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OCCIDENTAL CHEMICAL CORPORATION
MONTAGUE, MICHIGAN

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EPA ID NO. MID 006 014 906

1.0 INTRODUCTION

The Occidental Chemical Corporation (OCC) facility, located on the west side of
Montague, Michigan, is generally bounded on the south by Old Channel Trail, on
the east by Whitbeck Road, on the west by Lamos Road, and on the north by
Hancock Street. White Lake is located immediately to the south. The OCC
facility occupies approximately 860 acres (see figure 1). The manufacturing plant
is no longer in operation, and the production buildings have been demolished.
Buildings remaining on-site include a groundwater treatment plant, trailer/office
building, and storage outbuildings.

Past activities at the OCC facility have resulted in polychlorinated biphenyls '
(PCBs) and hexachlorobenzene (C-66) contamination of White Lake sediment.


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UNITED STATES GEOLOGIC SURVEY
MONTAGUE, FLOWER CREEK, MICHIGAN QUADRANGLES
TOPOGRAPHIC, 7.5 MINUTES SERIES 1983
SCALE: 1:25,000

MILLER SPRINGS REMEDIATION MANAGEMENT INC.

Montague, Michigan


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2.0 PROJECT DESCRIPTION

EPA issued an Administrative Order to OCC in March 1993 requiring corrective
action at the facility. A Final Decision for remediating the OCC facility was
published in July 2001. Part of the remedy required OCC to dredge approximately
8,500 cubic yards of contaminated sediment from a 1.6-acre area of White Lake
near the OCC outfall off Dowies Point. The purpose of this dredging project was
to remove sediment containing over 2 milligrams per kilogram (mg/kg) of PCBs or
0.45 mg/kg of C-66. This cleanup goal is derived from a risk assessment and is
necessary to protect human health based on fish consumption.

OCC submitted a plan for dredging activities in March 2003, entitled "Final
Dredging Design for Dredging White Lake Sediment Near the Occidental
Chemical Corporation Site in Montague, Michigan" (Dredging Design). A second
plan, "Final Dewatering Design for Dredging White Lake Sediment" (Dewatering
Design), March 2003, describes the final design for dewatering and disposing of
sediment after it is removed from White Lake. Both plans were approved by EPA.

Miller Springs Remediation Management, Inc. (MSRMI), managed the dredging
project for OCC. The dredging contractor was Faust, Inc. (Faust), and sediment
sampling and turbidity monitoring was provided by Earth Tech, Inc. (Earth Tech).
Earth Tech also operated the dewatering area and associated water treatment plant.
Field mobilization for the dredging began in June 2003, as described in the
Dredging Design. Dredging was performed from July 21 to September 10,2003.

2.1 Dredging Design

Sediment was characterized prior to developing the Dredging Design. The total
amount of sediment to be dredged to meet the cleanup goal was 8,500 cubic yards.
Approximately 1,300 cubic yards of sediment was found to contain PCBs with
concentrations over 50 mg/kg [the regulatory level for management as Toxic
Substances Control Act (TSCA) PCB remediation waste]. Hie sediment dredge
zone was divided into five subsections where PCB concentrations exceeded
50 mg/kg. Each subsection was one to two-feet in thickness.

The Dredging Design discussed the proposed dredging equipment and dredging
sequence, surface water quality monitoring plan, bathymetric survey and bottom
terrain modeling, confirmation and post-removal verification sampling plans, and

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equipment decontamination procedures.

2.1.1	Dredging Equipment

Sediment was dredged using a cable crane equipped with a Cable Arm
environmental bucket. The crane was mounted on a barge with a flat work deck
and positioned within the dredging area by anchorage cables. The position of the
barge was changed by varying the length of the anchorage cables using on-board
winches. Once the bucket was closed, sediment contained in the bucket was
raised to the surface. The operator attempted to ensure that free water remained
above the sediment such that sediment was not released through vents in the
bucket after closure. The bucket assembly was equipped with an alarm, which
would sound to notify the operator if the bucket failed to close completely.

The bucket was lowered using a slow, controlled descent. A differential global
positioning system (GPS) placed on the cable crane boom tip determined the "x"
and "y" coordinates of the bucket (areal location), while a pressure transducer
mounted on the bucket to measured the depth (the "z" coordinate). A shoreline
benchmark allowed the dredge to reference a fixed elevation, rather than a water
depth, and provided a consistent control point for the removal operation. The
bucket was also equipped with Windows operating system Offshore Positioning
System (WINOPS), a dredge positioning and location tracking software. Pressure
transducers and echo sounders attached to the pivot axle of the bucket measured
the distance of the bucket cutting lip to the lake bottom, to within two inches of
accuracy. Readings from these instruments were recorded on the WINOPS data
logger.

