potable water, and pump it through a high pressure hose at up to 2500
psi (170 atm) and 80 gpm (302 L/min). Water at a flow of 70 gpm (265 I ./mill) and 2300 psi
(157 atm) pressure were used to operate the chain cutter inside of the 450 foot (ft) section of the
WSTB pipe. Figure 14 shows the chain cutter installed at the end of the high pressure hose.
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Sewer vacuum and storage tank
650 gal water storage tank
(identical tank on the other side)
High pressure hose reel
Figure 13: Combination (Vactor) truck.
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Figure 14: Chain cutter nozzle attached to the combination truck high pressure hose.
Images showing the process of pigging the 450 ft WSTB pipe are shown in Figure 15 and Figure
16. After the combination truck was filled with water and the chain cutter was installed on the
hose, the 450 ft WSTB pipe was depressurized. A cap on the end of the 450 ft pipe was removed
and the pipe was drained. The chain cutter was then inserted into the end of the dry,
depressurized pipe (Figure 15). When the high pressure water pump on the combination truck
was turned on, the water began flowing through the nozzle, and the chain cutter began spinning.
High pressure water exited through an opening in the rear of the chain cutter nozzle, and this
pressurized water flow propelled the chain cutter down the pipe (notice the water spray exiting in
the pipe in Figure 15).
Fi gure 16 shows the chain cutter at the other opposite end of the 450 ft pipe. Once the chain
cutter had traversed the length of the pipe, the hose reel on the combination truck pulled the
chain cutter back down the pipe. The chain cutter was then retrieved and removed from the
Vactor truck hose reel. After chain cutter pigging, a water flushing "bullet" attachment was
attached to the hose reel and reinserted into the 8 inch main to flush out any materials chipped
off the interior pipe surfaces during the chain cutting procedure.
It should be noted that the chain lengths were considerably eroded or shortened (approx. 1/8
inch) during the pigging operations due to contacting the pipe walls. Sparks were very evident
from the physical contact with the pipe walls as the chain cutter progressed down the pipe length.
Care should be taken to reapply chain lengths to the assembly as needed in order to maintain the
desired amount of pipe wall contact/abrasion.
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High pressure hose reel
with chain cutter inserted
into the WSTB pipe
Figure 15: Chain cutter nozzle inserted into the 450 ft
Water Security Test Bed (WSTB) pipe.
Backsplash panel
Spray from the rear end
of the chain cutter nozzle
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Chain cutter nozzle at the
end of the WSTB pipe
Figure 16: Chain cutter nozzle after traversing the 450 ft
Water Security Test Bed (WSTB) pipe.
In addition to the 450 ft pipe, individual sections of pipe were pigged with the chain cutter. The
individual pipe setup is shown in Figure 17, and the pigging process is shown in Figure 18.
Pigging of the individual pipe sections took place in the same manner as the 450 ft pipe, with the
exception that the water pressure and flow were reduced to 25 gpm and 1200 psi. Two types of
pipe were pigged. One was the same cement-mortar lined iron pipe used in the 450 ft WSTB
pipe. The other was iron pipe with heavy corrosion on the interior. This pipe was obtained from
the District of Columbia Water and Sewer Authority (DC Water). All pipe surface samples
taken from the individual pipes were direct scrapings of the inner surface. Figure 19 shows the
scouring of the cement-mortar pipe after pigging, with some of the cement-mortar coating
removed.
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Figure 17: Individual pipe sections next to the Water Security Test Bed lagoon.
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Area scoured by the
chain cutter nozzle
Figure 19: Inside of the cement-mortar lined pipe section after pigging with the chain
cutter.