2.1.2	Surface Water Quality Monitoring Plan

The surface water quality in White Lake was monitored at five locations and two
depths (10 total monitoring points) to document whether the dredging activities
altered the water quality in the lake. Four locations were placed approximately
300 feet from the boundary of the dredging area to monitor turbidity, and one
location was placed 800 feet north of the dredging area to monitor background
turbidity in the lake.

A thermocline develops in summer at White Lake, which causes substantial
differences in shallow and deep water quality parameters, including turbidity.

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Therefore, at each of the five locations, turbidity monitoring equipment was
installed approximately 10 feet below the lake surface (above the thermocUne) and
10 feet above the bottom of the lake (below the thermocline). A temperature
survey was conducted to determine the depth of the thermocline in the lake prior
to the start of dredging, and water temperatures were re-measured periodically
during dredging. A turbidity monitor was set to record turbidity every 10 minutes
at each location. Monitoring began seven days before the start of dredging
activities to record background turbidity values.

The turbidity values were compared to the greatest of the following values:

•	Two times the pre-dredging background;

•	Two times the current background during dredging; or

•	A value of 20 nephelometric turbidity units (NTUs), which represented
the upper range of the approximate background levels from turbidity
measurements in April 2002.

Actions taken when turbidity measurements exceeded the criteria are discussed in
Section 3.1.

2.1.3	Bathymetric Surveys and Bottom Terrain Modeling

An initial bathymetric survey was performed before dredging began to map the
approximate lake bed elevations. Daily bathymetric surveys of the dredging were
performed to evaluate the accuracy of the WINOPs dredge positioning software.
A post-dredge survey was performed and compared to the initial survey to confirm
the total volume of sediments removed. The data were collected on survey lines of
20-foot spacing, to provide adequate resolution for bathymetry maps and cross-
sections.

2.1.4	Dredging Sequence and Confirmation Sampling

Contaminated sediment was dredged in one-foot intervals using the Cable Arm
environmental bucket, as measured by the on-bucket instruments and the WINOPS
dredging software package. Prior to beginning, a dredging pattern was developed
for each area, which outlined the targeted bucket contact locations and degree of
overlap between those locations. The planned dredging sequence consisted of
three phases to maintain separation of TSCA and non-TSCA sediment.

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Dredging activities were generally performed six days a week between the hours
of 7 AM and 7 PM. During Phase I of the dredging, one to two feet of non-TSCA
material that overlaid a known TSCA layer of sediment was removed. Phase I
began on July 21 and ended on August 1. Approximately 2,521 cubic yards of
non-TSCA sediment was dredged.

In Phase II, the known TSCA layer was removed. The dredging was completed
August 8 and approximately 1,334 cubic yards of TSCA sediment was dredged.
After allowing the suspended particles to settle for 24 hours, Earth Tech collected
15 TSCA boundary confirmation samples on August 11,2003 using a Ponar
dredge. These samples were collected to demonstrate that the remaining sediment
contained less than 50 mg/kg of PCBs and was not a PCB remediation waste. The
confirmation sample point coordinates were entered into the GPS unit, and the
Ponar was lowered to the bottom of the lake when the boat was positioned over
the sample collection point. Once the Ponar reached the bottom of the lake, it was
closed, and the sample was pulled to the surface.

The TSCA boundary confirmation sampling showed that two areas had sediment
containing greater than 50 mg/kg of PCBs. The two areas were re-dredged on
August 12 and confirmation sampling on August 14 showed that no PCB
remediation waste remained.

The final one-foot layer was removed in Phase III of dredging. This work was
completed on August 26 and an estimated 4,506 cubic yards of non-TSCA
sediment was dredged. A total in-place volume of 8,361 cubic yards of sediment
had been removed by August 26.

2.1.5 Post-Removal Verification Samples

Earth Tech collected 32 post-removal verification samples beginning on
August 28 after completion of the Phase III dredging. The dredge area was
evaluated using a grid of approximately 100-foot by 100-foot spacing, creating
eight polygons. Each of these eight polygons was further divided into four quarter
sections. Samples were collected within each quarter section with a petite Ponar
sampler lowered and raised manually.

If adequate sample volume was not obtained in the first pass, additional sediment
was collected using the petite Ponar. The samples were emptied into a stainless

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steel bin, collected in groups of four or five and then transported to the shore for
sample packaging.