Area sampled for
Bacillus globigii spores
Combination truck
and high pressure hose
Spray from the rear end .
of the chain cutter nozzle
Chain cutter nozzle at the end
of the individual pipe section
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2.3 Contamination and Decontamination Experiments
Contamination and decontamination took place as follows:
Step 1 - Pipe conditioning (cultivation of biofilm)
Step 2 - Contamination (addition of B. globigii spores to WSTB)
Step 3 - Decontamination (ice pigging/flushing)
Step 4 - Post-Decontamination Flushing, Reconditioning and Monitoring
Step 1 - Pipe Conditioning (Cultivation of Biofilm)
To effectively study the adsorption of contaminants such as B. globigii on pipe walls, it was
essential to ensure that there was a viable biofilm. The biofilm could influence adsorption of the
contaminant on the pipe wall. Similar to the past studies at WSTB, natural cultivation of biofilm
was chosen as the cultivation procedure for testing of the WSTB. This was accomplished by
passing INL tap water through the WSTB continuously over approximately 4 weeks before both
ice pigging and chain pigging experiments. After initial flushing to remove any debris, the
normal operating flow rate was set at 2.5 gallons per minute (gpm) with a total discharge of
25,200 gallons per week to the lagoon which allowed for weekly trucking and disposal of the
accumulated discharge.
For ice pigging and chain cutter pigging in the 450 ft WSTB pipe, samples of water from the
WSTB pipe and samples from the pipe interior were taken to determine background levels of
heterotrophic plate count (HPC) concentration and B. globigii. This sampling occurred prior to
contamination with B. globigii. After background samples were taken, the main pipe flowrate
was turned up from 2.5 to 15 gpm. For the individual pipes sections pigged with the chain
cutter, sampling for HPC and B. globigii took place in the same manner as the 450 ft pipe.
However, these pipes were not exposed to flow for 4 weeks before contamination.
Step 2 - Contamination (Addition of B. globigii Spores to WSTB)
During the contamination, the WSTB was operated at 15 gpm with a minimum contact time of
approximately 1 hour (to accommodate for travel time). Injection duration was also estimated to
be 1 hour so that there was a contact of one hour after the bolus of B. globigii suspension reaches
the coupon section of the pipe. Immediately prior to contamination of the 450 ft pipe, the B.
globigii stock was mixed with water to obtain 40 liters of the mixture with an expected in-pipe
mixed concentration of 1 x 106 colony forming units (cfu)/mL (at 15 gpm main flowrate).
Bacillus globigii injection was then started at 650 ml/min rate. The injection was complete after
one hour. After the injection was complete, flow in the pipe was reduced to 5 gpm, which was
maintained until the morning on the following day. Pipe surface and bulk water samples were
taken during injection, and then the morning of the day following contamination (immediately
before pigging).
For the individual pipe sections, caps were installed on each end of the pipe. The caps had two
influent ports so that tap water and B. globigii spores could be injected simultaneously. The
mixing action of simultaneous filling ensured that the spores were mixed evenly throughout the
bulk water phase in the pipe. Like the 450 ft pipe, enough spores were injected to achieve 1 x
106 cfu/mL in the bulk water phase. After the pipe sections were filled, the spores were allowed
to contact the pipe surfaces for 1 hr. The spore suspension was then drained, and the pipes were
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filled with tap water until chain cutter pigging. Background samples were taken before
contamination, immediately after contamination, and then the morning of the day following
contamination (immediately before pigging).
Step 3 - Decontamination (Pigging)
Ice pigging or chain cutter pigging was performed as described in sections 2.1 and 2.2,
respectively. As mentioned in Step 2, samples of bulk water and the scraped samples of the pipe
inner surface were taken immediately before and after pigging
Step 4 - Post-ice pigging disinfection and return to service.