Twenty-two of the 32 samples collected on August 28 contained over 2 mg/kg of
PCBs. No samples contained over 0.45 mg/kg of C-66 and the cleanup of C-66
was complete. Additional dredging was performed from September 3 through 6
and September 9 and 10. Verification sampling performed on September 11
confirmed that no sediment contained over 2 mg/kg PCBs and dredging was
complete. A total of 10,500 cubic yards (in-place) of sediment was dredged from
White Lake.

2.2 Dewatering Design

The Dewatering Design describes the planned methods for transfer of sediment to
the dewatering area and management, including:

•	Sediment dewatering

•	Containment of sediment during and after dewatering

•	Treatment of water removed from sediment

•	Dewatered sediment handling, transportation, and disposal

•	Decontamination procedures

•	Air monitoring.

2.2.1 Sediment Transfer to the Work Area

Sediment was transferred from the dredging barge to the dewatering area through
the use of the two methods described in the Dredging Design. The sediment was
deposited from the Cable Arm environmental bucket into a transfer barge, which
transported the sediment to an unloading station on a loading barge. The
sediments were transferred from the transfer barge by a hydraulic material handler
with a sealed clamshell bucket. The area beneath the swinging bucket on the
transfer barge and the loading barge was covered with a steel drip pan, which was
also used for setting aside the large dredged debris. The material was loaded into
trucks through a hopper. Spilled material was contained, loaded into trucks, and
transferred to the pumping station.

Trucks transported the dredged material to a pumping station. The trucks had a
sealed tailgate and drip overflow protection. A chute was created for the tailgate

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of the truck, which was fitted to the opening of the sump pump. Any sediment
material that did spill was containerized at the pump station and then transferred to
the dewatering area by truck. The majority of sediment was transported to the
dewatering area by being pumped through a pipeline, which extended under Old
Channel Trail and led to the western end of the dewatering area.

During the week of August 4, 2003, a pipeline was installed to pump water from
the transport barge to the pumping station. This reduced the truck loads of
dredged material transported up the hill to the pumping station. The pipeline was
controlled by four valve units.

2.2.2 Dewatering

Geotubes constructed of woven polypropylene geosynthetic material were used to
dewater the sediment, as described in the Dewatering Design. Nine Geotubes,
each 200 feet long and 45 feet in circumference, were constructed in three
containment areas at the dewatering area. Each containment area contained the
Geotubes, a filtrate collection sump, and wastewater treatment equipment. The
containment pads were lined with 60 milli-inch (mil), double-textured, high
density polyethylene (HDPE) geomembrane, and had continuous, two-foot high
perimeter berms to contain water discharged from the Geotubes and prevent storm
water run-on. The containment pads were sloped to one end, where the collected
water drained to a lined collection ditch. The ditch then conveyed the water to the
filtrate sump, located in an adjacent lined pond. Drainage nets were placed
beneath the Geotubes to protect the membrane liners and enhance drainage.

Separate Geotubes were used for TSCA and non-TSCA sediment. MSRMI
anticipated that a total of seven Geotubes would be required to contain all of the
dredged sediments, but constructed one additional for each type of sediment. The
Geotube containment area and water treatment system can accommodate up to
13 Geotubes. Each Geotube was connected to the common distribution header
connected to the slurry transfer pipe, but had a dedicated control/check valve.

A low-charge cationic polymer was injected into the slurry transfer line before the
slurry reached the Geotubes to promote flocculation of the sediment solids and
retention of the contaminants within the solids. A polymer injection system
controlled the dose rate and concentration of the polymer in the slurry.

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The sediment slurry was pumped into one Geotube at a time, reaching m initial
height of six feet An operator, in direct communication with the slurry pump
operator, was present at all times to ensure that the Geotubes were not overfilled.
The majority of excess water was discharged from the Geotubes within 24 hours
of filling, and additional slurry was added to the Geotube. Each Geotube was
typically filled three times to meet its design capacity of approximately seven feet
in height.

2.2.3	Water Treatment

The water treatment plant was installed on a containment pad located on the road
separating the Geotube containment pad from the filtrate sump. This pad was
lined with 60-mil, double-textured, HOPE geomembrane and sloped toward the
filtrate sump. The filtration basin contained two submersible pumps that
transferred water from the sump into the water treatment system. Filtrate collected
in the sump was first processed through pressure sand filters to remove suspended
sediments, then further treated by activated carbon adsorption to remove soluble
organic compounds. After treatment, the water flowed by gravity to the National
Pollutant Discharge Elimination System (NPDES)-permitted outfall discharging to
White Lake.