Following the completion of the ice or chain pigging, the water pressure was restored to 40 psi
and water flow was reset to 15 gpm. One gallon of commercially available bleach (8.25%
sodium hypochlorite) was diluted with water 4:1 and the resulting mixture was injected into the
WSTB at 200 ml/min. Once the diluted bleach was injected, pipe flow as stopped and the bleach
was allowed to sit stagnant in the pipe for 24 hours. The in-pipe concentration was expected to
be between 70 to 80 mg/L once the bleach mixed throughout the pipe bulk water phase. After 24
hours of contact, flow was restored to 15 gpm and the bleach was flushed from the pipe. Both
coupon and bulk water samples were collected after the bleach was flushed. A similar procedure
was followed for the individual sections of pipe, except that 100 to 150 ml, depending on pipe
volume, of bleach was added to each pipe as it was being refilled with tap water after pigging.
Chlorination is a common method of pipe disinfection in the drinking water industry, which is
why it was chosen for disinfection in this study. However, due to variations in pipe demand and
volume of bleach added, chlorine concentrations differed from the target of 70 to 80 mg/L in
some experiments. These results are described in the section 3.0.
2.4 Experimental Methods
Preparation and transport of B. globigii spores
Bacillus globigii spores were produced by mixing an inoculum of B. globigii spores with generic
sporulation media and incubating with gentle shaking at 35 °C for 7 days. The B. globigii
suspensions were heat-shocked and enumerated using the spread plate method with tryptic soy
agar and membrane filtration (plating is described later in this section). Approximately 40 liters
of prepared stock was shipped in separate 1 liter containers inside coolers (preserved at 4 ± 2 °C)
to the site.
Extraction of biofilm and spores from coupon and pipe surfaces for microbial analyses
Pipe surface samples were taken either from coupons removed from the WSTB coupon section
or scraped directly from the 450 ft pipe wall. Coupon/surface samples were collected from the
WSTB carefully without touching the sampled surface that was exposed to WSTB water. The
biofilm and spores were scraped from the surface using a disposable sterile surgical scalpel. For
coupons, the entire coupon surface was scraped. For the pipe sections, an o-ring with the same
diameter as the coupon surfaces was placed on the pipe wall, and the area inside the o-ring was
scraped. This ensured that the area scraped was the same for the coupons and pipe wall. The
extracted material was collected in a sterile sample bottle with a sodium thiosulfate tablet (for
dechlorination of the water) and 100 mL of pre-filled carbon-filtered water. The extracted
sample was transferred to a cooler at 4 ±2 °C. The samples were shipped cooled overnight to the
19

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EPA laboratory and analyzed upon receipt.
Enumeration of B. slobisii and Heterotrophic Plate Count
Upon receipt in the lab, samples containing B. globigii spores were heat-shocked at 80° C for 10
minutes and analyzed using the Standard Methods spread plate method 9215 (APHA, 2005).
Tryptic soy agar plates were used for B. globigii spores. B. globigii plates were incubated at 35°
to 37°C for 24 hours. Heterotrophic plate count samples were analyzed using the IDEXX
SimPlate® method (Westbrook, ME) according to Standard Methods 9215E (APHA, 2005).
Plates were inculcated at 35° ± 0.5° C for 45 to 72 hours. When needed, samples were serially
diluted (B. globigii and HPC) or membrane filtered (B. globigii).
Bulk water samples
The BWS for B. globigii were collected using the grab sampling technique in 100 mL sterile
sample bottles with a sodium thiosulfate tablet. The BWS sampling port in the WSTB coupon
section was opened and the water was drained for 15 seconds prior to collection of 100 ml of
water from the WSTB.
Free Chlorine
During decontamination experiments, 100 ml grab samples were collected from the water
sampling port in the WSTB coupon section. The water was drained for 15 seconds prior to
collection of 100 ml of water from the WSTB. Samples were collected in a clean glass
laboratory beaker and analyzed for free chlorine using a portable Hach® colorimeter Hach,
Loveland, CO). The sample was immediately processed for free chlorine using the Hach Method
10102 using N,N-diethyl-p-phenylenediamine (DPD) at the WSTB site. Samples were diluted in
distilled water as needed.
20

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3.0	Experimental Results
3.1	ice Pigging
The background HPC concentration on the inner pipe surface was analyzed via two coupon
samples. These samples were removed after one month of water flow through the WSTB pipe,
but before contamination with spores and decontamination with pigging. HPC values from the
two coupons were 4.0 x 105 most probable number (MPN)/cm2 and 2 x 105 MPN/cm2,
respectively. These results indicate that viable biofilm was present on the pipe walls at WSTB
prior to the initiation of the tests. It should be noted that all coupon samples for HPC and B.
globigii spores were removed from the WSTB coupon section.
Figure 20 graphically summarizes the data obtained from the ice pigging tests. The B. globigii
spore values obtained from the pipe wall coupons have been converted to colony forming units
per square centimeter (CFU/cm2). For all bars in Figure 20, the "n" value shown in the legend
represents the number of coupons samples taken during that phase of the experiment. The bar
represents the average of those coupons, and the error bars represent standard deviation. The
limit of detection (LOD) in Figure 20 was calculated as follows: The scrapings from the sampled
coupon surface went into 100 ml of sterile buffer. Then 22.2 ml of the buffer suspension
containing the coupons scrapings were membrane filtered in duplicate three sample volumes
(O.lmL, lmL, and lOmL). If one spore was contained in the filtered 22.2 ml, that scales up to 4.5
per 100 ml. When that value was normalized by the coupon area 2.4 cm2, this yields a value of
1.9 CFU/cm2.
Pre-BG injection:
None Detected
¦ Pre-BG injection Spore Density, n=2
^	¦ Spore Density During BG Injection, n=4	LOD: 1.9 cfu/cm2)
¦	Post-BG Injection, Pre-lce Pigging Spore Density, n=3
¦	Post Ice Pigging Spore Density, n=6
¦	Post Chlorination Spore Density, n=4
Figure 20: Decontamination of Bacillus globigii (BG) from the 450 ft Water Security Test
Bed pipe with ice pigging.
The missing first bar (pre-BG injection spore density) is not visible on the graph because no
spores were detected above the LOD in the background samples. These coupons had been in
21

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contact with the water for 4 weeks before the background samples were taken. A text label has
been added to reflect that no viable spores were detected in white space where the bar would
appear if any background B. globigii were present. The second bar (spore density during BG
injection) represents the number of viable spores detected on the coupons during the spore
injection. The bulk water phase had 1.2 xlO6 CFU/mL during this period of sample collection.
The third bar (Post-BG injection) represents the number of viable spores attached to the coupons
after the B. globigii contaminant slug passed out of the pipe with clean water behind it. These
coupon samples were taken the day after contamination, and immediately before ice pigging.
BWS taken during this time showed that 5.0 x 101 CFU/ml were present in the bulk water of
pipe. The fourth bar (Post ice pigging BG spore density) represents the number of viable B.
globigii spores attached to the coupons after ice pigging. The data suggest that there is no
difference between the pre and post ice pigging pipe wall spore densities. Furthermore, after
water was restored at 40 psi to the pipe, 7.3 x 101 cfu/ml viable spores were detected in the bulk
water phase. Therefore, it can be concluded that the ice pigging decontamination procedure is
not an effective way to remove spore from the water under the tested conditions.
The last bar in Figure 20 (Post chlorination spore density) represents the number of viable spores
recovered from the coupons after chlorination. As mentioned previously in the report, one gallon
of free chlorine (Clorox bleach) was pumped into the WSTB pipe after ice pigging so that it
spread out evenly through the pipe volume. The initial free chlorine concentration was 52 mg/L.
After 24 hours of contact, the free chlorine concentration was 55 mg/L. These values yield a bulk
phase CT (chlorine concentration, C, in mg/L and contact time, T, in minutes) of 77,040 mg-
min/L. After chlorination, the number of viable spores recovered from the pipe surface
decreased by 1 log. No viable spores were detected in the bulk water phase after the bleach had
been flushed from the pipe and tap water restored.