2.2.4	Handling and Disposal of Dewatered Sediment

Sediment dewatering is expected to be completed in November 2003. At that
time, the Geotubes will be cut open and dewatered sediment will be loaded into
trucks and disposed off-site. TSCA sediment and non-TSCA sediment will be
managed separately and disposed at appropriately permitted landfills.

2.3 Decontamination Procedures

The dredge and sediment transport equipment was decontaminated after removal
of the TSCA sediment by washing down the sides of the dredging transfer barge
and bucket and flushing the transport system with lake water. The wash water was
directed to the water treatment plant at the dewatering area (see Section 2.2.3
above). The truck beds and side walls of trucks used to transport dredged
sediments to the dewatering site were decontaminated using the same procedures.

For the sediment slurry transfer system, a volume of non-TSCA sediment and

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water equal to the full length of the pipeline was then flushed through the transfer
system and directed to one of the PCB remediation waste Geotubes. The transfer
barge, trucks, and slurry line were further decontaminated by processing at least an
additional 500 cubic yards of sediment that was not classified as PCB remediation
waste. Similarly, the dredge bucket was decontaminated by processing this
500 cubic yards of sediment.

2.4 Air Monitoring

Air monitoring was performed at four locations near the dewatering facility
(upwind, downwind, and in the direction of the nearest residences) to ensure that
the air leaving the facility did not contain constituents harmful to people adjacent
to the Facility. The air was monitored for PCBs and asbestos (asbestos was found
to be present in the sediment).

Ambient air concentrations of asbestos, PCBs, and dust [as particulate matter less
than 10 microns (PM10)] were monitored for two days before dredging and
dewatering began to obtain estimated site background concentrations. Once
filling of the Geotubes began, air samples were collected daily for seven days and
compared to the air toxics screening levels and other relevant criteria developed
by the Michigan Department of Environmental Quality (MDEQ). Activities
generating particulate emissions (which also could have contained asbestos and/or
PCBs adsorbed to the dust) were evaluated and changed if any parameters
exceeded the MDEQ screening levels. The ambient data did not exceed two times
the site background levels or the MDEQ screening levels during the first week of
monitoring; therefore, the monitoring frequency was decreased to weekly
thereafter.

Assessment monitoring to determine occupational exposure to workers at the site
was also performed as outlined in the Site Health and Safety Plan.

3.0 PROBLEMS ENCOUNTERED AND RESPONSE ACTIONS TAKEN

A few problems were encountered which were not anticipated in either the
Dredging or Dewatering Designs.

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3.1 Turbidity

Several turbidity exceedances occurred in White Lake during the dredging project
The first abnormal turbidity reading occurred on Wednesday, July 30, 2003, from
3:00 AM to 5:30 AM. The turbidity readings increased considerably during this
time period; however, dredging was not taking place during this time and had been
halted at least eight hours prior to this increase. The increase in turbidity appeared
not to be caused by dredging activities but by biological activities within the water
column.

Earth Tech personnel observed gradual increases in the turbidity measurements
and were informed by the instrument manufacturer that the lens on the monitors
should be cleaned on a regular basis. When the monitors were first cleaned, an
algal layer was removed, as well as small zebra mussel larvae. Thereafter, the
monitors were cleaned on a regular basis to remove zebra mussel larvae, algal
growth, and small zebra mussel shells.

During the weekly cleaning performed during the week of August 18, 2003,

Earth Tech observed that the wires on the turbidity monitors were rubbing on the
polyvinyl chloride (PVC) pipe housing, causing fraying. Monitors at four
locations were fixed to prevent rubbing and reconnected; however, the monitor at
one location could not be immediately repaired. The background turbidity
monitors were temporarily relocated to this location at the dredging area so that
dredging could continue.

3.2 Large Dredged Material

During dredging activities, large material (debris) was encountered, including
support beams to a deck and tires. Dredged material was loaded into the truck
beds through a hopper, which had a screen to recover large material prior to
entering the truck and prevent damage to the pumping system. The material
blocked by the hopper screen was removed from the screen into a dumpster on the
loading barge. Large material was also moved directly from the transport barge
and set to the side on the loading barge. When the dumpster filled and/or there
was large material (deck support beams) on the loading barge, a smaller roll-on
dumpster was moved onto the loading barge, and the materials were placed into
this dumpster.