3.2 Chain Cutter Pigging
The background HPC concentration on inner pipe surface was analyzed via two coupon samples.
These samples were removed after one month of water flow through the WSTB pipe, but before
contamination with spores and decontamination with pigging. HPC values from the two coupons
were 1.8 x 103 MPN/cm2 and 3.1 x 103 MPN/cm2, respectively. These results indicate that viable
biofilm was present on the pipe walls at WSTB prior to the initiation of the tests. It should be
noted that coupon samples for HPC were removed from the WSTB coupon section.
Figure 21 graphically summarizes the data obtained from the chain cutter pigging tests. The B.
globigii spore values obtained from the pipe wall coupons have been converted to colony
forming units per square centimeter (CFU/cm2). For all bars in Figure 21, the "n" value shown in
the legend represents the number of coupons samples taken during that phase of the experiment.
The bar represents the average of those coupons, and the error bars represent standard deviation.
The LOD in Figure 21 was calculated as follows: The scrapings from the sampled coupon
surface went into 100 ml of sterile buffer. Then 22.2 ml of the buffer suspension containing the
coupons scrapings was membrane filtered in duplicate three sample volumes (O.lmL, lmL, and
lOmL). If one spore was contained in the filtered 22.2 ml, that scales up to 4.5 per 100 ml. When
that value was normalized by the coupon area 2.4 cm2, you get a value of 1.9 CFU/cm2. In
Figure 21, note that the pre-BG injection spore density and the spore density during BG injection
were taken from the WSTB coupon section. This was done because the pipe was full and
22

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pressurized during these samples. During the next three sampling phases, the pipe was open and
depressurized, so pipe surface scrapings were taken directly from the pipe wall.
Pre-BG injection:
None Detected
¦ Pre-BG injection Spore Density, n=2
^	¦ Spore Density During BG Injection, n=4	LOD: 1.9 cfu/cm2)
¦	Post-BG Injection, Pre-Pigging Spore Density, n=4
¦	Post Pigging Spore Density, n=6
¦	Post Chlorination Spore Density, n=4
Figure 21: Decontamination of Bacillus globigii (BG) from the 450 ft Water Security Test
Bed pipe with chain cutter pigging.
The missing first bar (pre-BG injection spore density) is not visible on the graph because no
viable spores were detected above the LOD in the background samples. These coupons had been
in contact with the water for 4 weeks before the background samples were taken. A text label
has been added to reflect that no spores were detected in white space where the bar would appear
if any background B. globigii were present. The second bar (spore density during BG injection)
represents the number of viable spores detected on the coupons during the spore injection. The
bulk water phase had 1.9 xlO6 CFU/mL during this period of sample collection. The third bar
(Post-BG injection...) represents the number of viable spores recovered from the coupons after
the B. globigii contaminant slug passed out of the pipe with clean water behind it. These coupon
samples were taken the day after contamination, and immediately before chain cutter pigging.
BWS taken during this time showed that 4.3 x 101 CFU/ml were present in the bulk water of
pipe. The fourth bar (Post ice pigging BG spore density) represents the number of viable B.
globigii spores recovered from the coupons after chain cutter pigging. The data shows a 3.3-log
decrease in the number of spores after chain cutter pigging. This suggests that scouring the pipe
surface with the chain cutter removed enough of the cement-mortar matrix and biofilm to impact
the number of adhered spores. After water was restored at 40 psi to the pipe, 1.3 x 101 cfu/ml
viable spores were detected in the bulk water phase.
The last bar in Figure 21 (Post chlorination spore density) represents the number of viable spores
recovered from the coupons after chlorination. As mentioned previously in the report, one gallon
of free chlorine (Clorox bleach) was pumped into the WSTB pipe after chain cutter pigging so
that it spread out evenly through the pipe volume. The initial free chlorine concentration was 82
mg/L. After 17 hours of contact, the free chlorine concentration was 31 mg/L. These values yield
23

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a bulk phase CT of 109,650 mg-min/L. After chlorination, the number of viable spores
recovered from the pipe surface decreased by 1.0 log. No viable spores were detected in the bulk
water phase after the bleach had been flushed from the pipe and tap water restored.
Between chain cutter pigging and chlorination, viable spores adhered to the pipe wall decreased
by 4.3 log.
In addition to the 450 ft WSTB pipe, individual cement-mortar lined iron and corroded iron pipe
sections were also contaminated and pigged. The results from the cement-mortar lined pipe are
shown in Figure 22 and the corroded iron pipe in Figure 23. The bars in each figure correspond
with the same experimental phases as those used in Figure 20 and Figure 21. Like Figure 20 and
Figure 21, the "n" value shown in the legend represents the number of coupons samples taken
during that phase of the experiment. The bar represents the average of those coupons, and the
error bars represent standard deviation. All samples taken in Figure 22 and Figure 23 were
scraping from the pipe wall of the individual pipe sections.
Figure 22 shows that the number of viable spores adhered to the inner surface of the cement-
mortar pipe was between 105 and 106 cfu/cm2. The same range of initially adhered spores was
observed in contamination and pigging experiments performed in the 450 ft WSTB pipe. Chain
cutter pigging resulted in a 1.5 log reduction of adhered spores. Chlorination was conducted in
the same manner as the experiments in the 450 ft pipe, with household bleach added to the pipe
section and a contact time of 17 hours. The initial free chlorine concentration was 201 mg/L.
After 17 hours of contact, the free chlorine concentration was 154 mg/L. These values yield a
bulk phase CT of 228,990 mg-min/L. After chlorination, inactivation of the spores adhered to
the pipe inner surface decreased by 2.3 log. No spores were detected in the bulk water phase
after chlorination. Between chain cutter pigging and chlorination, spores adhered to the pipe
wall decreased by 3.8 log.
Results from the individual pipe differs from the pigging that took place in the 450 ft WSTB
pipe, which also contains cement-mortar lined iron pipe. Specifically, the reduction of spores
adhered to the pipe wall due to chain cutter pigging was 3.3 log in the 450 ft pipe, but only 1.5
log in the individual pipe section. This was likely because the chain cutter nozzle was not
operated at full strength in the individual pipe section. In the 450 ft pipe, the chain cutter nozzle
was operated with 2300 psi and 70 gpm. In the individual pipe section, 1200 psi and 25 gpm
was used, and this pressure and flow resulted in less scouring action compared to the 450 ft pipe
experiment. The combination truck operator used the reduced flow and pressure in the
individual pipe section for safety reasons. The individual pipe section was open at both ends,
and there was concern that operation at the maximum pressure and flow would push the chain
cutter out of the pipe and cause damage to the chain cutter or the surrounding area.
Chlorination in the individual pipe section inactivated the spores adhered to the pipe inner
surface by 2.3 log, with an initial chorine value of 201 mg/L and a CT of 228,990 mg-min/L. In
the 450 ft pipe, 1.0 log inactivation was observed with an initial concentration of 82 mg/L and a
CT of 109,650 mg-min/L. The increased spore inactivation in the individual pipe section was
likely due to the fact that a higher chlorine concentration was used. Ideally, the same chlorine
concentration would have been applied to both the 450 ft pipe and the individual pipe section.
However, achieving equal concentrations in a field setting was difficult due to the different pipe
24

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setups and varying disinfectant demand between individual pipe sections. However, it is notable
that if the chain cutter was used at a reduced pressure or flow, or if it does not contact a portion
of the pipe efficiently, application of a higher level of free chlorine can make up for the reduced
log reduction resulting from pigging alone.
ar i.E+06
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l.E+05
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in
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o
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a>
o
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l.E+04
l.E+03
l.E+02
l.E+01
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Pre-BG injection:
None Detected
i Pre-BG injection Spore Density, n=2
i Spore Density During BG Injection, n=4
Post-BG Injection, Pre-Pigging Spore Density, n=4
Post Pigging Spore Density, n=6
Post Chlorination Spore Density, n=4
LOD: 1.9 cfu/cm2)
?igure 22: Decontamination of Bacillus globigii (BG) from an individual cement-mortar
lined iron pipe with chain cutter pigging.