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On August 25, 2003, a roll-off dumpster was filled with large material and moved
for storage to the northeast of the loading barge, at the end of the gravel area at the
bottom of the road. As the roll-off dumpster was unloaded from the truck, the
cable from the truck to the dumpster broke and some of the dredged material
spilled out of the back of the dumpster. Prior to unloading the roll-off dumpster, a
plastic liner had been placed over the area on which the dumpster was to be
placed. When Faust personnel attempted to move the container, the sliding action
tore the plastic liner, and som e of the impacted material leaked through onto the
ground.

The material released to the underlying gravel and dirt was placed in the roll-off
dumpster by means of a skid-steer loader, with a vertical lift path. The remaining
spilled material and concrete mix, along with the dumpster, was covered with a
clear plastic liner on the same day. On August 27,2003, the skid-steer loader was
used to load a majority of the remaining spilled material into an empty, lined
dumpster. Materials that did not fit into this dumpster, mainly the dirt and gravel
underlying the liner, was stockpiled until it could be placed in another dumpster.
Earth Tech took a confirmation sample during the week of September 1, 2003,
to verify the cleanup.

In order to prevent future spillage of material from the small dumpsters, a large
roll-off dumpster was placed on the loading barge. Within this dumpster, large
debris and dredged material was mixed with concrete, and this mixture was then
loaded into several smaller roll-off, plastic-lined dumpsters. Once the smaller
dumpsters were loaded and the waste inside was tested for disposal classification,
they were covered with plastic liners. The plastic liners were then tied down and
sandbagged to secure them in place.

3.3 PCB Exceedances in Treated Water Effluent

Earth Tech collected samples of the treated water effluent periodically during the
treatment system's operation. On August 11, 2003, analytical results from the
previous week's sampling were received from the laboratory and reviewed by
Earth Tech personnel. These results showed the PCB concentration in the effluent
exceeded the discharge limit in the NPDES permit. Discharging of water was
halted, and Earth Tech installed additional treatment equipment and processes, as
discussed below..

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Earth Tech subsequently determined that algal growth on the surface of the
Geotubes and within the containment pond contributed to the increase in total
PCB concentrations in the effluent. Earth Tech then installed an alum injection
pump and a polymer injection pump system ahead of the existing treatment
system. After testing the water through the new treatment train, the water effluent
still exceeded the requirements of the NPDES permit. Earth Tech altered the
treatment train in various manners, in order to attempt to meet the requirement of
the NPDES permit. The final treatment system configuration routed raw effluent
from the containment pond, through the alum injection pump, then the polymer
injection pump, and then into a series of four frac tanks. The frac tanks acted as a
clarifying system, and the time it took for the water to travel through the frac tanks
provided time for the alum and polymer to flocculate, coagulate, and settle
suspended solids out of the water. For polishing, the water was next pumped into
sandbags, through a 1-micron (jam) filter, and finally through four activated
carbon filters (previously only two of the carbon filters on site were utilized).
On August 29,2003, Earth Tech received compliant results from the final
treatment effluent samples and was able to resume discharging treated water
through the NPDES outfall.

3.4 Water Containment

While the water treatment system was not discharging due to the problems
described above, the water level within the containment pond increased as the
sediment slurry continued to be pumped into the Geotubes. The water level
reached between five feet six inches and six feet, or approximately two feet below
the top of the berm surrounding the containment pond. In order to continue
dredging sediment, Earth Tech proposed to develop a second containment pond to
the east of the already existing containment pond. The area of the proposed
second containment pond was a previous concrete containment structure. Earth
Tech lined this concrete containment structure with clean sand, and then American
Liners lined the second pond with 60-mil, double-textured BDPE geomembrane
and constructed continuous, two-foot high perimeter berms.

Originally, discharged water from the Geotubes had entered the first containment
pond through a spillway. Once the second (new) pond was developed, this
spillway was dammed with sandbags, and water was pumped from the spillway
reservoir into the new containment pond. During construction of the new
containment pond, water was pumped from the first containment pond into several

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20,000-gallon lined frac tanks for temporary holding. Once the treatment effluent
met the NPDES permit standards and treated water was discharged, water from the
frac tanks was emptied into the new containment pond. During this time, water
was also pumped from the first containment pond, to the western end of the
dewatering area. Earth Tech believed pumping this water to the end of the
dewatering area would promote evaporation as the water traveled east, downward
to the first containment pond.

4.0 SUMMARY

Approximately 10,500 cubic yards of contaminated sediment was removed from
White Lake between July 21 and September 10, 2003. As a result, over 1,100
pounds of persistent, bioaccumulative, and toxic compounds such as PCBs and
hexachlorobenzene were removed from the White Lake environment. Long-term
fish monitoring will be conducted over the next 10 years to evaluate the
environmental success of the dredging project.

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