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u
3
-i—
(J
l/l
C
O
Q.
3
O
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+;
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l.E+07
l.E+06
l.E+05
l.E+04
l.E+03
l.E+02
l.E+01
g l.E+OO
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Pre-BG injection:
None Detected
I Pre-BG injection Spore Density, n=2
Spore Density During BG Injection, n=4
Post-BG Injection, Pre-Pigging Spore Density, n=4
Post Pigging Spore Density, n=6
Post Chlorination Spore Density, n=4
LOD: 1.9 cfu/cm2)
Figure 23: Decontamination of Bacillus globigii (BG) from an individual corroded iron pipe
with chain cutter pigging.
25

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Figure 23 shows that the number of spores adhered to the inner surface of corroded iron was
between 106 and 107 cfu/cm2. This range of initially adhered spores was higher than what was
observed in contamination and pigging experiments performed in the 450 ft WSTB pipe and the
individual cement-mortar lined iron pipe. The increase in initially adhered spores was likely due
to the tuberculation (iron corrosion) that protruded from the inner surface of the iron pipe. The
rough tuberculation has many ridges and crevasses where spores and particles can adhere.
Chain cutter pigging resulted in a 3.2 log reduction of adhered spores. Chlorination was
conducted in the same manner as the experiments in the 450 ft pipe, with household bleach
added to the pipe section and a contact time of 17 hours. The initial free chlorine concentration
was 140 mg/L. After 17 hours of contact, the free chlorine concentration was 25 mg/L. These
values yield a bulk phase CT of 201,450 mg-min/L. Chlorination resulted in a 0.6 log
inactivation of the spores adhered to the pipe inner surface. No spores were detected in the bulk
water phase after chlorination. Between chain cutter pigging and chlorination, spores adhered to
the pipe wall decreased by 3.8 log.
No comparable data exists for pigging of corroded iron pipe contaminated with Bacillus spores.
However, like the individual cement-mortar pipe section, the chain cutter nozzle was operated at
a reduced pressure and flow of 1200 psi and 25 gpm. In the individual corroded iron pipe, a 3.2
log reduction of adhered spores was observed compared to a 1.5 log reduction in the individual
cement-mortar lined pipe. Chain cutter pigging of the iron pipe section removed the
tuberculation protruding from the pipe interior, so it is possible that additional pressure and flow
may not have resulted in more removal. Chlorination of the individual corroded iron pipe only
resulted in a 0.6 log inactivation of the spores adhered to the pipe inner surface, with an initial
chorine value of 140 mg/L and a CT of 201,450 mg-min/L. The chlorination level was
comparable to in the individual cement-mortar lined pipe, but the log reduction was less due to
the increased disinfectant demand of the iron pipe.
26

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4.0 Conclusions
Removing adhered Bacillus spores from drinking water infrastructure can be challenging. This
study examined the ability of pigging, or physical scouring of the inside of pipes, followed by
chlorination, to remove adhered Bacillus spores. A summary of results are as follows:
•	No change in the number of spores adhered to the inner pipe surface was observed after
ice-pigging was conducted in the 450 ft pipe. After pigging, chlorination of the water in
the pipe at an initial concentration of 52 mg/L for 24 hours (55 mg/L after 24 hours)
resulted in a 1.0-log inactivation of the spores adhered to the pipe inner surface. Elevated
temperature may have impacted the efficacy of the ice pigging since the pipes were above
ground.
•	Pigging with chain cutting (2,300 psi, 70 gpm) resulted in a 3.3-log reduction of the
number of spores adhered to the inner surface of the 450 ft pipe. After pigging,
chlorination of the water in the pipe at an initial concentration of 82 mg/L for 24 hours
(31 mg/L after 24 hours) resulted in an additional 1.0-log inactivation of the spores
adhered to the pipe inner surface, for a total reduction of 4.3-log.
•	Chain cutter pigging (1,200 psi, 25 gpm) of an individual cement-mortar lined iron pipe
section resulted in a 1.5-log reduction of the number of spores adhered to the inner pipe
surface. After pigging, chlorination of the water in the pipe at an initial concentration of
201 mg/L for 24 hours (154 mg/L after 24 hours) resulted in an additional 2.3-log
inactivation of the spores adhered to the pipe inner surface, for a total reduction of 3.8-
log.
•	Chain cutter pigging (1,200 psi, 25 gpm) of an individual corroded iron pipe section
resulted in a 3.2-log reduction of the number of spores adhered to the inner pipe surface.
Chlorination of the water in the pipe at an initial concentration of 201 mg/L for 24 hours
(154 mg/L after 24 hours) resulted in an additional 0.6-log inactivation of the spores
adhered to the pipe inner surface, for a total reduction of 3.8-log. However, it should be
noted that the initial number of adhered spores were one log higher on the iron pipe
compared to the cement mortar pipe, likely due to the presence of tuberculation in the
iron pipe.
These results suggest that physical scouring of pipe interior with a chain cutter nozzle is an
effective way to achieve a 3.3 log reduction of spores when operated at maximum flow and
pressure. Chlorination at 82 mg/L for 17 hours immediately following the pigging resulted in
additional log reduction, for a total of a 4.3 log reduction of spores. In the experiments described
in this study, the 4.3 log reduction was not enough to remove all detectable spores from the pipe
surface. Should this situation occur in reality, a technique like pipe lining or replacement may
need to be implemented to ensure that human exposure to spores via drinking water does not
occur. However, pigging and chlorination can significantly reduce the number of spores adhered
to drinking water infrastructure, which may make further remedial actions easier. It should also
be considered that the consequence of pigging is the generation of contaminated waste and wash
water, which must be treated or disposed of properly.
27

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It should also be noted that the skill and experience of the operators applying either pigging
technology are important. There is an art to "working the pigs" effectively through the pipeline,
especially for the chain cutter. The speed of the chain cutter is controlled by the operator and
certain sections of pipe may require several passes or rework as the pig progresses through the
pipe. Similarly, for ice pigging, the pipe conditions and operator experience dictate whether
several smaller slugs of ice or one large slug of ice is needed to effectively scour the pipe.
28

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5.0 References
APHA (American Public Health Association), (2005). Standard Methods for the Examination of
Water and Waste Water, Method 9125, 21st edition. Washington, DC: American Public
Health Association.
Szabo, J.G.; Meiners, G.; Heckman, L.; Rice, E.W.; & Hall, J., 2017. Decontamination of
Bacillus spores adhered to iron and cement-mortar drinking water infrastructure in a
model system using disinfectants. Journal of Environmental Management, 187:1.
USC (Utility Service Company), (2016). Ice Pigging - Advanced Pipe Cleaning Technology.
USC Rebranded as Suez, Atlanta, GA. Available at:
https://www.utilitvservice.com/icepigging.html
USEPA (U.S. Environmental Protection Agency), 2016. Water Security Test Bed Experiments at
the Idaho National Laboratory. EPA/600/R-15/146, Washington DC: U.S. Environmental
Protection Agency.
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vvEPA
United States
Environmental Protection
Agency
PRESORTED STANDARD
POSTAGE & FEES PAID
EPA
PERMIT NO. G-35
Office of Research and Development (8101R)
Washington, DC 20460
Official Business
Penalty for Private Use
$300

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